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Category:CORRESPONDENCE-LETTERS
MONTHYEARML17313B0991999-10-14014 October 1999 Forwards LER 99-005-00 Reporting Findings & Corrective Actions Taken as Result of Out of Tolerance MSSV Condition in Unit 1 Which Was Discovered During pre-outage Testing ML17313B0881999-10-12012 October 1999 Forwards Response to NRC 990831 RAI Re Several Relief Requests That Accompanied Second ten-yr Interval ISI Program Submitted on 980317.Revised Relief Request 6 Is Provided in Encl 2 ML17300B3501999-09-29029 September 1999 Forwards Revised Bases Pages,Providing Addl Discussion of Options Available to Exit Required Action G of TS 3.8.1 & Revised Page for TS 3.3.7,in Response to NRC RAI Re Proposed Amend to TS 3.8.1 & 3.3.7 ML17300B3551999-09-28028 September 1999 Responds to Aministrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. Proposed Palo Verde Operator Licensing Exam Schedule & Estimated Number of Applicants Planning to Take Exams Encl ML17313B0851999-09-24024 September 1999 Requests Approval of Alternative to Repair Requirements of 10CFR50.55a,authorizing Alternative Use of Mechanical Nozzle Seal Assemblies,As Described in Encl,For RCS Hot Leg Instrumentation & Sampling Nozzles for Two Operating Cycles ML17313B0781999-09-20020 September 1999 Forwards Rev 22 to PVNGS Emergency Plan. Summary Description of Changes,Included ML17300B3331999-09-14014 September 1999 Forwards MOR for August 1999 & Revised MOR for Jul 1999 for Pvngs,Units 1,2 & 3 ML17300B3351999-09-0808 September 1999 Informs That Repairs to Plant EDG 2A Jacket Water Cooling sub-sys Were Completed & EDG Was Declared Operable on 990903 at Approx 21:45 Mst.Noed Was Not Necessary,Since 72 Hour Completion Time Was Met ML17313B0761999-09-0303 September 1999 Requests Enforcement Discretion to TS Section 3.8.1, AC Sources - Operating. Enforcement Discretion Would Allow,On One Time Basis,Extension of Completion Time in Required Action B.4 of TS 3.8.2 from 72 H to 108 H ML17313B0731999-08-31031 August 1999 Informs That RR Bean (License OP-50452-1) Has Been Permanently Reassigned to Position That Does Not Require License & Requests That Individuals License Be Expired Per 10CFR55.55 ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML17313B0581999-08-0606 August 1999 Forwards Rev 1 of Changes to TS Bases Implemented Between Aug 1998 & Jul 1999.Insertion Instructions & List of Affected Pages Included ML17313B0311999-08-0303 August 1999 Submits Response to NRC AL 99-02, Operating Reactor Licensing Actions Estimates, for Fys 2000 & 2001 ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams ML17313B0431999-07-30030 July 1999 Advises of Listed Senior Mgt Changes That Have Taken Place at Plant ML17313B0441999-07-30030 July 1999 Forwards Comments on Draft NRC Repts Evaluation of AOVs at Us Light-Water Reactors (1999) & Idaho Natl Engineering & Environ Lab Rept (INEEL)EXT-98-00383,Study of AOVs in Npps. ML17313B0151999-07-20020 July 1999 Submits Request to Obtain All Data Previously Sent by PVNGS & Currently in REIRS for OLs NPF-41,NPF-51 & NPF-74.Data Is Requested in Electronic Form (Ascii Format) as It Currently Exists in REIRS Sys ML17313B0091999-07-20020 July 1999 Forwards Requested Calculations Performed to Verify That Increase in Max Radially Averaged Enrichment for Fuel Assemblies from 4.3 Weight Percent to 4.8 Weight Percent Did Not Affect Requirements for TSs 3.7.15,3.7.17 & 4.3.1 ML17313B0171999-07-16016 July 1999 Forwards LER 99-005-00,re Automatic Rt Which Occurred on 990618,following Sensor Failure in Core Protection Calculators.Corrective Actions Described in LER Are Not Necessary to Maintain Compliance with Regulations ML17300B3111999-07-15015 July 1999 Forwards PVNGS Unit 2 ISI Rept for Eighth Refueling Outage. No Commitments Made to NRC by Ltr ML17300B3141999-07-15015 July 1999 Forwards Corrected Electronic Files for Individual Monitoring Repts for 1998.Original Electronic Files Were Found to Have Two Administrative Errors,Which Has Been Corrected.Encl Withheld,Per 10CFR2.790 ML20209G6771999-07-0808 July 1999 Forwards Supplemental Info to Confirm That Decommissioning Funding Plans of Public Service Co of Nm for Interests in PVNGS Have Been Reviewed by Nm Public Regulation Commission. Final Order & Recommended Decisions in Case 2742,also Encl ML17300B2931999-07-0202 July 1999 Submits Withdrawal of Relief 5 for Second ISI Interval for Units 1,2 & 3.Proposed Alternative Is Related to Exam Requirements for Component Supports for Second ISI Interval ML17313A9951999-06-26026 June 1999 Provides Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML17300B2831999-06-26026 June 1999 Requests NRC Approval of Proposed Alternative IAW Provisions of 10CFR50.55a(a)(3)(i) to 10CFR50.55a(g) & Requirements of ASME Boiler & Pressure Vessel Code Section XI for Repairs & Installation.Description of Proposed Alternative,Encl ML17313A9901999-06-15015 June 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. No Commitments Being Made to NRC by Ltr ML17313A9521999-05-24024 May 1999 Notifies NRC That Ja Proctor,License SOP-50314,has Been Permanently Reassigned to Position That Does Not Require License.License Should Be Expired,Per 10CFR55.55 ML20206Q3111999-05-18018 May 1999 Final Response to FOIA Request for Documents.Forwards App a Records Being Released in Entirety ML17313A9311999-05-13013 May 1999 Notifies NRC That Rev 2 to COLR for Unit 2 Remains Applicable Following Recently Completed Unit 2 Reload ML17313A9481999-05-12012 May 1999 Informs of Change Needed in Order to Update Current Mailing List.Future Mailings for J Horne Should Be Forwarded to Listed Address ML17313A9261999-05-0707 May 1999 Forwards LER 99-004-00,per 10CFR50.73.LER Repts Findings & Corrective Actions Taken as Result of Unit 2 Out of Tolerance Pressurizer Safety Valve (Psv) Condition Which Was Discovered During Outage Testing ML20206H1931999-05-0303 May 1999 Forwards 1998 Annual Rept, for SONGS Units 2 & 3 & PVNGS