ML20154C869

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Univ of Utah Triga Reactor Annual Operating Rept for Jul 1987 - June 1988
ML20154C869
Person / Time
Site: University of Utah
Issue date: 06/30/1988
From: Gehmlich D, Sandquist G
UTAH, UNIV. OF, SALT LAKE CITY, UT
To: Alexander Adams
Office of Nuclear Reactor Regulation
References
NUDOCS 8809150060
Download: ML20154C869 (10)


Text

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.a The University of Utah TRIGA Reactor Annual Operating Report for the period 1 July 1987 through 30 June 1988 A.

NARRATIVE.

1. Operating Experience.

De TRIGA Reactor was critical 76.4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and generated 3,726.1 kWh of themial energy during this reporting year. De reactor was used for educational demonstrations, laboratory expenments, systems tests, power measurements, and sample irradiations. The reactor has not vb.;wd sin'c 31 hiarch 1988 as requested by NRC pending implementation of additi al adndt:istrative support by the Licensee.

2. Changes in Facility Design.

On 7/2/87, the Startup Channel fissic. :Smber was moved from its original position closer to the reactor core to increase the neutron count rate during reactor startup. He chamber signal was calibrated and the channel entered back into > ervice.

The Intrusion Alarm system was rewired on 10/21/87 to provide a signal which is compatible with a new computerized console at the University of Utah Police Station. The modification causes a reversal in the signal vohage polarity upon activation which actuates a burglar alarm on the display console in the event of the following:

(1) intrusion, (2) low water level in the TRIGA tank, or (3) high level radiation in the Nuclear Engineering Laboratory (NEL).

Interruption of the signal to the University Police because of loss of power to the alarm system or failura of t,e dedicated telephone line between NEL and the University Police Station results in the activation of a trouble light on the display console. The University Police are instructed to respond to both alavs in the same manner.

The linear power meter in the control console was disconnected on 1/27/88 to correct a grounding problem in the Linear Power Channel. This problem caused the initiation of a SCRAh! at certain times whi'.e switching from one watt to higher power levels during reactor startup. Although disconnecting the meter temporarily corrects the switching problem, staff members will continue to check the Linear Power Channel circuitry to isolate the source of the grounding problem. T?e Linear Power Channel signal was routed from the console to the computerized display in February 1986 as reported in the Annual Operating Report for the period 1 July 1985 to 30 June 1986.

On 3/15/88, the high voltage (IIV) supply coaxial cable to the uncompensated ion chamber in the Linear Power Channel was disconnected from the llV power supply located in the 18h1 Series /I computer stack (see below in the hiaintenance section). The cable was reconnected to the llV power supply in the control console thereby rectifying an unstable wwer signal to the Linear Power channel which w.as the result of a failed capacitor in the ilV pcwer supply of the computer stack.

A new emergency power supply was installed on 12 April 1988. De new system consists of two independent and redundant 12 volt DC batteries which su nly power to the radiological monitoring and intrusion alarm systems in the event of a but cing power failure.

3. Surveillance Tests.

8809150060 880630 PDR ADOCK 05000407 R

PDC

University of Utah TRIGA Reactor Annual Operating Report page 2 (Documentation of all surveillance activities is retained and stored by the facility.)

a. Control Rod Worths, e

Core ConAcuration #19 25 Aucust 1987 Safety Rod

$1.81 Shim-safety Rod

$1.34 Regulating Rod

$0.44 Excess Reactivity

$1.17 Shutdown hfargin

$0.61 Core Con Acuration #19 17 hf arth 1988 Safety Rod

$1.82 Shim safety Rod

$1.77 Regulating Rod

$0.39 Excess Reactivity

$1.05 Shutdown hiargin

$1.1)

b. Control Rod Inspection.

The Biennial Control Rod Inspection was performed December,1987 through February,1988. The control rods were sec uentially removed from the reactor core for visual inspection and then reinstalled. A'l rods were found to be in good condition with no observable deterioration having occurred since the previous inspection. Rod drop times were measured on 8/25/87 and 3/17/88. All rod drop times were less than 0.7 second.

J. Reactor Power Level Instrumentation.

Calorimetric power calibrations were performed on 8/19/87 and 2/2/88. 'Ihe following results were obtained.

. Data hieter Readine Actual Power Level 8/19/87 90 kW 75.6 kW 2/02/88 90 kW 97.2 kW

d. Fuel Inspection.

