ML20151C176

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AO 73-32:on 731217 & 18,test Spool Valve for MSIV NS04A Failed to Properly Reset & Pressure Transients Experienced During 5% Closure Test.Caused by Valve Sticking Possibly Due to Foreign Matl Found Between Spool & Sleeve Assembly
ML20151C176
Person / Time
Site: Oyster Creek
Issue date: 12/20/1973
From: Rone A
JERSEY CENTRAL POWER & LIGHT CO.
To:
References
AO-73-32, NUDOCS 8103040891
Download: ML20151C176 (3)


Text

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Prellminary Abnormal occurrence Report No. 73-32

SUBJECT:

Failure of the test spool valve for NSO4A to properly ree.et after 5% closure test whidt resulted in it condition which may have cai,thed the FGIV to close slower-thrin norTnal should an ' isolation signal have occurred during the test Interval.

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e This event is considered to be an abnorrnal occurrence as defined in the Technical Specifications, paragraph 1.150 Notification of this event, as required by the, Technical Specifications, para-graph 6.6.2.a, was rade to AEC P.egion I, Directorate of Regultitory Operntions, by telephone on %ursday, Dece dier 20,1975 at 0900, and by telecopier at 1500.

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SITUATION:

it h.ad besn observed on~ Deceidier 17 nnd 18 that HSIV NSO4A was

.apparently overtravelling durinh the daily 5% closure exercise, thereby causing pressure transients of 6 psig and 10 pF res-N.

poetively.

Analysis of the. problem indicated that r

I overtravel was a result of the improper resetting cf the test spool v41ve.

To explore this possibility, reactor'pwcr was ro-duced to 853 ftit (<.40i of rated power) so that further excuzino-

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t. ion of the test spool valve. assechly could be conducted with reduced possibility of a reactor scr;un due.to Valve closure,

'and to reduce radiation levels in the work arcs.

THIS DOCUMENT CONTAINS POOR QUAUTY PAGES

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l Pre 11mii.ary Abnormal Occurrence f

Report flo. 73-32 k vececher 19, 1973 r

i The 5% valve closure test was redone with an instrument techni-I cian in local observance of the test, The sticking condition l

l bd apparently worsened, thereby catsing the161V to go approxi-mately 50% closed and then reopen in the normal manner. The technician concluded that the test valve was the cause of the

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1hus, a situation wns created whereby had the va..lve..

been required to isolato during the test interval (approximately-2-3 minutes) it is unlikely that it would have het the. required closure tiene of <10 seconds, sinco exhmut air from the tmder-side of the valve operator piston is required to pus through t

the test valve assorbly. BecauJsc of the malpositioned valve assembly, the er.haust air would have.bcen restricted, thereby-slowing the valve closure time.

g tipunk', removal tmd disassenbly of the test spool valvo, it was observed that foreign ruterial resenbling red powdct was found on imd between the spool and s1covo essembly, although it has o

not bocn conclusively determined that' this wits the cause of the V31Vc stickln2, 7he spool asserbly is being sent to a testing 2

lab for.further cyliluation.

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l The test spool y ve asser11y for NSO4A wm replaced. 1he 5%

1 closure tost w.w. repeated satisfactorily,.as well to a full closurv titeing test (6.7 seconds).

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Prelitinary

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Ahnut=31 Occurrence

- Report"po, '73 32 ;;cer.bor 19, 1973 s

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SAFET( SIfNJFICO!G:

haring-the 51, closure test, had an isolation signal boon intro-duced, the valve may not have closed in the required time. The conscquences of this cVent were minimized since the redundsnt i

valve NS03A would have provided isolation and closed 'in the re-quired tir.4, in the event of a reactor isolation. Furthemore,

the " slow closure condition" was only present for the length of tinee the 5% closure test was in })rogress (2 3 minuteij.

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