Units 1,2 & 3.SCEs Form 10K Annual Rept to Securites & Exchange Commission for Fiscal Yr Ending 981231,encl ML17313A9091999-04-30030 April 1999 Forwards Proprietary Proposed Test Outlines for Initial License Exams to Be Administered at PVNGS in Aug/Sept 1999. No Commitments Are Contained in Ltr.Proprietary Info Withheld ML17313A9181999-04-30030 April 1999 Forwards Electronic File of Individual Monitoring Repts for 1998.Encl Withheld Per 10CFR2.790 ML17313A9191999-04-30030 April 1999 Forwards Special Rept 2-SR-99-001 Re SG Tube Plugging in PVNGS Unit 2,per TS Reporting Requirement 5.6.8.Complete Results of SG Tube Inservice Insp Will Be Submitted by 000422 ML17300B3751999-04-23023 April 1999 Forwards LER 99-003-00,reporting Condition Prohibited by TS 3.7.17 Where Spent Fuel Assembly Was Stored in Inappropriate Region in Spent Fuel Pool ML17313A9081999-04-23023 April 1999 Documents 990421 Telcon with E Emeigh,Which Requested Extension for Submitting Next Matl Balance Rept for Pvngs,As Required by 10CFR70.53 & 74.13.Required Info Will Be Submitted by 990531 ML20205T7421999-04-21021 April 1999 Forwards Partially Withheld Insp Repts 50-528/99-05, 50-529/99-05 & 50-530/99-05 on 990322-26.Determined That Security Program Properly Implemented.Insp Repts Details Withheld (Ref 10CFR73.21) ML17313B0271999-04-21021 April 1999 Forwards Proprietary Epec Pro Forma Cashflow Statement for 1999.Proprietary Info Withheld,Per 10CFR2.790.Affidavit Encl ML17313A9031999-04-21021 April 1999 Forwards Rev to Relief Request 12 Submitted 990420 to Second 10-yr ISI Interval.Revised Relief Request Discusses in More Detail Actions APS Will Take When There Is Identified Leakage from Bolted Connection ML17313A8971999-04-20020 April 1999 Requests Use of Alternatives to 10CFR50.55a(g) Inservice Insp Requirements.Proposed Alternatives Are Related to Visual Exam of Bolted Connections 05000529/LER-1999-002, Forwards LER 99-002-00 Re Findings & Corrective Actions Taken as Result of Plant Out of Tolerance MSSV Condition Which Was Discovered During pre-outage Testing1999-04-19019 April 1999 Forwards LER 99-002-00 Re Findings & Corrective Actions Taken as Result of Plant Out of Tolerance MSSV Condition Which Was Discovered During pre-outage Testing ML17313A8931999-04-14014 April 1999 Forwards LER 99-003,reporting Condition Prohibited by TSs That Existed When Surveillance Requirement to Verify Essential Chilled Water Sys Valve Positions Was Not Met ML20205Q0821999-04-13013 April 1999 Forwards Second ISI Interval Relief Request 10 from ASME Section XI & Applicable Addenda Re Visual Exams Performed Subsequent to Repair or Replacement of Component or Alteration of Item ML17313A8901999-04-13013 April 1999 Forwards LER 98-003-01 Re MSSV as-found Lift Pressures out- Side of TS Limits.Ler Suppl Provides Evaluation Findings from Unit 3 out-of-tolerance MSSVs Conditions Which Were Discovered During pre-outage Testing ML17313A8831999-04-0808 April 1999 Forwards 1998 Annual Radioactive Effluent Release Rept for Pvngs,Units 1,2 & 3 & Rev 13 to ODCM, for Pvngs,Units 1,2 & 3 IAW TS 5.6.3 ML20205F3491999-03-30030 March 1999 Forwards Proprietary & non-proprietary Info Re Status of Decommissioning Funding for Pvngs,Units 1,2 & 3,per 10CFR50.75(f)(1).Proprietary Info Withheld,Per Requirements of 10CFR2.790(b)(1) ML17313A8671999-03-24024 March 1999 Submits Info Re Present Levels & Sources of Property Insurance Maintained for Pvngs,Per 10CFR50.54(w)(3) ML17313A8601999-03-16016 March 1999 Forwards Revised Relief Requests PRR-05,PRR-06 & PRR-11 to Clarify That Proposed Design Flow Testing for Lpsi,Hpsi & Containment Spray Pumps Will Be Performed Using Instruments That Comply with Code Requirements,Per 990226 Telcon ML17313A8551999-03-0505 March 1999 Requests Proposed Code Alternative IAW 10CFR50.55a(e)(3),as Acceptable Alternative to Requirements of 10CFR50.55a(e)(1), for Installation of in-line safety-related Flow Measurement Instrument in ASME Class 3 Pipe 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17313B0991999-10-14014 October 1999 Forwards LER 99-005-00 Reporting Findings & Corrective Actions Taken as Result of Out of Tolerance MSSV Condition in Unit 1 Which Was Discovered During pre-outage Testing ML17313B0881999-10-12012 October 1999 Forwards Response to NRC 990831 RAI Re Several Relief Requests That Accompanied Second ten-yr Interval ISI Program Submitted on 980317.Revised Relief Request 6 Is Provided in Encl 2 ML17300B3501999-09-29029 September 1999 Forwards Revised Bases Pages,Providing Addl Discussion of Options Available to Exit Required Action G of TS 3.8.1 & Revised Page for TS 3.3.7,in Response to NRC RAI Re Proposed Amend to TS 3.8.1 & 3.3.7 ML17300B3551999-09-28028 September 1999 Responds to Aministrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. Proposed Palo Verde Operator Licensing Exam Schedule & Estimated Number of Applicants Planning to Take Exams Encl ML17313B0851999-09-24024 September 1999 Requests Approval of Alternative to Repair Requirements of 10CFR50.55a,authorizing Alternative Use of Mechanical Nozzle Seal Assemblies,As Described in Encl,For RCS Hot Leg Instrumentation & Sampling Nozzles for Two Operating Cycles ML17313B0781999-09-20020 September 1999 Forwards Rev 22 to PVNGS Emergency Plan. Summary Description of Changes,Included ML17300B3331999-09-14014 September 1999 Forwards MOR for August 1999 & Revised MOR for Jul 1999 for Pvngs,Units 1,2 & 3 ML17300B3351999-09-0808 September 1999 Informs That Repairs to Plant EDG 2A Jacket Water Cooling sub-sys Were Completed & EDG Was Declared Operable on 990903 at Approx 21:45 Mst.Noed Was Not Necessary,Since 72 Hour Completion Time Was Met ML17313B0761999-09-0303 September 1999 Requests Enforcement Discretion to TS Section 3.8.1, AC Sources - Operating. Enforcement Discretion Would Allow,On One Time Basis,Extension of Completion Time in Required Action B.4 of TS 3.8.2 from 72 H to 108 H ML17313B0731999-08-31031 August 1999 Informs That RR Bean (License OP-50452-1) Has Been Permanently Reassigned to Position That Does Not Require License & Requests That Individuals License Be Expired Per 10CFR55.55 ML17313B0581999-08-0606 August 1999 Forwards Rev 1 of Changes to TS Bases Implemented Between Aug 1998 & Jul 1999.Insertion Instructions & List of Affected Pages Included ML17313B0311999-08-0303 August 1999 Submits Response to NRC AL 99-02, Operating Reactor Licensing Actions Estimates, for Fys 2000 & 2001 ML17313B0441999-07-30030 July 1999 Forwards Comments on Draft NRC Repts Evaluation of AOVs at Us Light-Water Reactors (1999) & Idaho Natl Engineering & Environ Lab Rept (INEEL)EXT-98-00383,Study of AOVs in Npps. ML17313B0431999-07-30030 July 1999 Advises of Listed Senior Mgt Changes That Have Taken Place at Plant ML17313B0151999-07-20020 July 1999 Submits Request to Obtain All Data Previously Sent by PVNGS & Currently in REIRS for OLs NPF-41,NPF-51 & NPF-74.Data Is Requested in Electronic Form (Ascii Format) as It Currently Exists in REIRS Sys ML17313B0091999-07-20020 July 1999 Forwards Requested Calculations Performed to Verify That Increase in Max Radially Averaged Enrichment for Fuel Assemblies from 4.3 Weight Percent to 4.8 Weight Percent Did Not Affect Requirements for TSs 3.7.15,3.7.17 & 4.3.1 ML17313B0171999-07-16016 July 1999 Forwards LER 99-005-00,re Automatic Rt Which Occurred on 990618,following Sensor Failure in Core Protection Calculators.Corrective Actions Described in LER Are Not Necessary to Maintain Compliance with Regulations ML17300B3111999-07-15015 July 1999 Forwards PVNGS Unit 2 ISI Rept for Eighth Refueling Outage. No Commitments Made to NRC by Ltr ML17300B3141999-07-15015 July 1999 Forwards Corrected Electronic Files for Individual Monitoring Repts for 1998.Original Electronic Files Were Found to Have Two Administrative Errors,Which Has Been Corrected.Encl Withheld,Per 10CFR2.790 ML20209G6771999-07-0808 July 1999 Forwards Supplemental Info to Confirm That Decommissioning Funding Plans of Public Service Co of Nm for Interests in PVNGS Have Been Reviewed by Nm Public Regulation Commission. Final Order & Recommended Decisions in Case 2742,also Encl ML17300B2931999-07-0202 July 1999 Submits Withdrawal of Relief 5 for Second ISI Interval for Units 1,2 & 3.Proposed Alternative Is Related to Exam Requirements for Component Supports for Second ISI Interval ML17313A9951999-06-26026 June 1999 Provides Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML17300B2831999-06-26026 June 1999 Requests NRC Approval of Proposed Alternative IAW Provisions of 10CFR50.55a(a)(3)(i) to 10CFR50.55a(g) & Requirements of ASME Boiler & Pressure Vessel Code Section XI for Repairs & Installation.Description of Proposed Alternative,Encl ML17313A9901999-06-15015 June 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. No Commitments Being Made to NRC by Ltr ML17313A9521999-05-24024 May 1999 Notifies NRC That Ja Proctor,License SOP-50314,has Been Permanently Reassigned to Position That Does Not Require License.License Should Be Expired,Per 10CFR55.55 ML17313A9311999-05-13013 May 1999 Notifies NRC That Rev 2 to COLR for Unit 2 Remains Applicable Following Recently Completed Unit 2 Reload ML17313A9481999-05-12012 May 1999 Informs of Change Needed in Order to Update Current Mailing List.Future Mailings for J Horne Should Be Forwarded to Listed Address ML17313A9261999-05-0707 May 1999 Forwards LER 99-004-00,per 10CFR50.73.LER Repts Findings & Corrective Actions Taken as Result of Unit 2 Out of Tolerance Pressurizer Safety Valve (Psv) Condition Which Was Discovered During Outage Testing ML20206H1931999-05-0303 May 1999 Forwards 1998 Annual Rept, for SONGS Units 2 & 3 & PVNGS Units 1,2 & 3.SCEs Form 10K Annual Rept to Securites & Exchange Commission for Fiscal Yr Ending 981231,encl ML17313A9191999-04-30030 April 1999 Forwards Special Rept 2-SR-99-001 Re SG Tube Plugging in PVNGS Unit 2,per TS Reporting Requirement 5.6.8.Complete Results of SG Tube Inservice Insp Will Be Submitted by 000422 ML17313A9181999-04-30030 April 1999 Forwards Electronic File of Individual Monitoring Repts for 1998.Encl Withheld Per 10CFR2.790 ML17313A9091999-04-30030 April 1999 Forwards Proprietary Proposed Test Outlines for Initial License Exams to Be Administered at PVNGS in Aug/Sept 1999. No Commitments Are Contained in Ltr.Proprietary Info Withheld ML17313A9081999-04-23023 April 1999 Documents 990421 Telcon with E Emeigh,Which Requested Extension for Submitting Next Matl Balance Rept for Pvngs,As Required by 10CFR70.53 & 74.13.Required Info Will Be Submitted by 990531 ML17300B3751999-04-23023 April 1999 Forwards LER 99-003-00,reporting Condition Prohibited by TS 3.7.17 Where Spent Fuel Assembly Was Stored in Inappropriate Region in Spent Fuel Pool ML17313B0271999-04-21021 April 1999 Forwards Proprietary Epec Pro Forma Cashflow Statement for 1999.Proprietary Info Withheld,Per 10CFR2.790.Affidavit Encl ML17313A9031999-04-21021 April 1999 Forwards Rev to Relief Request 12 Submitted 990420 to Second 10-yr ISI Interval.Revised Relief Request Discusses in More Detail Actions APS Will Take When There Is Identified Leakage from Bolted Connection ML17313A8971999-04-20020 April 1999 Requests Use of Alternatives to 10CFR50.55a(g) Inservice Insp Requirements.Proposed Alternatives Are Related to Visual Exam of Bolted Connections 05000529/LER-1999-002, Forwards LER 99-002-00 Re Findings & Corrective Actions Taken as Result of Plant Out of Tolerance MSSV Condition Which Was Discovered During pre-outage Testing1999-04-19019 April 1999 Forwards LER 99-002-00 Re Findings & Corrective Actions Taken as Result of Plant Out of Tolerance MSSV Condition Which Was Discovered During pre-outage Testing ML17313A8931999-04-14014 April 1999 Forwards LER 99-003,reporting Condition Prohibited by TSs That Existed When Surveillance Requirement to Verify Essential Chilled Water Sys Valve Positions Was Not Met ML20205Q0821999-04-13013 April 1999 Forwards Second ISI Interval Relief