ML20148T322

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Part 21 Rept Re Stress Corrosion Cracking in Reactor Coolant Pump Oiler Tubing,Initially Reported 801202.Evaluation of Westinghouse Quotation Re Replacement of Pump Lubrication Oil Cooler w/90-10 copper-nickel in Progress
ML20148T322
Person / Time
Site: Sequoyah 
Issue date: 02/04/1981
From: Mills L
TENNESSEE VALLEY AUTHORITY
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
REF-PT21-81-360-000 10CFR-050.55E, 10CFR-50.55E, PT21-81-360, PT21-81-360-000, SQRD-50-328-81, NUDOCS 8102250541
Download: ML20148T322 (1)


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TENNESSEE VALLEY AUTHORITY CH ATTANOOG A, TENNESSEE 374ot l

400 Chest a t Street Tower II i

1 February 4, 1981 1

1 SQRD-50-328/81-11 i

Mr. Ja2nes P. O' eilly, Director i

Office of Inspection and Enforcement U.S. Nuclear Regulalory Co==ission Region II - Suite 3100

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s 101 Marietta Street Atlanta, Georgia 30303

Dear Mr. O'Reilly:

i SEQUDYAE NUCLEAR PLAhT UNIT 2 - STPESS CORF.0SION CFACl2NG IN TUBING ON THE REACTOR C30LAhT FUMP OIL COOLERS - SOF.D-50-328/81 SECOND INTERIM REPORT The s':bject deficiency was initially reported to NRC-0IE Inspector i

R. W. Wright en December 2, 1980, 'in accordar.ce with 10 CFR 50.55(e) as NCR SQN EE 8025. An interic report ns sub=.itted on January 2, 1981.

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We expect to subtit our next report by March 27, 1961.

We consider 10 CFR g applicable to this deficiency.

TVA has received and is evaluating the quotatics frc: Wes:inrf.ouse for replacing the unit 2 reactor coolant pump lubrication oil a aler tubing with 90-10 copper-nickel.

TVA is also investigating the idem of plugging the oil cooler tubes which leal:.

This would be acceptable in view of the fact that hydra::ine, which as used as the ec:penent cooling system water treatment, has been ree ved fro: the sysne:.

A=:enia, which resulted frc:

the deco positien of hydrazine, in conjuncticn with residual P.nd operating i

stresses, caused the stress corrosion crack:ing.

If you have any questions concerning this catter, please Eet in t.uch with D. L. Lt.=bert at FTS 857-2561.

Very truly yours, TENESSEE VALLEY AUTHORITY L. M. Mills, Manager Nuclear F.egulation and Safety Mr. Victor Stello, Jr., Director /

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Office of Inspection and Enforcement U.S. Nuclear Regulatory Co==ission Washington, DC 20555

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