Notice of Deviation from Insp on 871202-880105.Deviation Noted:Calculation Package Incorrectly Dated & Isometrics for Conduit Runs Incorrectly Depicted & MeasuredML20149J659 |
Person / Time |
---|
Site: |
Comanche Peak ![Luminant icon.png](/w/images/d/d7/Luminant_icon.png) |
---|
Issue date: |
02/12/1988 |
---|
From: |
Warnick R NRC OFFICE OF SPECIAL PROJECTS |
---|
To: |
|
---|
Shared Package |
---|
ML20149J607 |
List: |
---|
References |
---|
50-445-87-35, 50-446-87-26, NUDOCS 8802230165 |
Download: ML20149J659 (3) |
|
|
---|
Category:NOTICE OF DEVIATION/NONCONFORMANCE FROM A REGULATORY
MONTHYEARML20248A6681989-09-26026 September 1989 Notice of Deviation from Insp on 890802-0905.Deviation Noted:Applicant Did Not Replace Nonqualified Class 1E Diesel Generator Wattmeters W/Qualified Components,Per Util 880325 Commitment ML20147G7121988-03-0202 March 1988 Notice of Deviation from Insp on 880105-0202.Deviation Noted:Nonconformance Rept NCR-87-A00491 & QC Hold Point Not Trended as Required by FSAR to Identify Any Trend Adverse to Quality ML20149J6591988-02-12012 February 1988 Notice of Deviation from Insp on 871202-880105.Deviation Noted:Calculation Package Incorrectly Dated & Isometrics for Conduit Runs Incorrectly Depicted & Measured IR 07100104/20120011987-12-18018 December 1987 Notice of Deviation from Insp on 871104-1201.Deviation Noted:Baseplate Reported to Be 8 Inches Long Found by NRC Inspector to Be 9 Inches Long ML20237D7291987-12-16016 December 1987 Notice of Deviation from Insp on 871104-1201.Deviation Noted:Checklist Attribute 20.2 Incorrectly Verified as 3/4 Inches Npt ML20236L9191987-11-0505 November 1987 Notice of Deviation from Insp on 870903-1006.Deviation Noted:Performance Guidelines for Conduit Support & Routing Walkdowns Not Followed ML20236C6101987-10-23023 October 1987 Notice of Deviation from Insp on 870805-0902.Deviation Noted:Administrative Controls Not Contained in Procedure to Ensure Adequate Retesting of Sys or Design Features Which Have Been Maintained or Modified Following Testing ML20237G3081987-08-0505 August 1987 Notice of Deviation from Insp on 870301-0430.Deviations Noted:Rev 24 to B&R Procedure QI-QAP-11.1.28 Not Revised to Require QC Inspector to Assign Weld Number to Each Weld Shown on Design Drawing & to Document Weld Size ML20216C1801987-06-22022 June 1987 Notice of Deviation from Insp on 870101-0228 ML20214R9351987-06-0101 June 1987 Notice of Deviation from Insp on 861101-1231 ML20206E7981987-04-0202 April 1987 Notice of Deviation from Insp on 860901-1031 ML20205L2351987-03-30030 March 1987 Notice of Deviation from Insp on 860401-0531 ML20205D1021987-03-18018 March 1987 Notice of Deviation from Insp on 860701-0831 ML20207E0131986-12-22022 December 1986 Notice of Deviation from Insp on 860601-30 ML20207E1081986-12-22022 December 1986 Notice of Deviation from Insp on 860401-0531 ML20215J8321986-10-17017 October 1986 Notice of Deviation from Insp on 860201-0331 ML20212P7611986-08-29029 August 1986 Notice of Deviation from Insp on 851101-860131 ML20198E8501986-05-12012 May 1986 Notice of Deviation from Insp During Dec 1985 ML20197E5501986-05-0707 May 1986 Notice of Deviation from Insp on 860201-0331 ML20199K9721986-04-0404 April 1986 Notice of Deviation from Insp on 851101-30 ML20141P0541986-03-0606 March 1986 Notice of Deviation from Insp on 851001-31 ML20133M7301985-10-11011 October 1985 Notice of Deviation from Insp on 850801-31 1989-09-26