Request 10 from ASME Section XI & Applicable Addenda Re Visual Exams Performed Subsequent to Repair or Replacement of Component or Alteration of Item ML17313A8901999-04-13013 April 1999 Forwards LER 98-003-01 Re MSSV as-found Lift Pressures out- Side of TS Limits.Ler Suppl Provides Evaluation Findings from Unit 3 out-of-tolerance MSSVs Conditions Which Were Discovered During pre-outage Testing ML17313A8831999-04-0808 April 1999 Forwards 1998 Annual Radioactive Effluent Release Rept for Pvngs,Units 1,2 & 3 & Rev 13 to ODCM, for Pvngs,Units 1,2 & 3 IAW TS 5.6.3 ML20205F3491999-03-30030 March 1999 Forwards Proprietary & non-proprietary Info Re Status of Decommissioning Funding for Pvngs,Units 1,2 & 3,per 10CFR50.75(f)(1).Proprietary Info Withheld,Per Requirements of 10CFR2.790(b)(1) ML17313A8671999-03-24024 March 1999 Submits Info Re Present Levels & Sources of Property Insurance Maintained for Pvngs,Per 10CFR50.54(w)(3) ML17313A8601999-03-16016 March 1999 Forwards Revised Relief Requests PRR-05,PRR-06 & PRR-11 to Clarify That Proposed Design Flow Testing for Lpsi,Hpsi & Containment Spray Pumps Will Be Performed Using Instruments That Comply with Code Requirements,Per 990226 Telcon ML17313A8551999-03-0505 March 1999 Requests Proposed Code Alternative IAW 10CFR50.55a(e)(3),as Acceptable Alternative to Requirements of 10CFR50.55a(e)(1), for Installation of in-line safety-related Flow Measurement Instrument in ASME Class 3 Pipe ML17313A8241999-02-23023 February 1999 Advises That Kp Jarvis,License OP-50287-1,no Longer Needs to Maintain License as Permanently Assigned to Position Requiring No License ML17313A8111999-02-18018 February 1999 Forwards PVNGS Unit 3 7th Refueling Outage, Which Provides Complete Results of SG Tube Inservice Insp Performed,Per TS 5.6.8 ML17313A8721999-02-16016 February 1999 Discusses Resolution of Generic Safety Issue 171, ESF Failures from Loss-of-Offsite Power Subsequent to Loca. Util Has Low Vulnerability to Loca/Grid Collapse/Loop Scenario ML17313A7611999-01-22022 January 1999 Forwards PVNGS Unit 3 Inservice Insp Rept Seventh Refueling Outage, Per 10CFR50.55a.Ltr Contains No New Commitments 1999-09-08
[Table view] Category:UTILITY TO NRC
MONTHYEARML17305B0681990-09-17017 September 1990 Forwards Response to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Exam Dates,Anticipated Number of Candidates & Requalification Exam Schedules for FY91-FY94 Also Encl ML17305B0491990-09-12012 September 1990 Forwards Palo Verde Nuclear Generating Station Unit 2 Steam Generator Eddy Current Exam,Second Refueling Outage Apr 1990. ML17305B0281990-08-27027 August 1990 Forwards fitness-for-duty Semiannual Performance Rept for Period of Jan-June 1990,per 10CFR26.71(d) ML17305B0111990-08-15015 August 1990 Responds to Request for Addl Info Re Emergency Lighting,Per Insp Repts 50-528/90-25,50-529/90-25 & 50-530/90-25. Availability Info Provided in Ref 2,most Appropriate Analysis of Lighting Sys Availability ML17305B0021990-08-0909 August 1990 Provides Update on Status of Record 546 post-restart Item, Per 900412 Ltr.Record Will Revise Procedures for Analyzing & Disseminating Incident Investigation,Operations & Maint Experience to Appropriate Dept ML17305A9871990-08-0303 August 1990 Forwards Rev 1 to Abb Impell Rept 01-1658-1815, Emergency Lighting Independent Review, Per Insp Repts 50-528/90-25, 50-529/90-25 & 50-530/90-25 ML17305A9791990-07-31031 July 1990 Forwards, Conceptual Design for Palo Verde Nuclear Generating Station for Diverse Auxiliary Feedwater Actuation Sys (Dafas) for Review.Schedule of Implementation as Indicated ML20056A4161990-07-31031 July 1990 Forwards Revised Security Plan Implementing Procedures.Encl Withheld (Ref 10CFR2.790) ML17305A9831990-07-27027 July 1990 Requests Temporary Waiver of Compliance from Limiting Condition for Operation 3.6.3 to Allow Corrective Maint to Be Performed on Main Feedwater Isolation Valves by Extending Allowed Outage Time to 12 H Instead of 4 H ML20055J2671990-07-25025 July 1990 Forwards Info Constituting Decommissioning Financial Assurance Certification Rept,Per 10CFR50.33(k)(2) & 50.75(b) ML17305A9771990-07-25025 July 1990 Forwards Status of Corrective Actions to Min Multiple Control Element Assembly Drop Events at Plant.Insp of Insulation Coils & Replacement of Defective Coils for Units 1 & 2 Completed ML20055J1711990-07-25025 July 1990 Forwards Certification of Decommissioning Financial Assurances for Plant,Per 10CFR50.75(b) & 50.33(k)(2) ML20055J1031990-07-25025 July 1990 Forwards Certification of Decommissioning Financial Assurances ML17305A9411990-07-20020 July 1990 Forwards Response to NRC Bulletin 90-001, Loss of Fill Oil in Transmitters Mfg by Rosemount. ML17305A9431990-07-17017 July 1990 Forwards Rev 1 to Palo Verde Nuclear Generating Station Annual Radiological Environ Operating Rept for 1987. Rev Results from Internal Review Bu Nuclear Safety Group & Audit Performed by Radiation Protection Stds ML17305A9601990-07-13013 July 1990 Forwards Preliminary Response Re Justification for Continued Operation of Fire Protection Sys Equipment,Per Insp Repts 50-528/90-25,50-529/90-25 & 50-530/90-25 ML17305A9331990-07-12012 July 1990 Discusses Util Compliance w/fitness-for-duty Program Implementation.Lab Specialists,Inc Audited & Monitored W/ Satisfactory Results.Ltr of Agreement Has Been in Place Since 900202 ML17305A9391990-07-0909 July 1990 Forwards Endorsement 44 to Maelu Policy MF-116 & Endorsement 62 to Nelia Policy NF-266 ML17305A9341990-07-0909 July 1990 Submits Results of 900514-18 NUREG-1220 Audit,Per NRC 900608 Request,Per Insp of Plant.Remaining Licensed Operators Found to Be in Conformance W/Medical Exam Requirements of 10CFR50.55 ML17305A9151990-06-29029 June 1990 Forwards Emergency Lighting Failure Data Update,Per 900621 Request ML17305A9061990-06-26026 June 1990 Suppls 891114 Response to Violations Noted in Insp Rept 50-528/89-16.Application for Amend to License NPF-41 Will Be Submitted in Oct 1990 to Permit