ML20195D078

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Insp Rept 50-267/86-16 on 860506-0509.Violation Noted:On 860506,reactor Power Level Drifted Above Authorized Limit
ML20195D078
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 05/22/1986
From: Farrell R, Jaudon J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20195D075 List:
References
50-267-86-16, NUDOCS 8606020088
Download: ML20195D078 (5)


See also: IR 05000267/1986016

Text

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APPENDIX

U.S. NUCLEAR REGULATORY C0fittISSION

REGION IV

NRC Inspection Report:

50-267/86-16

License: DPR-34

Docket: 50-267

Licensee: Public Service Company of Colorado (PSC)

P. O. Box 840

Denver, Colorado 80201

Facility Name:

Fort St. Vrain Nuclear Generating Station

!

Inspection At:

Fort St. Vrain Nuclear (FSV) Generating Station, Platteville,

Colorado

Inspection Conducted: May 6-9, 1986

Inspector-

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. {. F[rrell, Senior Resid t Inspector (SRI)

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Approved:

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Inspection Sunnary

Inspection Conducted May 6-9, 1986 (Report 50-267/86-16)

Areas Inspected: Special, unanr.ounced inspection of operation in excess of

duthorized power limit.

Results: Within the areas inspected, one violation was identified

(paragraph 2).

8606020088 860523

PDR

ADOCK 05000267

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2

DETAILS

1.

Persons Contacted

Principal Licensee Employees

  • H. Brey, Manager, Nuclear Licensing and Fuels
  • M. Deniston, Shift Supervisor
  • D. Evans, Superintendent Operations
  • J. Gahm, Manager Nuclear Production
  • D. Rodgers, Planning & Scheduling Manager
  • J. McLotter, Lawyer, Kelly, Stansfield, and O'Donnell
  • R. Walker, President and Chief Executive Officer

NRC/NRR Personnel

  • F. Allenspach, Reactor Systems Engineer
  • R. Farrell, Senior Resident Inspector
  • J. Gagliardo, Chief, Reactor Projects Branch
  • R. Ireland, Chief, Engineering Section
  • J. Jaudon, Chief, Reactor Projects Section A
  • E. Johnson, Director, Division Reactor Safety Project
  • D. Powers, Enforcement Officer
  • M. Skow, Project Engineer

The SRI also contacted other licensee and contractor personnel during

the inspection.

  • Denotes those in attendance during the Enforcement Conference held in

Arlington, Texas on May 9,1986.

2.

Operation in Excess of Authorized Power Limit

At 1009 MDT, on May 6, 1986, the NRC SRI was contacted by FSV operations

management and informed that there had been a small perturbation with the

reactor.

The SRI was infornied that based on preliminary information then

available, the reactor power level had " drifted" above 35% power to a

possible maximum of 40% power. The SRI, was additionally told, that the

time above 35% power was approximately 10 minutes. The following is a

narrative description of the actual event as determined from plant

personnel interviewed, computer printouts, recorded plant parameters, and

inspection of control room strip chart recorders.

At 0820 MDT, on May 6,1986, the reactor was in steady-state operation

with the following parameters:

core power = 34.7%

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generator output = 90 megawatts electric

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core outlet temperature = 1207 F

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reactor pressure = 618 psia

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reactor coolant flow = 47%

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reactor coolant dewpoint = -42.6 F

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,

The licensee had been experiencing a hydraulic fluid leak on a

hydraulically operated steam isolation valve. The valve was on a main

steam bypass line which is used in startup, prior to admitting steam to

the high pressure turbine. With the turbine on line, this valve is

normally closed, and main steam follows its normal flow path through the

high pressure turbine. With the valve open, steam is bypassed to the

desuperheater and the flash tank and hence to the cold reheat steam line

without passing through the high pressure turbine. Cold heat steam drives

the circulators and then is reheated in the steam generator. A decision

had been made to remove hydraulic oil pressure from this valve and to

repair the hydraulic fluid leak, utilizing a downstream pressure control

valve as the steam isolation valve because the licensee anticipated that

the isolation valve could drift open when hydraulic fluid pressure was

removed.

The pressure control valve in the main steam by-pass line was closed and

hydraulic fluid pressure to the isolation valve in this line was removed

to facilitate repair of the hydraulic fluid leak.

Following removal of

hydraulic fluid pressure from the main steam by-pass isolation valve, the

control room noted a step increase in feed water flow. Concurrenuy, the

control room received a Delta Temperature Alann between reactor Loop I and

reactor Loop II. That is, the steam coming from the steam generator for

one loop was at a temperature different than that from the other steam

generator. A shift supervisor who was acting as operations superintendent

Wds in the control room and directed the reactor operators to increase

helium circulator speed on the loop with the lower temperature to equalize

the steam outlet temperatures of the two steam generators. This increased

helium flow to the core, increasing heat removal from the core and raising

core power. At this point, the reactor was already above its authorized

power level of 35%, and operator actions taken were tending to increase

power level even further. The reactor was in the remote automatic control

mode, in which all control systems follow main turbine steam demand.

