ML20203D727

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Forwards Insp Rept 50-289/97-09 on 970907-1101.Apparent Violations Being Considered for Escalated Enforcement Action.Conference Scheduled for 971215
ML20203D727
Person / Time
Site: Crane Constellation icon.png
Issue date: 12/02/1997
From: Hehl C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Langenbach J
GENERAL PUBLIC UTILITIES CORP.
Shared Package
ML20203D733 List:
References
50-289-97-09, 50-289-97-9, EA-97-533, NUDOCS 9712160275
Download: ML20203D727 (3)


See also: IR 05000289/1997009

Text

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December 2, 1997

EA No. 97 533

Mr. James Langenbach

Vice President and Director, TMl

GPU Nuclear Corporation

Three Mile Island Nuclear Station

Post Office Box 480

Middletown, PA 17057 0191

SUBJECT:

NRC INTEGRATED INSPECTION REPORT NO. 50 289/97 09

Dear Mr. Langenbacn:

-This lette, refers to the NRC inspections conducted between September 7 and November

1,1997, at your Three Mile island 1 reactor facility. The inspections focused on nuclear

safety during the conduct and completion of the 12th refueling outage, in the areas of

operation, maintenance, engineering and plant support. The ins,aectors included resident

and regional based personnel. The enclosed report presents the results of the inspections.

Overall your staff conducted the outage activities safety. Operators controlled plant

conditions effectively and conducted a well planned and coordinated plant restart.

Maintenarice and surveillance activities went on properly, including the replacement of

control rod drive mechanism thermal barriers to avert future slow control rod drop times

and the inspection of all high pressure injection thermal sleeves and needed repairs to one.

Engineering performed well, as exemplified by the identification that the power operated

relief valve on the pressurizer was inoperable durin0 the prior operating cycle and in the

development and accomplishment of a modification to enhance the closure capability of

the outboard reactor coolant letdown containment isolation. The Inspectors also found the

core flood system maintained in good material condition and that the associated design

basis adequately reflected the current system operatlag parameters. The outage

radiological controls generally met acceptable staridards. Controls over the protected area

boundary improved since the last outage.

Despite the overall good performance severalissues developed that appeared to reflect

poorly on personnel performance in tS areas of operations, maintenance, and radiological

controls. As such, the inspection report identifies four apparent violations that we are

considering for escalated enforcement action in accordance with the " General Statement of

Policy and Procedure for NRC Entorcement Actions " (Enforcement Policy), NUREG-1600.

Specifically: 1) A licensed senior reactor operator directed that a reactor coolant system

fill flowpath, not allowed by the governing procedure, be used to increase the fill rate.

This resulted in an uncontrolled spill of water from the control rod drive mechanism vents,

before the unauthorized fill path could be secured. 2) Your staff found that the pressurizer

power operated relief valve had been inoperable since the last refueling outage, which

ended in October 199Q.nThis condition resulted from a wiring error and the failure to

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Mr. James Langenbach

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conduct a post maintenance test to verify operability. This issue concerned the NRC staff

because of the inability to use this valve during emergency procedure evolutions, to contro!

reactor coolant system pressure. 3) During once through steam generator tube

inspections, contract personnel left a locked high radiation area boundary unlocked. This

incident seemed similar to previous problems with locked area and radiological boundary

controls. 4) Following work in the fuel transfer canal, after refueling, a worker became

contaminated by a rodioactive particle, due to an apparent failure to conduct detailed

suivoys and take actions to control the spread of radioactive particles. Accordingly no

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Notices of Violation are presently being issued for these inspection findings, in addition,

please be advised that the number and characterization of these apparent violations may

change because of further NRC review.

A predecisional enforcement conference (conference) to discuss the api

nt violations

has been scheduled for December 15,1997. The decision to hold a coni ince does not

mean that the NRC has determined that violations have occurred or that ei.lorcement

action will be taken. This conference in being held to obtain information to enable the NRC

to make an enforcement decision, such as a common enderstanding of the facts, root

causes, missed opportunities to identify the apparent violations sooner, corrective actions,

significance of the issues, and tne need for lasting and effective corrective actions. In

addition, the conference will be an opportunity for you to point out any errors in our

inspection report and for you to provide any information concerning your perspective on 1)

the severity of the apparent violations, 2) the applicability of the factors that the NRC

considers when it determines the amount of a civil penalty that may be assessed in

accordance with Section VI.B.2 of the Enforcement Policy, and 3) any other application of

the Enforcement Policy to thesc cases, including the exercise of discretion in accordance

with Section Vll.

At the conference we would also like to discuss the Unresolved item dealing with your

management's decision to enter the mid loop condition with only one means of decay heat

removal available. While allowed by the Technical Specifications, this evolution appeared

to reflect a poor safety interpretation of the bases for the Technical Specifications and poor

minimization of shutdown risk.

Following the conference we will advise you by separate correspondence of the results of

our deliberation on tlase matters. No response regarding these apparent violations is

required at this time.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter

and its enclosures will be placed in the NRC Public Document Room (PDR).

Sincerely,

,

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Charles W. Hehl, Director

Division of Reactor Projects

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Mr. James Langenbach

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Docket No.: 50 289

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License No.: DPR 50

Enclosure:

NRC Inspection Report No. 50 289/97 09

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cc w/ encl:

J. C. Fornicola, Director. Nuclear Safety Review

M. J. Ross, Director, Operations and Maintenance

D. Smith, rnMS Manager

TMI Alert (TMIA)

M. Laggart, Manager, TMl Regulatory Affairs

E. L, Blake, Shaw, Pittman, Potts and Trowbridge (Legal Counsel for GPU,N)

Commonwealth of Pennsylvania

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Distribul!Qn_wlencit

Region 1 Docket Room (with concurrences)

Nuclear Safety Information Center (NSIC)

PUBLIC

NRC Resident inspector

H. Miller (RA)/W. Axelson, ORA

T. Kenny,DRS

P. Eselgroth, DRP

D. Haverkamp, DRP

N. Perry, DRP

A. Linde, DRP -

Distribution w/enci (VIA E MAIL):

W. Dean, OEDO

P. Milano, NRR, PDI 3

B. Du:kley, PM, NRR, PDI 3

L. Thonus, NRR

3. Weiss, NRR

R. Correia, NRR

F. Talbot, NRR

DOCDESK

Inspection Program Branch, NRR (IPAS)

DOCUMENT NAME: G:\\ BRANCH 7\\TMi\\lR97 09

To receive a copy of this document. Indicate in the box: "C" = Copy without

attachment / enclosure

"E" = Copy with attachment /enclosyreh,"N" = No copy

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