Lower Flow Rate for RCS & Shutdown Cooling Sys ML17305A9111990-06-25025 June 1990 Responds to Generic Ltr 90-04, Status of Implementation of Generic Safety Issues. ML17305A9081990-06-25025 June 1990 Forwards Schedule Reiterating Util Plans for Implementation of USIs A-9 & A-44 & Provides Current Forecast Refuel Dates ML17305A9051990-06-25025 June 1990 Forwards Endorsement 45 to Maelu Policy MF-116 & Endorsement 63 to Nelia Policy NF-266 ML17305A9121990-06-24024 June 1990 Forwards Discharge Test Voltage Curve,Per 900623 Request for Completion of Emergency Lighting Exide Power Supply Prior to Entry Into Mode 2 ML17305A9171990-06-24024 June 1990 Confirms Compliance W/Agreed Upon Course of Action for Restart of Facility as Outlined in 891224 Ltr & Completion of Items Contained in Restart List Provided as Attachment to 900111 Ltr ML17305A8961990-06-20020 June 1990 Responds to NRC 900521 Ltr Re Violations Noted in Insp Repts 50-528/90-12,50-529/90-12 & 50-530/90-12.Corrective Action: Wiring in PPS Cabinets & Cabinet Drawers Reworked in Accordance W/Approved Work Authorization Documents IR 05000528/19900021990-06-19019 June 1990 Describes Current Status & Provides Description of Actions Taken to Ensure Continued High Reliability of Emergency Lighting Sys,Per Insp Repts 50-528/90-02,50-529/90-02 & 50-530/90-02.Emergency Lights Mfg by Emergi-Lite ML17305A9041990-06-19019 June 1990 Describes Current Status & Provides Description of Actions Taken to Ensure Continued High Reliability of Emergency Lighting Sys,Per Insp Repts 50-528/90-02,50-529/90-02 & 50-530/90-02.Emergency Lights Mfg by Emergi-Lite ML17305A8891990-06-15015 June 1990 Informs NRC That post-restart Items Due Prior to Scheduled Restart Have Been Completed on Schedule W/Listed Exceptions ML17305A8871990-06-14014 June 1990 Advises That Fuel Pool Cooling & Cleanup Procedures Being Restructured,Per Response to Violations in Insp Repts 50-528/89-36 & 50-530/89-36 ML17305A8731990-06-0808 June 1990 Responds to Bulletin 88-005 Re Product Forms Other than Fittings & Flanges for Plant.Significant Number of Lugs Delivered to Plant.Util Should Be Notified,If NRC Previous Review of Records Has Identified Other Product Forms ML17305A9421990-06-0101 June 1990 Forwards Pinnacle West Response to State of Az Corp Commission Complaint Filed W/Us Securities & Exchange Commission on 900521,to Revoke Exemption from Public Utils Holding Co Act ML17305A8661990-05-31031 May 1990 Forwards Projected 1990 Cash Flow Statements ML17305A8391990-05-31031 May 1990 Forwards 1990 Reactor Containment Bldg Integrated Leak Rate Test,Final Rept. ML17305A8571990-05-31031 May 1990 Forwards Amended Pages of Feb,Mar & Apr 1990 Monthly Operating Repts for Palo Verde Nuclear Generating Station Unit 2 ML17305A8201990-05-23023 May 1990 Provides Status of Improvements to Eliminate Possibility of Multiple Control Element Assembly Drop Events.Licensee Developed Mod to Ground Fault Detection Sys to Assure Continuous Monitoring & Annunciation of Any Future Faults ML20043B6421990-05-19019 May 1990 Forwards Amend 26 to Security Plan.Amend Withheld (Ref 10CFR2.790(d) & 10CFR73.21) ML17305A7841990-05-15015 May 1990 Forwards Special Rept 2-SR-90-002 Re Steam Generator Tube Plugging Due to Inservice Insp Activities.Twenty Tubes Plugged in Steam Generator 1 & ninety-one Tubes Plugged in Steam Generator 2 ML17305A8721990-05-14014 May 1990 Forwards Arizona Corp Commission Complaint Filed W/Us Securities & Exchange Commission Seeking Revocation or Mod of Exemption of Pinnacle West Capital Corp.Complaint Wholly W/O Merit ML17305A7621990-05-11011 May 1990 Responds to NRC 900413 Ltr Re Violations Noted in Insp Repts 50-528/90-03,50-529/90-03 & 50-530/90-03.Corrective Actions: Night Order Written for Guidance on Use of Instrumentation W/Maint Tag Present ML17305A7921990-05-0808 May 1990 Forwards Public Version of Rev 2 to EPIP-14, Dose Assessment. W/900523 Release Memo ML20043A0511990-05-0303 May 1990 Forwards Public Version of Revised Epips,Including Procedure Change Notice 11 to Rev 12 to EPIP-04 & Procedure Change Notice 1 to Rev 6 to EPIP-15 ML17305A7421990-05-0303 May 1990 Responds to 900330 Enforcement Conference Re Violations Noted in Insp Repts 50-528/90-04,50-529/90-13 & 50-530/90-13.Corrective Action:Special Locking Mechanisms Installed on Currently Posted Radiation Area Doors & Gates ML17305A8861990-04-30030 April 1990 Forwards EPIP Update,Including Rev 7 to EPIP 02,Rev 12 to EPIP 03 & Rev 9 to EPIP 20.W/o Encl ML17305A7381990-04-30030 April 1990 Forwards Annual Environ Operating Rept for 1989 & Annual Rept for Salt Deposition Monitoring Program 1989. ML17305A7131990-04-20020 April 1990 Responds to NRC 900321 Ltr Re Violations Noted in Insp Rept 50-530/90-08.Corrective Action:Plant Guideline Providing Addl Guidance Re Prioritization of Work Promulgated ML17305A6891990-04-16016 April 1990 Forwards Rev to Cycle 3 Reload Analysis Rept,Submitted 891024.Rev Reflects Early end-of-cycle Unit Shutdown & Replacement of Eight New Fuel Assemblies ML17305A7011990-04-12012 April 1990 Forwards Rev 3 to Palo Verde Nuclear Generating Station Post-Restart Actions, Per JB Martin 891224 Ltr ML17305A7081990-04-0909 April 1990 Forwards post-exam Security Agreements for Dk Hendrick, D Ensign,M Alavi & Author.Agreement Certifies That Signatories Will Not Divulge Info Re 900320 Exams 1990-09-17
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f Arizona Nuclear Power Project ,
I P o Box 52034
- PHOENIX, ARIZONA 8507M034 HMk -$ j#7 ?wg lr AEGiG;; y; 3 March 3, 1986 ANPP 35365-EEVB/JYM/98.05 Mr. John B. Martin, Regional Administrator Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5638
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 (License No. NPF-41)
Notice of Violation, 50-528/85-43-01, 50-528/85-43-03 File: 86-019-026; D.4.33.2; 86-056-026
Reference:
NRC Inspection Report Nos. 50-528/85-43, 50-529/85-44, Letter from J.B. Martin to E. E. Van Brunt, Jr. , dated January 30, 1986.
