ML20151E035

From kanterella
Jump to navigation Jump to search
Requests That 880622 Amend Application Re UHS Be Processed Under Emergency Provisions of 10CFR50.91a(5) for OL NPF-66. Request Based on Discussed 880714 Breaker Event
ML20151E035
Person / Time
Site: Byron Constellation icon.png
Issue date: 07/14/1988
From: Lentine F
COMMONWEALTH EDISON CO.
To: Murley T
Office of Nuclear Reactor Regulation
References
4925K, NUDOCS 8807250338
Download: ML20151E035 (3)


Text

..

Commonwealth Edison 2

/

One First Nabonal Plaza. Chicago, Illinois -

' @V Address Reply to: Poet Omco Box 76,7

'u CNeago, lainois 6061,0 0767 July 14, 1988 Mr. Thomas E. Murley Director of Nuclear Reactor Regulation U.S. Nuclear-Regulatory Commission Mail Station P1-137 Washington, DC 20555

Subject:

Byron Station Unit 2

-Application for Amendment to Facility Operating License NPF-66 Appendix A, Technical Specifications NRC Docket No. 50-45_5 Reference (a):

June 22, 1988 K.A. Ainger letter to T.E. Murley

Dear Mr. Murley:

1 Pursuant to 10 CFR 50.90, reference (a) provided Commonwealth Edison's application for an amendment to Facility Operating Licenses NPF-37 and NPF-66, Appendix A Technical Specifications.

The purpose of this amendment is to revise a

' technical ~ specification action statement concerning the ultimate heat sink.

The particular action statement involves Rock River water level and flow.

Attachment A to reference (a) contains the proposed change to action requirement 3.7.5.e.(2).

Attachment B to reference (a) contains background information regarding the proposed change.

l The purpose of this letter is to request that this amendment be processed under the emergency provisions of 10CFR 50.91a(5) for Facility Operating License NPF-66.

At approximately 1:14a.m. on Thursday, July 14, 1988, Bfron Unit 2 experienced an unexpected shutdown due to the inadvertent opening of the two feeder breakers that connect the Unit Aux and System Aux Transformers to the Unit 2 non-safety related bus, which fo l

o 8807250339 880714 g

{DR ADOCK 05000455 I

PDC

_ _ _ _ _ {

5 resulted in the loos of the 2C feedwater pump.

The unit is currently in Mode 3.

As stated in Attachment B to reference (a),

I the ongoing drought in the mid-western part of the nation has caused 2

the level in the Rock River to drop below the limit specified in the limiting condition for operation of the ultimate heat sink technical

=

specification.

That limit is 670.6 feet mean sea level (hSL).

As a result, Byton Station has entered technical specification action 4

requirement 3.7.5.e.

This action requirement permits reactor i

operation to continue for an unlimited period of time as long as river flow remains greater than 700 cubic feet per second (cfs) and

[3 river level remains above 664.7 feet MSL.

Since entering the action requirement, the river level has fluctuated between 670 feet E

- 3 inches and 670 feet - 8 inches and river flow has fluctuated between approximately 1250 cfs and 2100 cfs.

Therefore, substantial PD margin to the technical specification minimum values currently

[

exists.

River flow must be verified every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> under these conditions until the level excees 670.6 feet MSL.

W General technical specification 3.0.4 applies to technical E-specification 3.7.5.

According to specification 3.0.4, entry into E;

an operational mode or other specified condition cannot be made g;

unless the conditions of the limiting condition for operation are met without reliance on provisions contained in the action E-l!

requirements.

As a result, Byron Unit 2 cannot startup until the Rock River level exceeds 670.6 feet MSL.

{

E Edison's service territory is expected to see temperatures greater than 900F through at least Monday, July 18, 1988, with ur today's peak load estimated at 15,500 MW.

Other Commonwealth Edison E=

units down in addition to Byron 2 include Zion 1, Crawford 8 and F-Collins 5.

There are also deratings on Dresden, Quad Cities and LaSalle due to river and lake temperature limitations.

As a result, lg Byron Unit 2 is needed to provide power to the service territory and g-needs to be returned to service as soon as possible.

Current plans k

are to return Unit 2 to service at 3:00P.M. on July 14, 1988.

Commonwealth Edison believes that it has taken actions

-p-necessary to try to prevent an emergency situation from occurring.

The proposed Technical Specification amendment was submitted as soon

[

as the potential for such a situation was recognized, and today's unit trip could not have been anticipated.

Processing the Technical Specification change under the emergency provision of 10CFR 50.91(5) ir r

will allow startup to occur with the required river flow being

-F-verified.

This ensures an acceptable level of safety for unlimited continued operation while eliminating an unnecessary restriction on unit startups.

K.

b 7

\\

3

.e*

Please-direct any questions you may have concerning this matter to this office.

Very truly yours, N

F. G. Lentine PWR Licensing Supervisor cc:

Byron Resident Inspector L. N. 01shan - NRR Regional Administrator - RIII 4925K i

1

..