The Biennial Fuel Inspection was conducted December,1987 through hfarch,1988.

The discovery of a potential leaking fuel element (see below in the section pursuant to 10 CFR 50.59) prompted a detailed examination of fuel for cladding integrity. Each TRIGA fuel element was visually inspected while keeping the element submerged in the reactor tank for shielding purposes. Fuel elements showing discolorations or other indications of corrosion were noted for exchange with fuelin storage. Operating the reactor for a short period following the fuel exchange and then monitoring a water sample from the reactor tank for the presence of fission products was performed to ascertain if the source of the leakage had been renmved by the fuel exchange.

Although several elements with evidence of corrosion were noted, no obviously damaged fuel was observed during the inspection and the source of the leakage has not yet been determined.

c. Fuel Temperature Calibration.

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University of Utah TRIGA Reactor Annual Operating Report page 3 Fuel temperature circuits were calibrated on 8/20/87 and 2/18/88. 'Ihe circuits were calibrated to less than a 5 *C error over the range 20 'C to 500 *C.

f. Reactor Safety Committee Audits.

Reactor Safety Committee (RSC) member J. M. Byrne audited the maintenance and operational activities of the facility during February,1988.

University of Utah Radiation Safety Officer (RSO) and RSC member K. J. Schlager prepared an audit report and made recommendations concerning Monthly Inspections, Visitor leg, and Radiation Protection and Monitoring in January 1988.

g. Environmental Surveys.

RSO K. J. Schlager reported to the RSC a maximum net exposure of 10 millirem to environmental dosimeters located at various positions surrounding the NEL for the period July 1,1987 through June 30,1988.

h. Analysis of Water from TRIGA Fuel Storage Pits.

i The University of Utah Radiological IIcalth Department performed analyses of water samples taken from the three TRIGA Fuel Storage Pits on 10/28/87. Two of the tanks contained no detectable contamination and will be discharged to the sanitary sewer. The other tank, the North Storage Tank, was found to contain trace amounts of Cs 137 and Cef0 contamination. The volumetric activity of the Cs 137 and Co-60 was determined to be 1.6 x 104 pCi/ml and 9.5 x 10 6 Ci/ml, respectively. This contaminated water will be recirculated through the water purification system until the activity is well below 10 CFR 20 guidelines and then discharged.

B.

ENERGY OUTPUT.

The reactor was critical for 76.4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and produced 0.156 megawatt days (3726.2 kWh) of energy during this reporting period. Smce initial criticality, the reactor has been critical a total of 1,702.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> with an accumulated total energy output of 4.24 megawatt-days (101,770.5 kWh).

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C.

INADVERTENT SCRAMS.

I There were fiftcen inadvertent SCRAMS while the reactor was critical during the current re rting period. The type, cause, ant'

' n taken by the operations staff of each S M are outlined below:

Ouanti'y Tyne Cause Action 4

liigh Log Signal spike from Cautioned personnel.

Power bumping console (2).

Channel Noise and drift in channel Recalibrated channel, calibration (2).

6 Linear Signal spike during Restart.

Power switching power level (5).

Channel Drift in powerlevel at Cautioned operator to one watt during startup monitor all power meters, due to slight positive period (1).

s University of Utah TRIGA Reactor Annual Operating Report page 4 Ouantity Tvoe Cause Action 2

Power Failure Strong power fluctuation (2).

Restan.

1 Magnet Current Interruption of current Run terminated.'

Failure while attempting to connect x y plotter to Linear Power Channel during control rod wonh determination (1).

1 Area Perimeter alarm activated Cautioned personnel, by personnel opening rear door to perform maintenance (1).

I High level Hot sample removed Cautiomd Radiation from reactor (1).

experimenter.

Alann D. MAJOR MAINTENANCE.