Dear Mr. Martin:
This letter is provided in response to the inspection conducted by Messrs. R. Zimmerman, C. Bosted and G. Fiore111 of the NRC staff on November 13 through December 27, 1985, of activities licensed by License Nos. NPF-41 and NPF-46.
Based on the results of the inspection, two violations of NRC requirements (failure of closing the 8-inch containment purge supply and exhaust isolation valves and submittal of late Licensee Event Reports (LERs)) were identified.
The violations are discussed in items a. and b. in Appendix A of the referenced letter, which is provided in Attachment 1. Responses to these items are submitted herewith in Attachment 2 to this letter.
Also included in Attachment 3 are responses to other concerns mentioned in the referenced letter. These concerns include the: 1) Poet Trip Review process;
- 2) mispositioned diesel generator jacket water makeup valve; and 3) procedural adherence.
B60331023e 860 528 PDR ADOCK O PDR G -
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Mr. Martin Notice of Violation, 50-528/85-43-01, 50-528/85-43-03 ANPP-
- Page 2 4
The response to the concern regarding errors made by the I&C Technicians will be included in the response to the Notice of Violation dated February 21, 1986, concerning the failure to bypass a radiation unit being tested. The response to this violation is scheduled to be submitted by March 24, 1986.
4 Very truly yours, b' L1 LLW v'd E. E. Van Brunt, Jr.
Executive Vice President Project Director EEVB/JYM/dk Attachments cc: A. C. Gehr (all w/a) 1 R. P. Zimmerman
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ATTACHMENT 1 APPENDIX A NOTICE OF VIOLATION --
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Arizona Nuclear Power Project Docket No. 50-528 Post Office Box 21666 -
License No. NPF-41
. Phoeni::, Arizona 85036 -
AL a result of the inspection conducted on November 13 - December 26, 1985, and in accordance with NRC Enforcement Policy, 10 CFR Part 2, Appendix C, the following violations were identified:
- a. Technical Specification 3'.6.1.7.b requires, in part, that the 8-inch containment purge supply and exhaust' isolation valves be sealed closed to the maximum extent practicable, but may be opened for purge system operation for ALARA and respirable air quality considerations for personnel entry.
Contrary to the above, the 8-inch containment purge supply and exhaust isolation valves were not sealed closed to the maximum extent practicable during the period 10:00 PM on December 2, through 12:06 PM on December 3, 1985, in that, the valves remained open without justification following the completion of a contaicment personnel entry. -
This is a Severity Level IV Violation (Supplement I)
- b. Technical Specification 6.6.1.a requires that the Commission be notified of Reportable Events, and a report be submitted pur-suant to the requirements of 10 CFR Part 50.73.q 10 CFR Part 50.73 requires, in part, that a Licensee Event Report be submitted within 30 days after discovery of any operation or condition prohibited by the plant's Technical Specifications.
Contrary to the above, the following instances of submittal of late Licensee Event Reports (LERs) were identified:
o LER 85-70, documenting a condition prohibited by Technical Specification 3.2.3.b.3, was submitted to the Commission on October 25, 1985, 31 days after discovery, rather than 30.
o LER 85-72, documenting a condition prohibited by Technical Specification 3.3.3.9, was submitted to the Commission on October 16, 1985, 31 days after discovery, rather than 30.
This is a repeat Severity Level V Violation (Supplement I) .
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. ATTACHMENT 2 RESPONSE TO NOTICE OF VIOLATION 50-528/85-43-03 (ITEM a)
I. THE CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED The immediate corrective action taken, when this problem was identified, was to secure power access purge operation and terminate the approved purge permit. During the entire period of purge operations, automatic isolation capabilities were operable so safety to the public was not compromised.
4 The root cause for this violation was a misinterpretation of administrative procedure 75AC-9ZZ02 which limited the duration of any power access purge to seven days in order to assure that the conditionally required weekly fune.tional test would not be overlooked.
- If a purge operation required more than seven days, a new release permit would be created which would document a new functional test. In some cases, the administrative guidance was misinterpreted to mean that power access purge permits should be created for seven day periods.
II. THE CORRECTIVE STEPS WHICH WILL BE TAT.EN TO AVOID FURTHER ITEMS OF NONCOMPLIANCE Corrective actions taken to prevent recurrence have been primarily addressed in our release permit procedure in the form of a caution statement that identifies specifically when power access purge operations are permitted. The technicians responsible for the implementation of the procedure are aware of the contents of the procedure revision. Additionally, the continuing need for an in progress power access purge will be addressed each day based on an evaluation performed by radiation protection and shift supervision.
III. THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED i
l Technical Specification compliance was achieved upon valve closure on December 3, 1985.
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ATTACHMENT 2 (continued)
RESPONSE TO NOTICE OF VIOLATION 50-528/85-43-01 (ITEM b)
I. THE CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND RESULTS ACHIEVED An investigation of the two late submittals of - LER's revealed that the root cause was an overly cumbersome review and approval process for LER's, with multiple organizations sharing responsibility for both timeliness and adequacy. This investigation has been under constant scrutiny from the management of ANPP since the initial Notice of Violation which was issued in August of 1985 as a result of the late submittal of LER No. 85-32. At that time, the process used to identify, prepare, review, approve and submit reports was examined, and the conditions which led to the initial violation were corrected. In the case of LER 85-32, a non-conservative assumption related to reportability was made early in the identification and review process, which was not corrected soon enough to allow research and preparation of a timely report. To rectify the circumstances which led to that violation, extremely conservative criteria were imposed for the initial screening of events for reportability, and no similarly caused delays have been experienced to date.