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000445/19990151999-10-20020 October 1999 Insp Repts 50-445/99-15 & 50-446/99-15 on 990822-1002. Non-cited Violations.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000445/19990141999-09-14014 September 1999 Insp Repts 50-445/99-14 & 50-446/99-14 on 990707-0821.Four Violations Occurred & Being Treated as Ncvs.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000445/19990131999-08-18018 August 1999 Insp Repts 50-445/99-13 & 50-446/99-13 on 990720-23.No Violations Noted.Major Areas Inspected:Licensee Performance & Capabilities During full-scale,biennial Exercise of Emergency Plan & Implementing Procedures IR 05000445/19990101999-08-12012 August 1999 Insp Repts 50-445/99-10 & 50-446/99-10 on 990510-0628. Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Engineering & Plant Support IR 05000445/19990121999-07-29029 July 1999 Insp Repts 50-445/99-12 & 50-446/99-12 on 990530-0710.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000445/19993011999-07-16016 July 1999 Exam Repts 50-445/99-301 & 50-446/99-301 on 990618-24.Exam Results:Six Applicants for Senior Operator Licenses Passed Exams IR 05000445/19990111999-06-22022 June 1999 Insp Repts 50-445/99-11 & 50-446/99-11 on 990418-0529.No Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000445/19990081999-06-0909 June 1999 Insp Repts 50-445/99-08 & 50-446/99-08 on 990503-11.Noncited Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000445/19990091999-05-12012 May 1999 Insp Repts 50-445/99-09 & 50-446/99-09 on 990419-23.No Violations Noted.Major Areas Inspected:Reviewed Implementation of Liquid & Gaseous Radioactive Waste Effluent Mgt Program IR 05000445/19990071999-05-11011 May 1999 Insp Repts 50-445/99-07 & 50-446/99-07 on 990307-0417.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000445/19990061999-04-30030 April 1999 Insp Repts 50-445/99-06 & 50-446/99-06 on 990329-0402.No Violations Noted.Major Areas Inspected:Planning & Preparation,External Exposure Controls & Quality Assurance of Radiation Protection Activities IR 05000445/19990031999-04-0707 April 1999 Insp Repts 50-445/99-03 & 50-446/99-03 on 990124-0306.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000445/19990051999-03-19019 March 1999 Insp Repts 50-445/99-05 & 50-446/99-05 on 990222-26.One Violation Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radioactive Matls Transportation Programs IR 05000445/19990011999-03-0909 March 1999 Insp Repts 50-445/99-01 & 50-446/99-01 on 990208-12.No Violations Noted.Major Areas Inspected:Licensed Operator Requalification Program IR 05000445/19990021999-01-10010 January 1999 Insp Repts 50-445/99-02 & 50-446/99-02 on 990119-22.No Violations Noted.Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000445/19980081998-12-30030 December 1998 Insp Repts 50-445/98-08 & 50-446/98-08 on 981025-1205.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support Re Licensee Emergency Response Organization IR 05000445/19980151998-11-19019 November 1998 Insp Repts 50-445/98-15 & 50-446/98-15 on 981102-06.No Violations Noted.Major Areas Inspected:Radiation Program Activities,Including External & Internal Exposure Controls & Controls of Radioactive Matl & Contamination IR 05000445/19980071998-11-19019 November 1998 Insp Repts 50-445/98-07 & 50-446/98-07 on 980913-1024.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000445/19980161998-10-29029 October 1998 Insp Repts 50-445/98-16 & 50-446/98-16 on 981019-23.No Violations Noted.Major Areas Inspected:Testing & Maint, Protected Area Barrier & Detection Aids,Vital Area Barriers & Detection Aids & Security Sys Power Supply IR 05000445/19980141998-10-21021 October 1998 Insp Repts 50-445/98-14 & 50-446/98-14 Has Been Canceled.No Insp Rept Will Be Issued IR 05000445/19980061998-09-30030 September 1998 Insp Repts 50-445/98-06 & 50-446/98-06 on 980802-0912.