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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 ML20199B6301997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H5991997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20216H6071997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for Vogtle Electric Generating Plant ML20210K5081997-07-31031 July 1997 Monthly Operating Repts for July 1997 for VEGP ML20140D7301997-05-31031 May 1997 Monthly Operating Repts for May 1997 for Vogtle Electric Generating Plant ML20141D8531997-04-30030 April 1997 Monthly Operating Repts for Apr 1997 for Vogtle Electric Generating Plant Units 1 & 2 ML20137T6191997-03-31031 March 1997 Monthly Operating Repts for Mar 1997 for Vogtle Electric Generating Plant ML20136G3471997-02-28028 February 1997 Monthly Operating Repts for Feb 1997 for Vogtle Electric Generating Plant Units 1 & 2 ML20134H3481997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20133F6551996-12-31031 December 1996 Monthly Operating Repts for Dec 1996 for Vogtle Electric Generating Plant,Unit 1 & 2 ML20132B9671996-11-30030 November 1996 Monthly Operating Repts for Nov 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20134K7361996-10-31031 October 1996 Monthly Operating Repts for Oct 1996 for Vogtle Electric Generating Plant,Units 1 & 2 ML20128N1541996-09-30030 September 1996 Monthly Operating Repts for Sept 1996 for Vogtle Electric Generating Plant,Units 1 & 2 ML20117N1731996-08-31031 August 1996 Monthly Operating Repts for Aug 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20116J3461996-07-31031 July 1996 Monthly Operating Repts for Jul 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20115E9821996-06-30030 June 1996 Monthly Operating Repts for June 1996 for Vogtle Electric Generating Plant ML20112H6411996-05-31031 May 1996 Monthly Operating Repts for May 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20111B2461996-04-30030 April 1996 Monthly Operating Repts for Apr 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20101R0251996-03-31031 March 1996 Monthly Operating Repts for Mar 1996 for Vogtle Electric Generating Plant ML20100R2701996-02-29029 February 1996 Monthly Operating Repts for Feb 1995 for Vogtle Electric Generating Plant ML20100F2071996-01-31031 January 1996 Monthly Operating Repts for Jan 1996 for Vogtle Electric Generating Plant Units 1 & 2 ML20096C3051995-12-31031 December 1995 Monthly Operating Repts for Dec 1995 for Vogtle Electric Generating Plant,Units 1 & 2 ML20095E0201995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for Vogtle Electric Generating Plant ML20094J0741995-10-31031 October 1995 Monthly Operating Repts for Oct 1995 for Vogtle Electric Generating Plant Units 1 & 2 ML20093F5031995-09-30030 September 1995 Monthly Operating Repts for Sept 1995 for Vogtle Electric Generating Plant 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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GEORGIA POWER
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' Georgia Power b ENCLOSURE-TABLE OF CONTENTS PLANT V0GTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68 HONTHLY OPERATING REPORT Aori l . 1988 NARRATIVE REPORT Page E-1 OPERATING DATA REPORT Page E-2 !
AVERAGE DAILY POWER LEVEL Page E-3 !
UNIT SHUTDOHNS AND POWER REDUCTIONS Page E-4
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.s NARRATIVE REPORT DOCKET NO. 50-424 UNIT 1 DATE: MAY 3,1988 COMPLETED BY: S.C. DILWORTH TELEPHONE: (404) 724-8114 x3070 APRIL 1 00:00 UNIT OPERATING AT 100% POWER WITH NO OPERATING PROBLEMS.
APRIL 7 08:46 REACTOR TRIP DUE TO TURBINE TRIP, TURBINE TRIP ON HIGH STATOR COOLING TEMPERATURE.
APRIL 8 01:25 MANUALLY TRIPPED MAIN TURBINE AND OPENED REACTOR TRIP BREAKERS.
PLANT STILL IN MODE 3 FROM PREVIOUS TRIP.
APRIL B 23: 40 UNIT 1 ENTERED MODE 2.
APRIL 9 00:17 UNIT 1 REACTOR IS CRITICAL.
APRIL 9 03:17 UNIT 1 ENTERED MODE 1.
APRIL 9 11:03 UNIT 1 TIED TO GRID.
APRIL 10 15:52 UNIT 1 OPERATING AT 100% POWER WITH NO OPERATINS PROBLEMS.
APRIL 20 10:00 NI-41 INOPERABLE. REDUCED POWER TO 98%.
APRIL 20 13:05 INCREASING POWER TO 100%.
APRIL 20 15:00 OPERATING AT 100% POWER WITH NO OPERATING PROBLEMS.
APRIL 24 09:22 MANUAL REACTOR TRIP DUE TO STEAM GENERATOR 84 LEVEL AT 42%. LOOP 4 MAIN FEEDWATER ISOLAT!ON VALVE NOT RESPONDING TO OPEN SIGNAL.