As stated above, the management of ANPP recognized at that time that a comprehensive review and corrective measures may have been needed to fully address the overall reporting process. Detailed evaluation of this area by corporate QA/QC resulted in its issuance of a Management Corrective Action Report on August 13, 1985. Review of the MCAR, and internal discussions at the project management levels, resulted in the assignment of the Assistant Vice President, Nuclear Production, with the primary charter for developing an overall action plan and procedures to address its identified concerns. '
During the period of October 1985 through January 1986, the interfaces, responsibilities and procedures used for the reporting of events, interface with regulatory agencies, and associated actions, were studied and an overall project reorganization was proposed and initiated. On
. February 7, 1986, the first of these changes was implemented with the i naming of a Compliance Manager with overall responsibility and control in these areas. This position is being elevated to report to the Plant Manager. The Compliance Manager is in the process of implementing the required corporate restructuring, staffing evaluation, and procedure preparation to implement the plan developed. Two additional Compliance Supervisors are being selected and will join the organization in March and April. Each of these individiuals will be experienced in the Project's controls and Lprocedures, and will nave previously worked in the reportability area. The balance of the staffing needs for the organization is under final review, and will be commensurate with the final scope of responsibilities assigned. )
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ATTACHMENT 2 (continued) i At no time have the few late LER's been late because they were not tracked properly.
1 To address the specific issue of late LER's, .the proposed draft
- procedures for the new organization streamline that review and approval process, while placing additional emphasis on prompt attention to i immediate corrective actions, resoltuion of technical issues and comprehensive actions to prevent recurrence.
II. THE CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER ITEMS OF NONCOMPLIANCE The additional steps which will be taken to prevent further items of
! noncompliance are detailed above, and include completion of the
- reorganization, completion of the staffing evaluation, and implementation of the procedures to implement the overall program.
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, III. THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Since the occurrence of the circumstances described in the Notice of Violation, no further LER's have been submitted late. The required modifications to the project organization, staffing evaluation, and procedures are forecast for completion by April of 1986. These actions should prevent further occurrences of late LER's.
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ATTACHMENT 3 POST TRIP REVIEW ADEQUACY NRC Concern The inspector examined the adequacy of the licensee's evaluation process for the reactor trip which occurred on December 16 and was documented in the Post Trip Review Report (PTRR) which received management approval prior to plant restart on December 18. Background information associated with the reactor trip is documented in paragraph 3.a. The implementing procedure, 79AC-92208, Post Trip Review Reporting, which specified the instruction for completing the PTRR was considered adequate; however, the evaluation of the December 16 trip was considered to lack thoroughness with regard to identifying and documenting plant anomalies and problem areas, including the implementation of appropriate corrective actions. The following examples were discussed in detail with plant management.
- a. The PTRR did not address the fact that the securing of the running main feedwater pump prior to the start of an auxiliary feedwater pump was a significant contributor to the reactor trip on low s team generator level. Further, although identified as not having been performed in the desired order by the licensee, specific operetor shif t briefings / training were not performed prior to restart to minimize similar future trips.
- b. The licensee's evaluation of the sequencer malfunction and corrective actions initiated prior to restart were considered adequate; however, plant management did not include the sequencer problem or actions taken to prevent recurrence in the PTRR. Rather, a reference to an addendum report to be issued by December 31, 1985, describing the sequencer problem was included in the PTRR. This report would also address longer term corrective action, if necessary. The inspector stated that although the. sequencer problem was not directly tied . to the reactor trip, it raised the most significant safety questions which needed to be resolved prior to restart. Thus, inclusion of more details on this issue in the PTRR report would seem to be appropriate,
- c. Similar to the item above, the "B" Chiller was repaired and root cause analysis initiated; however, no reference to the cause of the chiller l trip or its effect on overall reliability was included in the PTRR.
- d. The PTRR did address the fact that the "N" Auxiliary Feedwater Pump discharge pressure gauge was valved out in preparation for performance f a surveillance test; however, it did not address the apparent lack familiarity of Control Room personnel with the status of plant equipmea6 and instrumentation.
- e. The PTRR did not address whether Technical Specification compliance was maintained during the initial transient and subsequent reactor trip.
i ATTACHMENT 3 (Continued) j .
ANPP Resolution
- a. The PTRR did not address securing the running Main Feedwater Pump prior to starting the Non-Essential Auxiliary Feedwater Pump because while these actions were not taken in the preferred order, the order in which j they were performed was not a significant issue for the following reasons
s j 1) According to available indication, flow was not being supplied to
. the Steam Generator by the running Main Feedwater Pump due to low i
feedwater regulating valve differential pressure. It made no difference that the running Main Feedwater Pump was secured prior to starting the Non-Essential Auxiliary Feedwater Pump.
- 2) Operational order of starting the Non-Essential Auxil.iary Feedwater Pump prior to securing the running Main Feedwater Pump is highly stressed during operator training in the Simulator. In this j isolated case, the Shift Supervisor and Reactor Operator did not properly communicate to assure the intentions of the Shift Supervisor were carried out. This was corrected the following day ,
when, at the direction of the Shift Supervisor, this crew discussed their communications during the event in an effort to enhance
! them. This was not considered to be a significant issue since, as
! stated in 1) above, the order of performance of operations did not have a significant effect on the transient and because this issue was addressed and resolved by the operating crew the following shift.
I Although no forma!. briefings / training were held with each crew, each i operating crew reviewed this event. Additionally post trip reviews are.
formally reviewed under the Operating Department Experience Report Program. Also, a letter was issued by the Unit 1 Superintendent addressing proper operational order when transferring from the Main Feedwater Pump to the Non-Essential Auxiliary Feedwater Pump. The Post Trip Review Reporting Procedure is being revised to include a section on r PTRR Shif t Briefing in which the Operations Manager or designee will I
determine whether it is necessary for the oncoming control room crew to i participate in a briefing session to assure that event circumstances and l plant response are understood. The revised PTRR Procedure will be i
effective by March 15, 1986.
- b. It is the intent of PVNGS management to comple:ely review and document corrective action for significant operational events such as the failure-
., of the sequencer. The purpose of a Post Trip Review Report is to assure
- that all Reactor Protection and other safety related eiystems function as
! required prior to and following a trip. As such, the PTPR is used as a i tool by plant management. Since the Sequencer failure was unrelated to the cause of the Reactor trip and did not create complications to mitigating the consequences of the trip, the failure of the Sequencer was not included in the PTRR. An addendum was added to.the PTRR to address the Sequencer failure as a means to assure proper review of the Sequencer
- failure and to document and track corrective actions for that failure.
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ATTACHMENT 3 (Continued)
The Sequencer failure and repairs were tracked and documented with the existing methods contained in the work control program. The operational status of the technical specification related equipment was monitored using the Technical Specification Component Condition Records (TSCCR).
Following identification that high temperature was a significant contributor to the Sequencer failure, cabinet temperature was monitored and documented hourly with a specific action plan identified and documented for Operations to implement if temperature reached a predetermined level. The identified condition was evaluated and corrective action identified and completed prior to restart. Also, a DCP upgraded the cabinet fans. This was accomplished independent of the PTRR.
