ML20202C746

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Forwards Insp Rept 50-263/97-18 on 971125-980112.No Violations Noted.Two Discrepancies Identified Between as- Built Plant Condition,Ts & USAR
ML20202C746
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 02/04/1998
From: Grant G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Wadley M
NORTHERN STATES POWER CO.
Shared Package
ML20202C752 List:
References
50-263-97-18, NUDOCS 9802130018
Download: ML20202C746 (2)


See also: IR 05000263/1997018

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NUCLEAR RE ULATORY COMMISSION

UNITO STATES

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801 WARRENVILLE nOAD

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LISLE. ILLINOIS 60532-4351

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february 4,1998

Mr. M. Wadley, Vice President

Nuclear Generation

Northom States Power Company

414 Nicollet Mall

Minneapolis, MN 55401

SUBJECT:

MONTICELLO NRC INSPECTION REPORT NO. 50 263/97018(DRP)

Dear Mr. Wadley;

On January 12,1998, the NRC completed an inspection at the Monticello reactor facility. The

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enclosed report presents the results of that inspection.

During the seven week period covered by this inspection, the conduct of activities at the

Monticello facility was acceptable. For example, operations personnel responded appropriately

to a loss of both recombiner trains and a resultant manual reactor scram. The subsequent

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reactor startup and two planned power changes were completed in a controlled rnanner.

Engineering personnelidentified that a Technical Specification required test was not performed

en an automatic depressurization system initiation inhibit switch. Radiation protection personnel

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demonstrated a strong commitment in reducing personnel exposure during a maintenance

activity in a high dose area. However, inadequate planning on two occasions for performance of

a surveillance test and maintenance activity resulted in generation of a reactor scram signal for

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13 control rods and a reactor water level transient. Planning, maintenance, and operations

personnel did not consider the compatibility of performing activities simultaneously.

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During this period, the inspectors identified two discrepancies between the as built plant

condition, Technical Specifications, and the Updated Safety Analysis Report. Although these

findings were not safety significent, they indicate technicat inconsistencies between design

documents. We understand that your staff is involved in an effort to validate the Updated Safety

Analysis Report and we encourage you to continue to su2 port this effort.

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9002130010 990204

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ADOCK 05000263

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M. Wadley

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In occordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter and its

enclosure will be placed in the NRC Public Document Room.

Sincerely,

/s/ Marc L. Dapas for

Geoffrey E. Grant, Director

Division of Reactor Projects

Dock 6, No.: 50-263

License No.: DPR 22

Enclosure:

Inspection Report

No. 50 263/97018(DRP)

cc w/ encl:

Plant Manager, Monticello

State Liaison Officer, State

of Minnesota

Distribution:

Docket File w/ encl

Rlli PRR w/ encl

PUBLIC IE 01 w/ encl

Project Manager, NRR w/enct

SRI Monticello w/ encl

Rlli Enf. Coordinator w/enct

A. B. Beach w/ encl

CAA1 w/enet (E rnell)

Deputy RA w/enci

DRS (2) w/ encl

TSS w/enci

DOCDESK (E mail)

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DRP w/ encl

DOCUMENT NAME: G:\\MONT\\ MON 97018.DRP

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DATE

02/;L/98

02/%/98

02/3 /98

OFFICIAL RECORD COPY