ML20151C126

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Notice of Violation from Insp on 880220-0318.Violation Noted:Jumpered Terminals 9 to 10 on Ground Overcurrent Relay on Breaker 152-1609 Instead of 152-1606 & Failure to Document Installation of Equipment in Condenser Offgas Sys
ML20151C126
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 04/05/1988
From: Verrelli D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151C122 List:
References
50-416-88-03, 50-416-88-3, NUDOCS 8804120167
Download: ML20151C126 (2)


Text

_.

r ENCLOSURE 1 NOTICE OF VIOLATION System Energy Resources, Inc.

Docket No.50-416 Grand Gulf License No. NPF-29 During the Nuclear Regulatory Commission (NRC) inspection conducted on February 20 - March 18,1988, a violation of NRC requirements was identified.

In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1987), the violation is listed below:

Technical Specification 6.8.1 requires that written procedures be established, implemented and maintained covering surveillance activities-of safety related equipment and applicable procedures recommended in Regulatory Guide (RG) 1.33. RG 1.33 recommends administrative procedures covering procedural adherence.

Surveillance Prccedure 06-EL-1E12-M-0001, paragraph 5.3.1 states to jumper terminals 9 to 10 on the ground over-current relay on breaker 152-1606.

Administrative Procedure 01-S-07-1, Control of Work on Plant Equipment and Facilities, paragraph 6.3, provides for work accomplishment per the Shift Superintendents verbal directions during critical events and requires immediate subsequent initiation of a Maintenance Work Order for documentation of work accomplished.

Contrary to the above:

1.

On March 17, 1988, to prevent auto-start of the B residual heat removal pump, a technician jumpered terminals 9 to 10 on the ground overcurrent relay on breaker 152-1609 instead of breaker 152-1606, specified by the procedure, resulting in the auto-start of the pump.

J 2.

On February 27, 1988, following a hydrogen ignition in the condenser offgas system, the Shift Superintendent directed the installation of equipment necessary to put a nitrogen blanket on the offgas system charcoal adsorbers. As of March 10, 1988, no documentation of work accomplished had been initiated.

This is a Severity Level IV Violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, System Energy Resources, Inc. is hereby required to submit to this Office within 30 days of the date of the letter transmitting this Notice a written statement or explanation in reply including (for each violation):

(1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will 8804120167 880405 PDR ADOCK 05000416 O

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System Energy Resources, Inc.

2 Docket No.50-416 Grand Gulf License No. NPF-29 be taken to avoid further violations, and (5) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

FOR THE NUCLEAR REGULATORY COMMISSION David M. Verrelli, Chief Reactor Projects Branch 1 Division of Reactor Projects Dated at Atlanta, Georgia this 5thday of April 1988 i

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