A procedure, separate from the PTRR procedure, is being drafted which will analyze, and specify corrective actions for significant events whi-h are unrelated to Reactor trips. Following its implementation, events such as the Sequencer failure will be handled using the new procedure.
The procedure is forecasted to be implemented by June 30, 1986.
- c. Our response to the item regarding the trip of the "B" Chiller is similar to that above for the Sequencer. The failure of the "B" Chiller was not a contributing cause to the Reactor trip.
- d. We do not attribute "... apparent lack of familiarity...with the status of plant equipment and instrumentation" to the Control Room staff.
Isolation of the gauge in question was masked due to control of this activity being in a procedure and therefore not requiring a Control Board discrepancy tag. This problem was quickly recognized and corrected by deleting the requirement for isolation of this gauge from the surveillance test.
! While it is true that the crew failed to recognize and remember that the
- Non-Essential Auxiliary Feedwater Discharge Pressure Gauge had been isolated for performance of a surveillance test, it is an overstatement to characterize them as having a general lack of familiarity with the status of plant equipment and instrumentation.
- e. Compliance with the Technical Specifications was verified in the PTRR in
. parts 111B, 111C, 111D, 111E and 111F. In addition, part IVC verified I that no Technical Specification action statements were in effect which would prevent the Unit from returning to power. The STA verified compliance with Technical Specifications during and following the transient as part of his routine duties in such a situation. These routine actions are not noted in the PTRR.
The PTRR procedure will be upgraded to provide clarification of the process.
Items addressed are listed below:
! 1) The requirement for a more detailed sequence of events was formalized.
ATTACHSDrr 3 (Continued)
- 2) The review process (flow) was clarified. The Unit Superintendent was included in the review process and the requirement for the Shift Supervisor to review the PTRR was clarified. In addition, the method for controlling addenda to the PTRR was included.
- 3) Plant status data sheets were revised to provide additional information.
- 4) The Post Trip Review Committee function was clarified.
- 5) A requirement was added to specify dates or conditions by which corrective actions must be implemented.
i ATTACHMENT 3 (Continued) a MISPOSITIONED DIESEL GENERATOR JACKET WATER MAKEUP VALVE ,,
a NRC Concern On November 29, 1985, the inspector observed that the "A" Diesel Generator jacket water makeup valve (DGA-V004) was in the closed, rather than the normally open position. The makeup valve is a small, manual valve with a non-cri ti cal function. The Control Poom alignment sheets and status print incorrectly indicated the valve was open. Upon informing operating shift personnel of the mispositioned valve, it was promptly returned to the proper, open position. The licensee's investigation was unable to conclusively determine how the valve became closed. On December 2, 1985, the inspector l observed that the above valve was in the proper open position; however, the 4 alignment sheets and status print now showed the valve as closed. The 1
licensee determined that the valve was closed during a jacket water heater i
replacement performed on November 30 and December 1, and the Control Room status systems were not updated following reopening of the valve. The
! inspector discussed the mispositioned valve and the two instances of I maintaining inaccurate valve status in the Control Room with licensee management. The inspector also reviewed a large sample of valve position verifications performed without identification of discrepancies by the [
i licensee's Quality Assurance Department. The adequacy of the licensee's valve !
j position controls will be reviewed as a follow-up item.
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! ANPP Resolution i
In both cases, the operator took prompt action upon realizing that the valve
- position did not correspond to the Control Room alignment sheets and status l prints. This appears to be an isolated occurrence substantiated by the j , extensive monitoring program by Quality Assurance.
The monitoring program ine1udes checking valve status and the corresponding Control Room alignment sheets and status print. The number of deficiencies noted by QA has been small, indicating that the overall program is working. QA monitoring is l
j frequent, sometimes 2 or 3 times a month. Whenever a significant number of l valve manipulations and/or significant maintenance has been done on a system, a complete system realignment is generally performed to minimize any errors that could be due to the valve status file.
Additionally, it should be noted that no locked valve or breaker, required to
- be locked in a specific position, has been . found out of the required position for the mode the plant was in during the extensive er iring by Quality Assurance.
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ATTACHMENT 3 (continued) 1 PROCEDURE ADHERENCE NRC Concern On December 3,1985, at about 8:10 A.M., a leaking main condenser tube plug resulted in a high silica concentration of .37 ppm in the No. 1 Steam Generator. Procedure 74AC-9ZZ04, Systems Chemistry Specifications, step 5.3.4.1, required that with a silica concentration greater than .3 ppm (action level 3) shutdown was required within four hours. Responsible chemistry
- personnel identified that the specified required action level 3 was in error,
! and that in accordance with the PWR Secondary Water Chemistry Guidelines prepared by the Steam Generator Owners Group, the proper action level should be level 1, which required that the concentration be returned to within normal range within one week. The licensee did increase steam generator blowdown and the silica concentration was returned to acceptable levels at about 11:50 A.M., prior to exceeding the four hour action level 3. The inspector noted that a procedure change to 74AC-92Z04, step 5.3.4.1 was not initiated to
- correct the erroneous action level from a level 3 to a level 1 with greater than .3 ppm silica.
Based on discussions with Chemistry and Operations staff, the inspector learned that no plans to commence a plant shutdown were considered due to the knowledge of the procedure error and action to initiate a procedure change to correct the error in "real time" was ' not pursued, apparently due in part to the fact that changes to 74AC-9ZZ04 require a Plant Review Board approval prior to implemantation.
The inspector informed licensee management that the potential deviation from step 5.3.4.1 appeared to indicate a lack of understanding on the part of plant personnel concerning when a proced' ire change is required. '
Corporate, plant and Quality Assurance management stressed to the inspector their policy of commitment to procedure compliance.
The inspector expressed concern that basic procedure adherence must be
, understood and appreciated at all levels of the organization for company
! policy to be effectively carried out. The area of procedure adherence will continue to be evaluated as part of the routine inspection program.
i ANPP Resolution Procedure 74AC-9ZZ04 has been revised to correct the required action level change for silica concentrations greater than .3 ppm. The action level has been changed from level 3 to level 1.
, In addition, provisions have been made in Prceedure 74AC-9ZZ04 to permit the
- Chemical Services Manager or his designee to modify system chemistry specifications (excluding Technical Specificatioc related specifications) by performing and documenting an evaluation of the condition and effect using a j sound technical basis for the change. This will help ensure procedure compliance and still provide flexibility in plant operation. l i
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ATTACHMENT 3 (Continued)
Senior management is committed to full compliance with procedures. This commitment has been stressed at meetings between various levels of management, including meetings between the Vice President, Nuclear Production, and the plant personnel. This commitment will continue to be stressed and individuals.,
will be held accountable for procedure violations.
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