On November 10-12,1987 the instrumented fuel element (IFE) was removed from the core to allow for visual inspection by the Reactor Supervisor. This element was suspected of being the source of the fission product leakage during reactor operations because of the amount of corrosion observed on the element and because of the recent physical manipulations of the IFE that occurred between June 8 24,1987 during thermocouple calibrations for verification of proper operation. Samples of the corrosion precipitate obtained from the element were analyzed and found to contain Cs 137 and other radionuclides suggesting the IFE was the source of the leakage. A replacement IFE was constructed from spare IFEs acquired from Nonhrup Corporation in 1986. Following the successful splicing of the three thermocouples to chromel/alumel thermocouple wire, the element was thoroughly tested for correct response to thermal stimuli. De replacement IFE was then inserted into the core adjacent to the suspect IFE to compare and calibrate its performance during reactor operation, ne old IFE was removed from the core and stored at the side of the reactor tank after the calibration of the replacement. On December 22,1987 the reactor was operated for a period of three hours during whic.h time no appreciable increase in radiation level was observed on any of the area radiation monitors. An analysis of a tank water samph taken at the conclusion of the run showed that fission products continued to be released despite removal of the IFE. De replacement IFE continued service throuch the end of the reporting period.

De dry tube irradiator was removed from the heavy water reflector tank during a January 8,1988 inspection of the assembly. Upon removal from the reactor tank, the polyethylene tubing was found to be severely damagen due to neutron embrittlement and was replaced.

Supp ementary ballast in the form oflead buckshot was added to the annular region of the canister to prevent it from accidentally floating out of the heavy water tank. The assembly was replaced in the heavy water tank and the top of the dry tube was securely fastened to a supporting beam at the top of the reactor tank.

De i 18 volt DC power supply in unit J10 of the control console was damaged 1/13/88 while the reactor was shutdown when a high voltage signal from a TINNELEC Counter Timer was inadvertently connected to the fission cham xr pre-amplifier to monitor the startup neutron count rate. The high voltage destroyed an integrated circuit chip in the pre amphfier thereby short circuiting the power supply outputs resulting in the burning of

University of Utah TRIGA Reactor Annual Operating Report page 5 two 26.8 volt power transformers and two power transistors. The damaged components were replaced with equivalent parts which were reviewed by the Reactor Supervisor for quality assurance. The unit was returned to service after verifying the operability of the mwer supply. Steps taken to prevent recurrence of this event include: (1) the counter has xen clearly labelled with a warning to not input a high-voltage signal while connected to the console, and (2) two fuses were installed in the i 18 volt power supply to preclude drawing too much current from its output.

On February 5,1988 the two uncompensated ion chambers (UIC) of the Linear and Per-cent Power Channels were disconnected from the Series /l computer and control console, respectively, for maintenance. During maintenance on the Linear Power Channel UIC in hiay,1987, the insulation of the coaxial cables was observed to be severely damaged by the mtense radiation field surrounding the reactor core. The condition of the cables was believed to be the cause of a very unstable signal from this channel which could not be used to calibrate the control rod worths. The decision was made to replace the signal and high voltage supply coaxial cables of both UICs since the two detectors share a common support assembly which secures them to the core structure. The cables and connectors were replaced and the detectors returned to their original positions. Both detectors were verified to be operational and were returned to service. A subsequent attempt to calibrate the control rod worths proved unsuccessful, however, due to the continuance of the unstable signal.

Further investigation showed the source of the problem was the superposition of an AC signal over the high voltage bias supply to the detector due to a failed capacitor in the high voltage power supply of the 1Bh1 computer stack. The bias supply was reconnected to the control console and the nomial, stable signal from the LNar Power Channel was recovered, thereby allowing the successful calibration of the control rod worths.

A series of false intrusion alarms during January and February,1988, was caused by the themial ex 3ansion of the metallic foil taped around the perimeter of the exterior windows of the NEL.

nsulated wire jumpers were installed across the window mullions to prevent the occurrence of more false alarms. The junctions between the old foil and the wires proved to be poor and resulted in further false alarms. NEL staff removed the existing foil from the exterior windows of the reactor room and the radiochemistry laboratories and applied new foil which improved the foll wire junctions. The entire system was retumed to service after the system was tested and verined to be operational.

During the NRC inspection of February,1988, removable contamination was found in the exhaust duct of the NEL ventilation system. The duct was decontaminated by NEL staff on 2/26/88. The contamination consisted of Co 60 which is transported by moist air and condenses on the relatively cool interior surfaces of the exhaust duct. The Reactor Supervisor performed a survey of areas of the exhaust stack and found no evidence of removable contamination. Subsequent surveys of the exhaust duct by Radiological llcalth Department personnel during monthly inspections of the facility have not shown further contamination.

'Ite Victorcen Area Radiation hionitor located above the entrance to classroom h1EB 1205 was sent to the U. S. EPA in Las Vegas, Nevada for calibration on 3/30/88.

E.