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000445/19980121998-09-16016 September 1998 Insp Repts 50-445/98-12 & 50-446/98-12 Cancelled IR 05000445/19980051998-08-20020 August 1998 Insp Repts 50-445/98-05 & 50-446/98-05 on 980621-0801.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000445/19980041998-07-16016 July 1998 Insp Repts 50-445/98-04 & 50-446/98-04 on 980510-0620.No Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support IR 05000445/19983011998-07-10010 July 1998 Insp Repts 50-445/98-301 & 50-446/98-301 on 980619-26.No Violations Noted.Major Areas Inspected:Operations.All 9 License Applicants Passed Exam ML20236G9321998-07-0202 July 1998 Notice of Violation from Insp on 980329-0509.Violation Noted:Four Examples Were Identified,Where Licensee Failed to Meet Requirement for Design of ECCS Switchover from Refueling Water Storage Tank to Containment Recirculation IR 05000445/19980031998-07-0202 July 1998 Insp Repts 50-445/98-03 & 50-446/98-03 on 980329-0509. Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support IR 05000445/19980131998-06-26026 June 1998 Insp Repts 50-445/98-13 & 50-446/98-13 on 980615-19.No Violations Noted.Major Areas Inspected:Licensee Physical Security Program IR 05000445/19980021998-04-24024 April 1998 Insp Repts 50-445/98-02 & 50-446/98-02 on 980215-0328. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20217F6051998-04-24024 April 1998 Notice of Violation from Insp on 980215-0328.Violations Noted:Corrective Actions Were Not Sufficient to Identify That Excessive Leakage in ECC Sys Check Valves During Unit 1 Cycle 6 Required Unit 1 Safety Injection Pumps Be Started ML20216H3501998-04-16016 April 1998 Insp Repts 50-445/98-11 & 50-446/98-11 on 980323-27.No Violations Noted.Major Areas Inspected:Physical Security Program IR 05000445/19980011998-03-19019 March 1998 Insp Repts 50-445/98-01 & 50-446/98-02 on 980104-0214. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20248L8831998-03-19019 March 1998 Notice of Violation from Insp on 980104-0214.Violation Noted:Licensee Failed to Document Heat Related Degredation of Unit 2,Train B Solid State Safeguards Sequencer IR 05000445/19970211998-02-11011 February 1998 Errata to Insp Repts 50-445/97-21 & 50-446/97-21,correcting Errors in Insp follow-up Sys Number Associated W/Items Described in Rept IR 05000445/19970231998-01-30030 January 1998 Insp Repts 50-445/97-23 & 50-446/97-23 on 971123-980103.No Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support IR 07100012/20110221998-01-16016 January 1998 Notice of Violation from Insp on 971012-1122.Violation Noted:Procedure IPO-005B,rev 2,not Appropriate to Circumstances in That Procedure Did Not Require Pressure Be Maintained Below Rc System Pressure & Temp Limits ML20198S1891998-01-16016 January 1998 Insp Repts 50-445/97-20 & 50-446/97-20 on 971012-1122. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20198R6571998-01-16016 January 1998 Notice of Violation from Insp on 970922-25.Violation Noted: on 961029,licensee Made Changes to Emergency Plan,W/O Commission Approval,That Decreased Effectiveness of Plan & Did Not Continue to Meet Planning Standard 50.47(b)(2) ML20198N2071998-01-14014 January 1998 Notice of Violation from Insp on 970608-0719 & Subsequent Inoffice Reviews Concluded on 971114.Violation Noted: Procedures OPT-102A & 102B Did Not Include Appropriate Quantitative Acceptance Criteria ML20199H0131997-11-21021 November 1997 Notice of Violation from Insp on 970831-1011.Violation Noted:Thermometer IC1473,was Used During Performance of Procedure PPT-SX-7505A on 970807 ML20199H0241997-11-21021 November 1997 Insp Repts 50-445/97-18 & 50-446/97-18 on 970831-1011. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering PNO-IV-97-067, on 971117,medical Emergency Declared in Unit 1 Electrical Switchgear Room.Licensee Issued Stop Work Order for Electrical Maint While Investigation Conducted.Nrc Resident Insp Staff Will Be Following Licensee1997-11-17017 November 1997 PNO-IV-97-067:on 971117,medical Emergency Declared in Unit 1 Electrical Switchgear Room.Licensee Issued Stop Work Order for Electrical Maint While Investigation Conducted.Nrc Resident Insp Staff Will Be Following Licensee PNO-IV-97-066, on 971115,new Fuel Damage Occurred.Licensee Suspended Fuel on-load & Conducting Investigation Into Why Damage Occurred.Licensee Expects Delivery of Replacement Fuel Assembly on 971123.State of Tx Informed1997-11-17017 November 1997 PNO-IV-97-066:on 971115,new Fuel Damage Occurred.Licensee Suspended Fuel on-load & Conducting Investigation Into Why Damage Occurred.Licensee Expects Delivery of Replacement Fuel Assembly on 971123.State of Tx Informed IR 05000445/19970221997-11-17017 November 1997 Insp Repts 50-445/97-22 & 50-446/97-22 on 971103-07.No Violations Noted.Major Areas Inspected:Maint ML20199E6481997-11-13013 November 1997 Insp Repts 50-445/97-21 & 50-446/97-21 on 971027-31.No Violations Noted.Major Areas Inspected:Licensee Physical Security Program Including Records & Repts,Test & Maint and Access control-vehicle PNO-IV-97-061, on 971027,Unit 1 Experienced Main Generator Lockout,Turbine Trip & Reactor Trip from 100% Power.Afw Manually Started Shortly Following Trip,In Anticipation of Automatic Initiation of AFW Sys.State of Tx Informed1997-10-30030 October 1997 PNO-IV-97-061:on 971027,Unit 1 Experienced Main Generator Lockout,Turbine Trip & Reactor Trip from 100% Power.Afw Manually Started Shortly Following Trip,In Anticipation of Automatic Initiation of AFW Sys.State of Tx Informed IR 05000445/19970191997-10-10010 October 1997 Insp Repts 50-445/97-19 & 50-446/97-19 on 970922-25. Violations Noted.Major Areas Inspected:Rev 25 to Comanche Peak Steam Electric Emergency Plan ML20211A1051997-09-19019 September 1997 Insp Repts 50-445/97-17 & 50-446/97-17 on 970720-0830. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20211A0691997-09-19019 September 1997 Notice of Violation from Insp on 970720-0830.Violation Noted:On 970507,while Performing Procedure OPT-457B,licensed Operator Failed to Close Valve 2-8812A Per Step 8.8 ML20198G1821997-09-12012 September 1997 Notice of Violation from Investigation on 970606.Violation Noted:Mn Shook Submitted Falsified Info to NRC Re Being Denied Access to Nuclear Power Plant as Result of fitness-for-duty Policy 1999-09-14
[Table view] |
Text
m s
APPEND Q B NOTICE OF DEVIATION TU Electric Dockets: 50-445/87-35 50-446/87-26 Comanche Peak Steam Electric Station, Permits: CPPR-126
?] nits 1 and 2, Glelt Rose, Texas CPPR-12'i The following deviraions were identified during inspections conducted on December 2, 1987, through January 5, 1988.
A. Appendix A to Project Instructjon (PI) PI-0210'053a001, Revision 6, "Checking Procedures," states, in part, "Tne ,
purpose of an engineering check is to provide assurance that a '
tasx is performed and documented thoroughly and that the ,
results are correct and reasonable . . . .
Further, Section F of this appendix to the PI, states, in part, "Once an item has beca checked and approved, it should 1 not be altered without issuing a revision of the item.".
- Cont'eary to the above,
- 1. In the calculati_n package for the Level 5 support evaluation A02454, on pages 15 end 16 of 39, the person checking the calculations dated them March 10, 1987, prior to the date of the calculations (March 11, 1987).
