ML20155E537
| ML20155E537 | |
| Person / Time | |
|---|---|
| Site: | Byron |
| Issue date: | 02/28/1988 |
| From: | Spitzer D COMMONWEALTH EDISON CO. |
| To: | |
| Shared Package | |
| ML20154J380 | List: |
| References | |
| NUDOCS 8806160135 | |
| Download: ML20155E537 (2) | |
Text
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i B.
OPERATING DATA REPORT DOCKET NO.:
050-453 UNIT:
Byron Two DATE:
03/10/88 COMPILED BY:
D. J. Spitzer TELEPHONE:
(815)234-5441 x2023 OPERATING STATUS 1.
Reporting Period:
February 1988. Gross Hours: 696
)
2.
Currently Authorised Power Level (MWt): 3411 i
Design Electrical Rating: 1175 (MWe-gross)
Design Electrical Rating: 1120 (MWe-net) 1 Max Dependable Capacity (MWe-net): NOT DETERMINED l
l 3.
Poder Level to Which Restricted (If Any): 1055 (Mwe-net) 1 4.
Reasons for Restriction (If Any):
Steam Generator Split Flow (65 MW) l THIS MONTH YR TO DATE CUMULATIVE
- 5.
Report Period Hrn.
696 1440 4633 6.
Rx Critical Hours 681.6 1425.6 3754.8 7.
Rx Reserve Shutdown Hours 0
0 0
8.
Hours Generator on Line 601.3 1345.1 3625.5 9.
Unit Reserve Shutdown Hours 0
0 0
- 10. Gross Thermal Energy (MWH) 1765813 3569270 10041434
- 11. Gross Elec. Energy (MWH) 577812 1183030 3287;41 1
- 12. Het Elec. Energy (MWH)
S43279 1109986 3080887
- 13. Reactor Service Factor 98 99 81
- 14. Reactor Availatility Factor 98 99 81
- 15. Unit Service Factor 86.4 93.4 78.3
- 16. Unit Availability Factor 86.4 93.4 78.3
- 17. Unit Capacity Factor (MDC net)
N/A N/A N/A
- 18. Unit Capacity Facter (DER net) 69.7 68.8 59.4 l
- 19. Unit Forced Outage Hrs.
25.2 25.2 313.2 1
- 20. Unit Forced Outage Rate 4
1.8 7.9
- 21. Sh \\ downs Sch' aled Over Next 6 Months:
- 22. If Shutdown at End of Report Period, Estimated Date of Startups 3/3/88
- 23. Units in Test Statub (Prior to Commercial Operation): None
- Note - The cumulative numbers do not reflect power generated 7 'ar to commerc Al 8
service.
(0625N/0062M-16) h!k knob 4
R
Csport Period February, 1988 UNIT SHUTDOWNS / REDUCTIONS BYRON (UNIT 2)
__Ilate___ Iype 5kour.s Benson Method LER_ Number System Component
__Cause & Correctite Action to Prevent Recurrence re.
3.
02/06/88 S A
5 CW Reduced load to allow for 2A CW box cleaning.
4.
02/'2/88 F 25.2 A
3 6-2-88-26 FW 2C FW Pp 20 Feedwater pump tripped - attempts to maintain SG level by running back the turbine failed.
5.
02/27/88 5 69.7 A
1 EH Took Unit 2 turbine off line to troubleshoot and repair EH system low pressure. Reactor at 12*. power.
4 cocoooce*******
O Summary
- ocooc*
e*******
"DfPE Reason Me.thod System & Component F-Forc;d A-Equip Failure F-Admin 1-Manual Exhibit F & H S-Sch2d B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refueling H-Other 3-Auto Scram Preparation of D-Regulatory Restriction 4-Continued Data Entry Sheet i
E-Operator Training 5-Reduced Load Licensee Event Report
& License Examination 9-Other (LER) File (NUREG-0161) 1 l
4
- (0625M/0062M-17)
- -