CilANGES, TESTS, AND EXPERlh1ENTS PURSUANT TO 10 CFR 50.59.

As of the end of the reporting eriod, the current membership of the Reactor Safety Committee (RSC) as designated b the Licensee is as follows:

Dietrich K. Gehmli h, Reactor Administrator Gary hl. Sandquist, Reactor Supervisor Keith J. Schlager, Radiation Safety OfScer John S. Bennion

s University of Utah TRIGA Reactor Annual Operating Repon page 6 John R. Burton James M. Byrne The presence of Cs-137 was discovered on 10/20/87 during routine monitoring of the ion exchange resin in the demineralizer tanks of the water purification system. The cesium indicated a possible leakage of fission products from a damaged or corroded fuel element.

Confinnation of the leakage was achieved on or about 11/11/87 with the demonstration that the majority of the activity contained in reactor water samples obtained subsequent to a one hour reactor run was due to relatively short lived noble gases, i.e., Kr 85m, t n = 4.5 i

hours, and Xe-135, t n = 9.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, as observed on an intrinsic germanium detector. He i

amount of activity released during short reactor operations was small-- well below levels of Co-60 contamination in the reactor tank incurred during the transfer of TRIGA fuel from a contaminated DOE fuel shipment cask in 1979; no abnormal increases in airborne activity had been observed. A program was devised to identify the source of the leakage and was reviewed and aoproved by the RSC. De program was designed to isolate the defective fuel element by exchanging incore with storage fuel and then operating the reactor for a short period of time. V/ater samples taken following the reactor oxration weie then counted to detennine if the leaking fuel element had been removed. A:1 reactor operations since the discovery of the cesium release were prformed in confonnance with TRIGA Technical Specification 4.4(3) which allows s tort term operation of the reactor to assist in determining the source of the fission product leakage.

During an inspection of the facility conducted by NRC on 16-19 February 1988, the Area Radiation Monitor (ARM) alann setpoints were observed to be 1.0 and 10.0 millirem per hour for the low-and high-level alarm setpoints, respectively. As pointed out by NRC, the Licensee had apparently indicated in question 46 in the 1983 84 TRIGA license renewal i

application addendum that the setpoint of the low level alann was 0.1 millirem per hour and tN setpoint of the high level alami was 1.0 millirem per hour. These values reported to NRC were typographical errors and are obviously too low to permit practical operations; the natural background radiation level in the area of the reactor facility is about 0.00 millirem per hour. The RSC reviewed this deviation and detennined that 1.0 and 10.0 millirem per hour setpoints are correct and acceptable and are adequate to insure proper response to radiological emergencies.

The RSC has reviewed and approved several NEL procedures which were modified to update and correct deficiencies noted in RSC audit reports and NRC inspections. Copies of the procedures have been sent to NRC Region IV. The NEL staff continues to review and update facility documentation to assure compliance with applicable regulations.

F.

RADIOACTIVE EFFLUENTS.

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1. Liquid Waste - Negligible.

Decontamination of removable Co-60 contamination from the accessible areas of the exhaust duct yielded approximately 2.5 gallons of liquid waste. The liquid was analyzed by the University of Utah Radiological llealth Department for activity content which was detem11ned to be approximately 4.6 x 104 pCi/ml. Since the activity of the liquid was 1

below 10 CFR 20 hmits for the unrestricted release of water, the waste was transferred to the Radiological llealth personnel for disposal on 5/2/88. The total amount of radioactivity released was estimated at 0.06 pCi.

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2. Gaseous Waste Negligible.

l De TRIGA Reactor was operated for 76.4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> at power levels up to approximately 90 l

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University of Utah TRIGA Reactor Annual Operating Report page 7 kW. At this power level argon-41 production is negligible. The minimum detectable concentration of Ar-41 for the stack monitor has been found to be one third of 10 CFR 20 appendix 11 limits for release to unrestricted areas. The average annual calculated concentration of Ar-41 generated during operations is estimated at 1.15 : 10-10 pCi/ml which is 0.3% of the hiPC for this radionuchde. The total amount of radioacdvity released was estimated at 26.0 pCi. A monthly summary of gaseous releases is given in Table I.

Table I.