The support load calculations in this package were
' performed on March 20, 1987, aCd checked on March 23, l 1987. The summary Of loads on page 19 or 39 was dated March 9, 1987, and checked on March 10, 1987, which is 1 before the date indicating when the calculations were :
performed.
l
- 2. Cn page la of 63, of Calculation A-02151 for Room 148B,
- entitled "Open Items", the checker indicated that his work was completed on January 6, 1987; however, the preparer signed and dated this document on January 7, 1987.
I These two examples comprise a deviation (445/8735-D-01).
D, Section 4.1, "Walkdown Guidelines," to Project Instruction PI 0210-052-004 provides checklists for documentation, tolerances for dimensions, and guidelines for performing the' i conduit routing valkdowns. The instruction requires an.,
l 88022301e3 ApocK 880212 05000445 l PDR '
,,0 DCD v,
e -
y 4 e
g-. . _ . , .y . ._ -, .. . , . .. _ -. . . _
. g. . , j ;.
^
pl >
- 2! .
..g**'
em' h' . 4 s ,
as-built sketch be drawn, lengths ~and sites _of structural i members be identijled, and' supports be identified, j i i contrary to the,above, i 1 1. In Roog 76, RFI-35-1-0118, Appendix'ATto cal'eulation, ,
A-00628,.page 4'ofE4 of this areendix lLs the.as-built
- drawing which forms the banis ' t this calculation. on: ,
this drawing, the.engincur Vho ptrformed the walkdown v
. reported that the Unistrut:bclte being used to secure the
! junction box to the Unistrut araber were 3/8" in i I diameter ; however, the NRC inspector found 'these bolts to
- be 1/2' in diameter, Also, on dm came drawing, the . '
walkdown enginoer_-reported that the HKB cn the. north side ,
of the junction box was located 171/ 2" away from the !
junction box. The NRC inspecter measured this distance. t to be 1 1/8".
.I i 2. In Room 148E on the isometric drawn tG depict the conduit [
runs being evaluated as part of calculation A-02151,-and j
- chown on page 24 of 43 of this calculation, the=
i dimensional data and orientation for conduits C-1PA-CR2'
'j "
d and C-lFD-A180, south of the Type 6 support tagged >
NQ-19688/A-02156 hava been reversed, thedefore,'the isometrics for both conduit rets are incorrectly .
}
j depicted. The dimension north of the Type.6 support ';
tagged NQ-06005/A-02157 to the change in elevation.is not i shown on the isometric for'the Conduit Run C-1PA-A265. ,
l
- 3. In Room 148E, the dittance from the Type 6 support tagged .
NQ-06004/A-02168 to the rise in elevation of the condui?. !
to the bolted junction box tagged NQ-08650 snus documented
~
by the walkdown engineer to be 22". The NRC inspector l measured this length to be 13".
J ]
- 4. In Room 148B, the overall lergth of the P1001 Unistrut l i member of the Type 7 support tagged NQ-06002/A-02160, :
L shown on page 26 of 43 for calculation A-02151 was
, documented by the walkdown engineer to be 10". This ;
1 length was measured to be 8" by the NRC inspector. ;
These four examples ccmprise a deviation (445/8735-D-03). !
Please provide to the U. S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555, with a copy to the !
) Assistant Director for Inspection Programs, Comanche Peak Project !
j Division, Office of Special Projects, in writing within 30 days of :
- the date of this Notice, the reason for the deviation, the l corrective steps which have been taken and the results achieved, l ~
1 !
1 ,
7 .Q. '. . . . ,. ., 6'.,,-,.-.--.<, r +4 -
1., [ -- - --+v-=* v - *SI - * '*8 ** ***+'**~~**~"i*~+F
. to
. 3 the. corrective stcps which will be taken to avoid further deviations, and the date when your corrective action will be -
completed. Where good cause is shown, consideration will be given to extending the response time. -
FOR THE NUCLEAR REGULATORY COMMISSION 0 5 !O O Dated this_12th day of February 1988 1
at Comanche Peak Site 2-I i
I i
- i a
e 5 4 f +
e l
t p
)
1 3
1 i
-