ML20151B017

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Monthly Operating Rept for June 1988 for Limerick Unit 1
ML20151B017
Person / Time
Site: Limerick Constellation icon.png
Issue date: 06/30/1988
From: Alden W, Gropp R
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
NUDOCS 8807200206
Download: ML20151B017 (6)


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DOCKET No. 50 - 352 UNIT LIMERICK UNIT 1 DATE JULY 15, 1988 COMPANY PHILADELPHIA ELECTRIC COMPANY R. H. GROPP

. TECHNICAL ASSISTANT LICEtGING SECTICH NJCLEAR SUPPORT DEPARTMENT TELEPHONE I215) 841-5058

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Morf7H JUNE 1988 DAY AVERAGE DAILY P0HER LEVEL DAY AVERAGE DAILY POHER LEVEL IINE-NET) iPNE-NET) 1 915 17 872 2

934 18 860 3

926 19 859 4

925 to 857 5

925 21 859 6

915 22 861 7

893 23 846 8

872 24 868 9

875 25 869 10 788 26 859 11 816 27 871 12 783 28 868 13 858 29 868 14 860 30 875 15 855 16 860 i

8807200206 880630',_

ADOCK 050003 2 j

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OPERATING DATA REPORT DOCKET NO. 50 - 352 v.

DATE JULY 15, 1988 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY

k. H. GROPP TECHNICAL ASSISTANT LICENSING SECTION p

PAJCLEAR SUPPORT DEPARTMENT TELEPHONE I215) 841-5058 OPERATING STATUS

1. UNIT NAME LIMERICK UNIT 1 l NOTESS UNIT 1 EXPERIENCED NO l

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2. REPORTING PERIODI JUNE, 1988 l

OUTAGES DURING THE l

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3. LICEIGED THERMAL P0HERitWT):

3293 l

MONTH. P0HER IS BEING l

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C. NAMEPLATE RATING (GROSS MNE ll 1138 l

ADMINISTRATIVELY LIMITED l

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S. DESIGN ELECTRICAL RATING (HET MHEll 1055 i

DUE TO A FUEL ROD LEAK.

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6. MAXIMUM DEPENDABLE CAPACITY (GROSS HHEll 1092 l

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7. MAXIMUM DEPENDABLE CAPACITY INET MHE) 1055 l
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUteER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONSI
9. P0HER LEVEL TO HHICH RESTRICTED, IF ANY INET MHEll 949.5 Power Restricted due to a
10. REASO G FOR RESTRICTI0tGe IF ANY8 Fuel Rod Leak

'THIS MONTH YR-TO-DATE

' CUMULATIVE

11. HOURS IN REPORT 1HG PERIOD 720 4:367 21:143
12. nut 1BER OF HOURS REACTOR KAS CRITICAL 720.0 4,059.3 16,927.3
13. REACTOR RESERVE SHUTDOHN HOURS 0.0 0.0 0.0
14. HOURS GENERATOR ON-lit 4E 720.0 4,053.0 16,615.7
15. UNIT RESERVE SHUTDOHN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MHH) 2.031.458 12,309.060 51,205 441
17. GROSS ELECTRICAL ENERGY GENERATED (MHH) 653.530 3.976.400 16,675,810
18. NET ELECTRICAL ENERGY GENERATED IMHH) 626,195 3.825,081 15e992,918 PAGE 1 0F 2

OPERAfhi?

~ ii' DOCKET No. 50 - 352' DATE JULY 15, 1988

.........n...................

THIS HONTH YR-TO-DATE CUNULATIVE

19. UNIT SERVICE FACTOR 100.0 92.8 78.6
20. UNIT AVAILASILITY FACTOR 100.0 92.8 78.6 21.' UNIT CAPACITY FACTOR IUSING MDC NET)

.82.4 83.0 71.7

22. UNIT *APACITY FACTOR (USING DER NET) 82.4 83.0 71.7
23. UNIT FORCEO OUTAGE RATE 0.0 7.2 4.6
24. SHUTD06fG SCHEDULED OVER NEXT 6 MONTMS (TYPE, DATE, AND DURATION OF EACH)
25. IF SHUTDOM1 AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUPs
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION)

FORECAST ACHIEVED INITIAL CRITICALITY 1E/19/84 12/22/64 INITIAL ELECTRICITY MID APRIL 85 4/13/85

.~.......

