ML20151X764

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 880223-0404.Violation Noted:Manual Suction Isolation Valve 3FWA-V2 Found Not Locked Open,Per Procedure ACP-QA-2.12
ML20151X764
Person / Time
Site: Millstone Dominion icon.png
Issue date: 04/25/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20151X762 List:
References
50-423-88-05, 50-423-88-5, NUDOCS 8805040244
Download: ML20151X764 (1)


Text

4 ,

is.. ,

I APPENDIX A NOTICE OF VIOLATION Northeast Nuclear Energy Company Docket No. 50-423 Millstone Unit 3 License No NPF-49 During NRC inspection from February.23 to April 4, 1988, a violation of NRC re-

. quirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 crd Part 2, Appendix C, that vio-lation is listed below:

Technical Specification 6.8.1 requires implementation of administrative prc-cedures for equipment control (e.g., locking and tagging) as specified in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Administra-tive Procedure ACP-QA-2.12 requires that system alignments be verified to be in accordance with their valve lineup. The Operating Procedure OP-3222 valve lineup for Auxiliary Feedwater specifies that manual suction isolation valve 3FWA-V2 be "Locked Open."

Contrary to the above, ACP-QA-2.12 was not acceptably implemented as of 3:30 p.m., March 4, 1988, in that valve 3FVA-V2 could have been operated without being unlocked. The valve was, however, in the required open position, and was locked open promptly when the inspector notified the control room of the valve's status.

This is a Severity Level IV Violation (Supplement I.E.).

Pursuant to 10 CFR 2.201, Northeast Nuclear Energy Company is required to submit to this-office, within 30 days of the date of the letter transmitting this Notice, a written reply Including: (1) the cotrective steps which have been taken and the results achieved, (2) the corrective shps which will be taken to avoid further violations, and (3) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

OFFICIAL RECC90 COPY DL50-423/68 0003.0.0 8805040244 880425 04/19/88 PDR ADOCK 05000423 O DCD

- _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _