ML20154D139

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Monthly Operating Rept for Aug 1988 for Callaway Plant Unit 1
ML20154D139
Person / Time
Site: Callaway 
Issue date: 08/31/1988
From: Blosser J, Moser T
UNION ELECTRIC CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
ULNRC-1829, NUDOCS 8809150161
Download: ML20154D139 (6)


Text

"

s DOCKET NO.

50 483 UNIT NAME CAllAWAY UNIT 1 DATE 9 06 88 COMPLETID DY T. A. Hoser TELEPHONE 314/676 9291 PART A OPEPATIONS SUMhARY R* Plant operated at approximately 100% power with the fo11oving exceptions.

1) On August 22, 1988 power was reduced to 65% to remove

'B' Main Feed Pucp from service in order to repair a faulty pcver supply. Full power operation resumed on August 23, 1988

2) On August 30, 1988 a turbine runback resulted from a

'B' Circulating Water Pump trip caused by a loose ector thermoc Nple scanner output lead. Full pcver operation resuaed on August 30 folleving repair of the loose lead.

PART B PORY AMD SATITY YALYI SLWARY None I /

S809150161 880831 Fase 1 of 4 PDR ADOCK 050004s3 R

PDC

n 1

Part C l

AVERACE ')AILY UNIT POWER LEVEL i

l DOCKET No.

50 483 VNIT NAME CALLAWAY UNIT 1 DATE 9 06 88 l

t COfLETFD BY T. A. leser 1

TELEPHONE 314/676 8291 l

J i

J

!ONTH:

August 1983 l

AVERACE DAILY PokTR LEVIL AVERACE DAILY TC4TR LEVIL M

(MWe Net)

(M Net) i I

1 1123 17 1112

{

)

2 1137 18 1137 l

1 3

1133 19 1151 I

i i

4 1136 20 1152 4

i 5

1150 21 1151 i

4 6

1150 22 1104 I

7 1129 23 791 q

l a

8 1107 24 1142 l

9 1139 25 1158 1

10 1148 26 1166

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l i

l 11 1140 27 1164 i

12 1133 28 1172 i

13 1145 29 1173 14 1121 30 1132 15 1093 31 1167 I

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16 109e i

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P rt D OPERAT1hc DATA REP (AT DOCKIT NO.

50 483

'! NIT NAME CALLAWAY LHIT 1 DaTE 9 06 88 COMPLETID BY T. A. Moser TELEPHONE 314/676 8291 OPERATING STATV$

(YTD CtH )

1.

RIPORTINC PERIOD: AUCUST 1988 CP0S$ HOUD9 IN RIPORTING PERIOD:

744 5855 32437.5 2.

Ct1tRENTLT AUTBORIZED 1%TR LIVIL (MWt):

3565 MAX. DEFEND. CAFACIIT (We Net): 1120*

DESICN ELECIll! CAL PATINC (MWe Net):

1171 1.

POWER LEiEL TO WICH RISTRICTED (IF ANY) (MWe* Net):

4 RIASONS FOR RESTRICIION (IF AhY):

THIS MONTH YR TO DATE CtHULATIVE 5.

EtHBER OF HOURS REACTOR WAS CRITICAL...............

744

$447.4 27426.1 6.

REACTOR RISERVE SHUTDOW HOURS.....................

0 0

0 7.

HOURS CINERATOR ON LINI............................

744 5395.0 26849.5 8

UNIT RESERVE SHUTDOW Hot 1tS........................

0 0

0 9.

CROSS THERMAL EhERGY CDERATED (WW)...............

2,590,033 18,524,091 86,795,871 10 CROS$ ELECT 1t! CAL DERCY CDIRATED (MW)............

679,870 6,289,963 29,331,683 11 N ET ELECTRICAL DERGY CENERATID (5U)..............

838,897 5,986,481 27,795,524 12.

REACICR S ERVICF, FACTOR............................

