ML20151C165

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Forwards Insp Repts 50-321/88-12 & 50-366/88-12 on 880502-12.Emergency Operating Procedures Adequate for Continued Plant Operation,Although Numerous Deficiencies Identified
ML20151C165
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 07/06/1988
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Hairston W
GEORGIA POWER CO.
Shared Package
ML20151C170 List:
References
NUDOCS 8807210246
Download: ML20151C165 (3)


See also: IR 05000321/1988012

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July

'6,' 1988

. Docket Nos. 50-321, 50-366

License Nos. DPR-57, NPF-5.

Georgia Power Company

ATTN: Mr. W. G. Hairston, III

Senior Vice President -

Nuclear Operations

P. O. Box 4545

Atlanta, GA 30302

Gentlemen:

SUBJECT: EMERGENCY OPERATING PROCEDURE TEAM INSPECTION

(NRCINSPECTIONREPORTNOS. 50-321/88-12 and 50-366/88-12)

This refers to the Nuclear Regulatory Commission (NRC) inspection conducted by

an NRC team led by Mr. Donald J. Florek on May 2-10, 1988, at Hatch Units 1

and 2.

The inspection included a review of Esr.ergency Operating Procedurcs

for your Hatch facility.

At the conclusion of the inspection, the findings

were discussed with Mr. J. T. Beckham, Jr. and other members of your staff

identified in the enclosed Inspection Report.

Areas examined during the inspection are identified in the report.

Within

these areas, the inspection consisted of selective examinations of procedures

and representative records, interviews with personnel, and observation of

activities in progress.

The inspection findings ident;fied several items that require actions to be

taken ori the Emergency Operating Procedures, associated supporting documenta-

tion, and training.

At tha exit, your staff indicated that a well discir'ined

approach would be taken to correct the findings and that a plan would be

developed and provided to the NRC.

We also consider that a well disciplined

timely approach to resolve the inspection findings is required.

Please

fonnally transmit your plans and schedule to Region II within 30 days of

receipt of this letter.

Although numerous deficiencies were identified, the Emergercy Operating

Procedures were found to be adequate for continued operation of the facility.

While none of the individual deficiencies observed during this inspection and

documented in this report are identified as violations or deviations, the large

number of them reduces the margin of safety by placing unnecessary demands on

the operators.

To restore this margin of safety, prompt corrective action is

appropriate. As discussed during the exit meeting following ti.. inspection, we

understand that Georgia Power Company will review the indiviAal deficiencies

noted in this report and take prompt corrective action to resolve them on a

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July 6, 1988

prioritized schedule.

This review and corrective action will specifically

address identification and elimination of potential programmatic weaknesses.

In addition, we understand that the technical bases for differences between

the BWR Owners Group Emergency Procedure Guidelines and Emergency Operating

Procedures are not documented.

Your corrective action should include estab-

'lishing this . documentation.

As we have discussed, you will meet with us in

Atlanta in the near future to discuss your progress and schedule for completing

this action.

In accordance with Section 2.790 of the NRC's "Rules of Practice," Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its enclosure

will be' placed in the NRC Public Document Room.

The responses directed by this letter and the enclosure are not subject to

-the clearance procedures of the Office of Management and Budget issued under

the Paperwork Reduction Act of 1980, Pub. L; No.96-511.

Should you have any questions concerning this letter, please contact us.

Sincerely,

(Original signed by J. Nelson Grace)

J. Nelson Grace

Regional Administrator

Enclosure:

NRC Inspection Report

cc w/ encl:

R. P. Mcdonald, Executive Vice

President, Nuclear Operations

J. T. Beckham, Vice President,

Plant Hatch

H. C. Nix, Plant Manager

0. M. Fraser, Site Quality Assurance

(QA) Supervisor

L. Gucwa, Manager, Nuclear Safety

and Licensing

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July 6, 1988

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