ML20154M619
| ML20154M619 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 09/23/1988 |
| From: | Counsil W TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| Shared Package | |
| ML20154M624 | List: |
| References | |
| NUDOCS 8809290046 | |
| Download: ML20154M619 (2) | |
Text
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'e MFE Log 4 TXX-88699 Fi1e # 10110 i
.r C
909.2 1UELECTRIC September 23, 1988 i
?. NiuSYrien.,
U. S. Nuclear Regulatory Commission r
Attn: DocurJent Control Desk Wr.shington, D.C.
20555 i
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES) i DOCKET NO. 50-445 i
C0ATING REMOVAL FROM STATION SERVICE WATER l
SYSTEM DIPING Gentlemen:
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TV Electric has been involved in a program to address corrosion concerns relating to the Station Service Water System (SSWS) at the Comanche Peak Steam Electric Station (CPSES).
A portion of that program involved removing the internal coating from specific sections of the SSWS piping.
The coating removal activities were discussed in Inspection Reports 50-445/88-34; 50-446/88-30 dated June 17, 1988: 50-445/88-40; 50-446/88-36 dated July 15, 1988: 50-445/88-47 and 50-446/88-42 dated September ?, 1988,
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dnd in d managemenc meeting on September 13, 1988.
In the meeting, TV Electric discussed coating removal activities including various concerns enc ontered, both administrative and technical.
The TV Electric presentation
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was based upon reviews which have been on-going and an engineering report which was under development.
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During the meeting, TV Electric committed to complete and submit this l
engineering report by September 23, 1988.
Subsequent to the meeting, an NRC representative requested a chronology of the events related to the coating t
removal effort.
This chronology has been prepared and incorporated into the i
engineering report.
The engineering report is enclosed with this letter.
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i TXX-88699 September 23, 1988 Page 2 of 2 As a result of this review, TV Electric has identified several actions which are being impicme'ted.
These actions inclu1e corrective actions as well as enhancement
- < assure that concerns are corrected and that similar concerns do not tur.
These actions are described in the enclosed
~ report and actions are scheduled to be comp 1"+ed on cr before December 1, 1988.
J Since TV Electric recognizes that identification of root causes and contributing J
facters can be a subjective process, there are two points that it believes
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should be emphasized.
First, labeling one concern as a root cause and r
others as contributing factors did not lead to the latter receiving any l
less attention.
Such con: erns were carefully evaluated for po*ential generic implications, and corrective and preventive :ctions were developed i
to preclude recurrence.
Secondly, TV Electric scrutinized the corcerns i
that were identified in the entire coating removal project, from the problem characterization phase to the evaluatton of dage to the pipe.
Consequently, l
all concerns have been fully and appropriately addressed.
Very truly yours.
I b?lJ{' '
j W.
Counsil t
MCP/grr i
Enclosure c - Mr. R. D. Martin, Region IV 1
Resident Inspectors, CPSES '3)
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Texas 04partment of L6bor and Standards l
Boiler !ivision f
i E. O. Tlempson State Offict Building I
P. O. Bcx 12157 Capitol Station i
Austin, Texas 78701 Attn: itee Pattt+ws l
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