100 93.0 64.6

13. REACTOR AVAILABILITY FACTOR........................

100 93.0 84.6

[

14 131T SERVICE FACTOR................................

100 92.1 82.8 l

l

15. UNIT AVAILA31LIIT FACTOR...........................

100 92.1 82.8 L

16 UNIT CAPACITY FACIOR (Using MDC)...................

100,7*

91.3*

76.5*

(

l 17 UNIT CATACITY FACTOR (Us ing te s ign MWe )............

96.3 87.3 73.2 i

Id. UNIT FORCED OL*TACI RATE............................

0 4.27 4.12

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19 SEUITGh3 $CEIDULID OYTR NIXT 6 HDNTES (TYPE, DATE AND DURATION OF EACH):

i 20 IT SWT DOW AT DD OF RIPORTIhC PER140, ESTIMATID DATI 0F STARTUP:

l

  • The unit capacity factor (usieg MDC) reflects use of the MDC value prior to utrating to 3565 Wt.

A uprated MDC value vill not te determined untti Iste in 1983.

Fage 3 of 4

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Part E 8

UNIT SIR:TDOWRS AhD F0WER REDUCTI3tS DOCKET NO.

50-483 CNIT RAPE CALIRAY IEEIT 1 DATE 9-06-88 QPfPLETED BY T. A. %ser TTH FHONE 314/676-8291 REFOKI NONTH: ADCUST 1988 METHOD 4 TTFE SifLTTINC DOWN Ts FORCED DURATION TIII RfACTOR OR DATE Sr SOrEDCLED (wx'Rs)

REASON RFICCINC F(ETR CORRECTIVE ACTIONS /(LPfG3ETS 16 8-22-88 5

0 A

1 De ste to repair the backup power supply on the

'S' P' in Feed Fump.

a 37 8-30-88 F

G A

4 Turbine rtaback due to a

'B' Circulating Water Pmp trip caused by a Icose motor thermocouple scatmer lead.

SUPMARTs REAT42 NETitre At EWIFMENT FAI!rRE (EIFIAIN) la MANUAL Br fu!NT. OR TEST 2: MA!CUAL SCRAM Cs REFLTLINC 3: AUIT9tATIC SCRAM Ds RECULATORT RIST1'ICTICIE 4: OTHER (EXI1AIN)

E OPERATLS TRAINIIIC AND LIQ 3SE EIAMIRATIO!E Fs ADMINISTFJLTIVE l

Cs CITRATIOMAL ERROR (EIFLAIN)

N CTI!ER (EIFLAIN)

Fage 4 of 4 l

1

Eu(.bNION zonuc 13 C h ayert September 6. 1988 Nuclear Regulatory Cornission Document Control Desk k'ashinsten. DC 20555 ULNRC-1829 Dear Sitt DOCKET NO2ER 50-483 CALLAk'AY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT l

Al'Cl'ST 1988 i

The enclosed Monthly Operating Report for August 1988 is submitted pursuant to section 6.9.1.8 of the Callaway L' nit 1 Technical Specifications.

14 Y J

D. Blosser Manager. Callavay Plant

/

p10 $N1V MET /DSH/ TAM /cre Enclosure cet Distribution attached I

un una eo a. e

.x r.ww

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j,

  • cc distribution for ULNRC-1829 l

1 with enclosures

?

Mr. Robert DePayette. Chief Project Section 1A p

U. S. Nuclear Regulatory Commission I

Region III 799 Roosevelt Read f

4 Glen Ellyn. IL 60137 i

4 Mr. Thomas Alexion (2 copies)

Office of Nuclear Reactor Regulation 1

U. S. Nuclear Regulatory Commission i

Mail Stop P-316

-t 7920 Norfolk Avenue

[

1 Bethesda MD 20014 f

NRC Resident Inspector Manager. Electric Department 1

i Misscuri Public Service Cornission j

P. O. Box 360 1

Jefferson City. Mo 65102 i

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