ML20168A449

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Final ASP Analysis - Crystal River (LER 302-79-057)
ML20168A449
Person / Time
Site: Crystal River 
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1979-059-00
Download: ML20168A449 (4)


Text

B-640 PRECURSOR DESCRIPTION AND DATA NSIC Accession Number:

150882 Date:

June 6, 1979

Title:

Both Diesel Generators Trip During Testing at Crystal River 3 The failure sequence was:

1. During performance of Engineered Safeguards Time Response Test, both diesel generators tripped when loaded on the emergency buses due to am imbalance in reactive load.

Corrective action:

1. A procedure revision was implemented to eliminate the high MVAR and reduce thkc reactive load imbalance.
2. The diesel generators were surveilled daily from June 9 -

June 15 and per-formed satisfactorily.

Design purpose of failed system or component:

1. The emergency diesel-generators provide power to safety-related equipment in the event of loss of offsite power.

Unavailability of system per WASH 1400: *emergency power systems:

1 x 10-2 /D Unavailability of component per WASH 1400:

  • each diesel generator:ý 3 x 10- 2/D Unavailabilities are in units of per demand D.

Failure rates are in units of per hour HR'1.

Reactor in Refueling Diesel Generator A Diesel Generator B Shutdown and Engineered Started and Loaded Started and Loaded Safeguards Time Response Successfully Successfully Test in Progress Potential Severe Core Damage

.No w

No -

of fsite power available NSIC 150882 -

Actual Occurrence for Failure of Both Diesel Generators During Testing at Crystal River 3

Loss of Turbine Emer-Auxiliary PORV PORV or High Long Offslte Generator gency Feedwater and Demanded PORV Isola-Pressure Term Power Runs Back Power Secondary

.tion Valve Injection Core and Assumes Heat Removal Closure Cooling House Loads Potential Severe Core Damage No Sequence No.

2 3

4 5

6 7

8 9

10 11 12 13 0%

4-3 NSIC 150882 -

Sequence of Interest for Failure of Both Diesel Generators During Testing at Crystal River 3

B-643 CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUMBER:

150882 DATE OF LER:

June 27, 1979 DATE OF EVENT:

June 6, 1979 SYSTEM INVOLVED:

Emergency Electric Power COMPONENT INVOLVED:

2 Diesel Generators CAUSE:

Imbalance in reactive load, both DGs tripped, (human error)

SEQUENCE OF INTEREST:

Loss of off-site power ACTUAL OCCURRENCE:

Both DGs tripped during test REACTOR NAME:

Crystal River 3 DOCKET NUMBER:

50-302 REACTOR TYPE:

PWR DESIGN ELECTRICAL RATING:

825 MWe REACTOR AGE:

2.4 yr VENDOR:

B&W ARCHITECT-ENGINEERS:

Gilbert Associates OPERATORS:

Florida Power Corp.

LOCATION:

7 miles NW of-Crystal River, Fla.

DURATION:

360(a) hours PLANT OPERATING CONDITION:

0% power SAFETY FEATURE TYPE OF FAILURE: E~inadequate performance; (b) failed to start; (c) made inoperable; (d)____________

DISCOVERY METHOD:

Testing COMMENT:

-