APRIL 27 11:45 UNIT 1 ENTERED MODE 2.
APRIL 27 12:15 UNIT 1 REACTOR IS CRITICAL.
APRIL 27 21:09 UNIT 1 ENTERED MODE 1.
APRIL 29 03:37 UNIT 1 T!ED TO GRID.
APRIL 29 04:00 UNIT 1 OPERATING AT 100% POWER WITH NO OPERATING PROBLEMS.
APRIL 30 24: 00 UNIT 1 OPERATING AT 100% POWER WITH NO OPERATING PROBLEMS.
SUMMARY
REPORT UNIT 1 THE FOLLOWING ITEMS WERE MODIFIED AND OR REPA! RED DURING THE OUTAGES. ALL WERE CRITICAL PATH ITEMS AND ARE LISTED IN THE ORDER THEY OCCURREC.
- 1. THE ONLY CRITICAL PATH ITEM FOR THE OUTAGE ON APRIL 7 WAS REPLACEMENT OF THE UNDERSIZED LINKAGE SHAFT WITH THE CORRECT S!!E SHAFT ON VALVE ITCV-6000
- 2. THE CRITICAL PATH ITEMS FOR THE OUTAGE ON APRIL 24 INCLUDED REPLACEMENT OF FOUR RELAYS, TWO ABASTAT T!MERS AND TWO AIR SOLEN 0!DS. ON APRIL 26, TRANSFORMER NB-10 WAS SHORTED OUT AND WAS REPLACED WITH TRANSFORMER ANB06, WHICH BECAME THE CRITICAL PATH ITEM.
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OPERATINS DATA REPORT DOCKET NO. 50-424 DATE: MAY 3,1988 COMPLETED BY S.C. DILWORTH TELEPHONE: (404) 724-8114 x3870 OPERATING STATUS
- 1. UNIT NAME: A. W. V06TLE UNIT 1
- 2. REPORT PERIOD: APR 98
- 3. LICENSED THERMAL POWER (MWt): 3411
- 4. NAMEPLATE RATING (6ROSS MWe): 1157
- 5. DESIGN ELECTRICAL RATINS (NET MWe): 1101
- 6. MAXIMUM DEPENDABLE CAPACITY (6ROSS MWe): 1133
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MWe): 1079
- 8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THROUGH 7) $1NCE LAST REPORT, SIVE REASONS:
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe): NO RESTR!CTIONS
- 10. REASONS FOR RESTRICTION, IF ANY: N/A THIS MONTH YR. TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD: 719 2903 8040
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL: 604.6 2224.9 6277.8
- 13. REACTOR RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
- 14. HOURS GENERATOR ON-LINE: 578.5 2150,6 6079.2
- 15. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
- 16. GROSS THERMAL ENERGY GENERATED (MWH): 1907244 7116240 19777287.8
- 17. GROSS ELEC. ENERGY GENERATED (MWH): 635710 2371050 6555030
- 18. NET ELEC. ENERGY GENERATED (MWH): 598280 2224740 6146260
- 19. REACTOR SERV!CE FACTOR 84.1% 76.6% 78.1%
- 20. REACTOR AVAILIBILITY FACTOR 84.1% 76.6% 78.1%
- 21. UNIT SERV!CE FACTOR: 80.5% 74.4% 75.6%
- 22. UNIT AVAILABILITY FACTOR: 80.5% 74.4% 75.6%
- 23. UNIT CAPACITY FACTOR (USING MDC NET): 77.1% 71.0% 70.8%
- 24. UNIT CAPACITY FACTOR (USINS DER NET): 75.6% 69.6% 69.4%
- 25. UNIT FORCED OUTAGE RATE: 19.5% 24.4% 21.3%
- 26. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE. AND DUPATION OF EACH) REFUELING OUTAGE SEPTEMBER 18, 1988 50 DAYS.
- 27. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: N/A
- 28. UNITS IN TEST STATUS ( PRIOR TO COMMERCIAL OPERATION): N/A E-2
. c.
ed UNIT 1 AVERAGE DAILY DOCKET NO. 50-424 POWER LEVEL DATE: MAY 3.1988 COMPLETED SY S. C. DILWORTH TELEPHONE: (404) 724-8114 x3870 DAY- Net MW 1 ......... 1087 2 ......... 1045 3 ......... 1083 4 ......... 1083 5 ......... 1091 6 ......... 1092 7 ......... 374 0 ......... 0 9 ......... 187 10 ......... 963 11 ......... 1088 12 ......... 1090 13 ......... 1089 14 ......... 1090 15 ......... 1084 16 ......... 1093 i 17 ......... 1089 18 ......... 1088 19 ......... 1085 20 ......... 1082 21 ......... 1086 22 ......... 1086 23 ......... 1087 24 ......... 396 25 ......... 0 26 ......... 0 27 ......... 0 28 ......... 444 29 ......... 1083
! 30 ......... 1095 t
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-424 DATE: MAY 3,1988 UNIT NAME: V0GTLE UNIT 1 COMPLETED BY: S. C. DILWORTH TELEPHONE: (404) 724-8114 r3870 REPORT MONTH APR 99 I I I I IR1 M !S I 1 1 I I I I IE1 EI I Y ! I i
! I ITI I AI T !LICENSEEl S C i 1 1 1 1 IYI 1S H EVENT 1 T 0 !COMPONENTI CAUSE & CORRECTIVE I I I I P IDURATIONI O 0 REPORT I E D 1 CODE I ACTION TO I I NO. I DATE I E f(HOURS) !N : 0: NUMBER I M E 1(SUBCODE)I PREVENT RECURRENCE I l 55~f'l556I6ft'F'!"56I25'l'6"~5':"57d~l'T3'~l"TCV""lS55' BEL 65""""'""""
I 88-8 18804241 F I 90.25 i A l 2: N/A I SJ ! ISV ISEE BELOW l l I I I 1 1 1, I I I !......l...l........l...l...l........l.....l.........l.............................I F FORCED REASON: METHOD: EVENTS REPORTED INVOLVF.
St SCHEDULED A-EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL A GREATER THAN 20%
B-MAINTENANCE OR TEST 2 - MANUAL SCRAM REDUCTION IN AVERAGE C-REFUELING 3 - AUTO. SCRAM DAILY POWER LEVEL FOR D-REGULATORY RESTRICTION 4 - CONT!NUATIONS THE PRECEEDING 24 HOURS.
E-OPERATOR TRAINING k LICENSE 5 - LOAD REDUCTION F-ADMINISTRATIVE 9 - OTHER (EXPLAIN)
G-OPERATIONAL ERROR (EXPLAIN)
H-0THER (EXPLAIN) 88-7 CAUSE: THE CAUSE OF THIS EVENT IS A FAILURE OF A LINKAGE SHAFT ON STATOR COOLING VALVE (1TCV-6000) TEMPERATURE CONTROLLER. V!BRATION OF UNDERLYING EQUIPMENT SK!D LED THE UNDERS!!ED LINKAGE SHAFT TO STRIP THE ENGAGED THREADS AND DROP OUT OF A NYLON THUMB NUT, GIVING A SIGNAL FOR ITCV-6800 TO CLOSE.
BB-7 CORRECTIVE ACTION: IMMEDIATE CORRECTIVE ACTION INCLUDES REPLACEMENT OF THE UNDERSIZED LINKAGE SHAFT WITH THE CORRECT S!!E SHAFT. .
98-9 CAUSE: REACTOR OPERATOR MANUALLY TRIPPED THE REACTOR IN ANTICIPATION OF AN AUTOMATIC TRIP DUE TO STEAM GENERATOR 84 LEVEL AT 421. OPERATORS WERE MANUALLY UNABLE TO OPEN LOOP 44 MAIN FEEDWATER ISOLATION VALVE.
THE VALVE WOULD NOT RESPOND TO AN OPEN SIGNAL.
98-8 CORRECTIVE ACTION: THE CORRECTIVE ACTION WAS TO REPLACE THOSE COMPONENTS WHICH ACTIVATE THE LOOP #4 MAIN FEEDWATER ISOLATION VALVE. THEY INCLUDE: FOUR RELAYS, TWO AGASTAT TIMERS AND TWO AIR SOLEN 0 IDS.
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AtiaMa, Gec<g'a 30308
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fbst O!t. .o Box 4545 ,
At:rta. Georg a 30302 .
R. P. Mc Donstd 1% $<Xtfco 6xBC 5rstem Esecutw Oce PresdeN tiacita 0;41stans SL-4661 0080m X7GJ17-V510 May 16, 1988 Director, Office of Resource Management :
U. S. Nuclear Regulatory Commission Washington, D.C. 20555 ..
PLANT V0GTLE - UNIT 1 NRC 00CKET 50-42 4 OPERATING LICENSF NPF-68 HONTHLY OPERAT 9G REPORT Gentlemen:
Enclosed is the Monthly Operating Report for Vogtle Unit 1 for -
April, 1988. This report is submitted in accordance with the requirements of Technical Specificaticn Section 6.8.1.5.
Sincerel3b I.P. Mcdonald ( .
6 JAE/Im
Enclosure:
- 1. Vogtle Unit 1 Monthly Operating Report for April, 1988 c: Georaia Power Comoany Mr. P. D. Rice Mr. G. Bockheid, Jr.
GO-NORMS U. S. Nuclear Reculatory Commission .
Dr. J. N. Grace, Regional Administrator Mr. J. B. Hopkins Licensing Project Manager, NRR (2 copies)
Mr. J. F. Rogge Senior Resident Inspector-0perations, Vogtle l
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