Following the step increase in feedwater flow, turbine generator power

increased, the center control rod (regulating rod) stepped out to mr *

turbine demand, and reactor power increased peaking between 42.6%

43.3% reactor power at approximately 0840 MDT.

The shift supervisoi

(acting operations superintendent) in the control room made the decision

to bring the plant down below its authorized power level of 35% in a " slow

controlled manner," rather than by scram of the reactor or by shifting the

control mode to local automatic to reduce power rapidly.

When the reactor operators noticed the turbine generator output had

increased from 90 megawatts electric to approximately 108 megawatts

electric, the shift supervisor directed them to reduce turbine generator

load demand in an attempt to reduce reactor power to within the authorized

operating limit of 35%. As the reactor operators reduced turbine

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generator demand, the regulating rod inserted, but reactor power continued

to increase as did feed water flow. The negative thermal coefficient of

reactivity inherent in the reactor core served to increase reactor power

as feedwater flow increased, and additional heat was removed from the

Core.

Control room personnel who were analyzing the event to determine why

feedwater flow and reactor power did not follow turbine generator demand,

identified the work on the main steam by-pass line valves as the apparent

cause. At this time maintenance was contacted, and hydraulic oil pressure

was restored to the main steam by-pass line isolation valve, causing that

valve to close. Reactor power dropped as did feedwater flow to correspond

to the power demanded by the turbine generator. At 0915 MDT, reactor

power was again below the authorized limit of 35%.

With the reactor in remote automatic control, the control loops in the

plant regulate equipment to match turbine generator load demand, taking

the signal from the high pressure turbine throttle pressure. When the

hydraulic pressure was removed from the main steam by-pass line isolation

valve, that valve partially opened, passing high pressure steam to the

by-pass line. The pressure control valve in the main steam by-pass line

was being relied upon to function as an isolation valve, even though it is

not designed to provide such service; this pressure control valve either

leaked or was not completely seated, and it passed high pressure steam.

The steam flow through the by-pass line reduced turbine throttle pressure

causing the control systems to demand more steam and power from the

reactor. Additionally, the steam passing through the flash tank and into

the reheat lines, increased reheat steam flow. Since a reheat steam flow

signal is utilized to control feed water flow, an increase in reheat steam

flow caused an increase in feed water flow. Consequently, the feedwater

system was getting an increase flow, signal from the turbine generator

control system, which was sensing an inadequate turbine throttle pressure

and was getting an increase feed water flow signal from reheat steam flow.

At the same time the turbine generator control system was demanding more

feedwater flow, it caused the regulating rod to withdraw, increasing

reactor power to match the turbine generator load demand. The increase in

feedwater flow cooled the reactor core and caused an increase in reactor

power due to the negative thermal coefficient of reactivity.

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The effect of the negative thermal coefficient of reactivity held reactor

power above 35% even as turbine generator load demand was reduced by the

reactor operators.

Reactor power returned to authorized levels when the

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flow through the main steam by-pass line was terminated, and the turbine

generator remote automatic controls were again sensing all of the steam

flow provided from the reactor.

The licensee, while operating at 34.7% reactor power with an authorized

,

reactor power limit of 35%, chose to do maintenance on a velve which had

the potential for effecting reactor power level. While doing this work,

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the licensee relied upon a pressure control valve, not designed as an

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isolation valve, to perform an isolation function. The pressure control

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valve utilized as an isolation valve was not tested for isolation

capability prior to relying upon it for isolation. When the first alarm,

the Delta T un main steam alarm, was received, the reactor operators were

directed to take action which increased reactor power in order to clear

the alarm.

The reactor was operated at power levels in excess of the authorized power

level from 0830 MDT, May 6,1986, to 0915 MDT, May 6,1986. Although

there was no apparent intention to exceed the authorized power level, the

licensee did choose to do maintenance on a valve which had the potential

to affect reactor power level without reducing reactor power level to

provide a margin of error in the event power level did increase.

Additionally, the licensee relied upon an untested valve to perform a

function for which it was not designed. When the licensee realized that

the reactor was not operating within the authorized power limit, the first

actions caused reactor power level to increase further. Additionally, the

licensee chose to remain at an unauthorized power level for 45-minutes

rather than manually scramming the reactor or quickly reducing reactor

power, risking an automatic scram.

Operating the reactor at power levels above 35% is an apparent violation

of the NRC Order of November 26, 1985, authorizing operation of the FSV

reactor at power levels not to exceed 35% (50-267/8616-01).

3.

Enforcement Conference

An Enforcement Conference was conducted on May 9, 1986, at the NRC Region

IV offices in Arlington, Texas. At that time, the events of May 6, were

reviewed and potential actions to prevent reoccurrence were discussed.

The meeting was attended by those indicated in paragraph 1.