Summary of Monthly Gascous Radioxtive Effluent

[

t July 1987 through 30 June 1988 Month Estinuted Release ( L1Cil July 1.4 August 7.4 September 1.2 October 0.5 l

November 2.0

)

December 1.7 t

January 5.4 Fetwuary 1.8 March 4.6 April 0.0 May 0.0 June 0.0 Total activity of gaseous effluenu 26.0

3. Solid Waste - None.

Approximately 0.5 cubic meter of solid waste was generated by the facility during the reporting pen,od. This waste consists of low level decontamination materials, debris removed from the reactor tank during cleaning, and radioactive reactor components which i

have been replaced during maintenance -- such as the ends of the UIC coaxial cables which were proximal to the reactor core. The waste is being stored in the Controlled Access Area of the facility pending transfer to the Radiological IIcalth Department for disposal.

O.

RADIATION EXPOSURES.

Personnel with duties in the reactor laboratory on either a regular or occasional basis I

have been issued a film badge dosimeter by the University of Utah Radiological llealth 1

Department. The duty category and monitoring period of personnel are summarized below Name hionitoring Period Duty Category f

1 G. ht. Sandquist 1/87 12/87;1/88 6/88 regular j

T. C. Gansauge 1/87 12/87;1/88 6/88 regular J. S. Bennion 1/87 12/87;1/88 6/88 regular V. Tang 1/88 6/88 regular K. C. Crawford 1/87 6/87 regular C. IIenderson 3/88-6/88 occasional hl. Tolle 1/87 12/87;1/88 6/88 terminated R. Deadman 1/87 9/87 terminated

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University of Utah TRIGA Reactor e

Annual Operating Report page 8 Dose liquivalent summary for Reporting Period:

Measured Doses 1987 Annual Doses: 10 mrem average; 30 mrem highest measured.

January - June,1988: 10 mrem highest measured.

Dose Eaulvalent Limits hiaximum Permissible Dose Equivalent = 5000 mrem / year (1250/quaner).

Minimum Detectable per Monthly Badge = 10 mrem.

Of the 639 visitors to the facility under the DOE Reactor Sharing Program for the reporting year, no visitor received a measurable dose. Therefore, the average and maximum doses are all within NRC guidelines. A summary of whole body exposures is presented in Table II.

Table II.

Summary of Whole Body Exposures 1 July 1987 through 30 June 1988 Estimated whole body exposure Number ofindividuals in range (rems):

each range:

No Measurable Dose 2

1. css than 0.10 6

0.10 to 0.25 0

0.25 to 0.50 0

0.50 to 0.75 0

0.75 to 1.00 0

1.00 to 2.00 0

2.00 to 3.00 0

3.00 to 4.00 0

4.00 to 5.00 0

Gresar than 5 0

Total number of individu21s reported 8

II. IABORATORY SURVEYS.

hionthly surveys of the facility were conducted by the University of Utah Radiological llealth Department during the reporting period. Some of these surveys have identified removable contamination sources which were immediately cleaned. The surveys have indicated no increase in radiation levels over previous years. Records of surveys are retained by the facility.

I.

ENVIRONMENTAL SURVEYS.

The Air Monitoring Station, operated by the Environmental Protection Agency and located outside the reactor building, has indicated no unusual changes in radiation or radioactive material concentrations dunng the reporting period.

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University of Utah TRIGA Reactor Annual Operating Report page 9 Environmental surveys conducted quarterly by the University of Utah Radiological Health Department indicated no unusual dose rates in the areas surrounding the Merrill Engineering Building, which houses the reactor facility, or anywhere on the Umversity of Utah campus.

~ Prepared by: A2(WU f&

4/t'dd Date: Sl M l$$h ca'ct5 isor p'

Approved by:'

M n'

Date: 8 (f

Reactor Administrator f

THE UMVERSITY

Project Manager Standardization and Non Power Reactor Propet Directorate Division of Reactor Projects - 111, IV, V and Special Projects Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D. C. 20555

Dear Mr. Adams:

Enclosed you will find a copy of the Annual Operating Report for the University of Utah TRIGA Reactor, Docket No. 50-407, for the period 1 July 1987 through 30 June 1988.

His report fulfills the requirements of TRIGA Technical Specification 6.10(5).

Please contact the operations staff at (801) 581-4188 with any questions you may have concerning the report.

Sincerely,

$ 5 Dietrich K. Gehmlich, PhD.

Reactor Administrator cy: Regional Administrator, NRC Region IV l

College of F.ngIncering Ottee of the Dean 1

eLt ta M 112 Teleptw>ne (Wil s91-6911 I

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