COMMERCIAL OPERATION IST QTR 86 2/01/86 J

PAGE 2 0F 2 i

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UNIT SHUTDODNS AND P0HER REDUCTIONS DOCKET No. 50 - 352 UNIT NAME LIMERICK LNIT 1 DATE JULY 15, 1988 REPORT MONTH JUNE, 1988

  • 0MPLETED BY PHILADELPHIA ELECTRIC COMPAt#

R. H. GROPP TECHNICAL ASSISTANT LICENSING SECTION NUCLEAR SUPPORT DEPARTMENT TELEPHONE (215) 841-5058 l

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l l NETH03 0F 1 LICEtCEE lSYSTEHlCOMP0tlENTl CAUSE AND CORRECTIVE l

l TY PE l DURATION I RE ASON I SHUTTING D06+41 EVENT l CODE l CODE l ACTION TO J.l DATE I 11)l IHOURSil (2) l AEACTOR (3) l REPORT 8 l (4) l

15) l PREVENT RECURRENCE 1

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i (1)

(2)

(3)

(4)

. F!RCED REASON METHOD EXHIBIT G - ItGTRUCTIONS

- SCHEDULED A - EQUIPHENT FAILURE (EXPLAIN) 1 - MAtAJAL FOR PREPARATION OF DATA B - itAINTENANCE OR TEST 2

MANUAL SCRAM.

ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.

IVENT REPORT (LER)

D - REGULATORY RESTRICTION 4 - OTHER IEXPLAIN)

FILE lifJREG-0161)

E - OPERATOR TRAINING + LICEtCE EXAMINATION F - ADMINISTRATIVE (5)

G - OPERATIONAL ERROR (EXPLAIN)

H - OTHERIEXPLAIN)

EXHIBIT I - SAME SOURCE a

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Docket No. 50-352 Attachment _to Monthly Oparating Report for June, 1988 Limerick Generating Station Unit 1 June 1 through June 30, 1988 I.

Narrative Summary of Operating Experiences The unit began the report period operating at approximately PO\\ power limited by a fuel rod leak.

On June 7, 1988, reactor power was further reduced and maintained at approximately 85% due to an increase in condenser offgas activity caused by the fuel rod leak.

On June 10, 1988 reactor power was reduced to approximately 65% when a failure of the "5C" feedwater heater level controllers caused a reduction in feedwater hercing and an unexpectcd increase in core reactivity.

The ' 5C" level controllers were repaired and the unit was ristored to approximately 85% by June 12, 1988.

On June 13, 1988, while attempting to stcrt the "lB" Reactor Enclosure Circulating Water (RECW) pump, an electrical arc occurred damaging a MCC bus bar and tripping the supply breaker to the MCC.

This loss of power resulted in the inoperability of the "D" RHR loop, "B" RHRSW loop, "D" Core Spray pump, "B"

Post-LOCA recombiner, and various primary containment isolation valves.

Power was restored and the systems were declared operable within 55 minutes.

No load reduction was experienced as a result of this event and the bus bar was replaced by June 15, 1988.

The Unit ended the report period operating at app 3 6ximately 85% power limited by a fuel rod leak.

II. Challenges to Main Steam Safety Relief Valves There were no challenges to the Main SteE. Relief valves during the month of June.

72

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PHILADELPHIA ELECTRIC COMPANY-2'.

M ARKET ST REET s

P.O. BOX 8690 PHILADELPHI A, PA.19101 (215)8484000 July 13, 1988 Docket No. 50-352 g

Director Office of Resource Management U.S.

Nuclear. Regulatory Commission Washington, DC 20555 Attention:

Document Control Desk

SUBJECT:

Limerick Generating Station Monthly Operating Report Gentlemen:

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Enclosed is the monthly operating report for Limerick Unit 1 for the month of June, 1988, forwarded pursaant to Technical Specification 6.9.1.6.

Very truly yours, l

hb-W. M. Alden Director Licensing Section Nuclear Support Division Enclosure cc:

Director, Office of Inspection & Enforcement, USNRC (12 copies)

William T. Russell, Administrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector Mr. David E. Ney, PA Dept. of Envir. Resources Mr. W.

H.

Lovelace, NRC (2 copies)

INPO Records Center 8

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