ML20148H108
| ML20148H108 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 01/21/1988 |
| From: | Kemper J PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | Russell W NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| Shared Package | |
| ML20148H115 | List: |
| References | |
| IEB-85-003, IEB-85-3, NUDOCS 8801270129 | |
| Download: ML20148H108 (3) | |
Text
PHILADELPHIA ELECTRIC COMPANY 2301 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 (215)841 4500 JOHN S. KEMPER CE NIO R VICE+PR ESIDENT = NUCl.E A R Mr. William T. Russell, Administrator Docket Nos.:
50-277 Region I 50-278 U. S. Nuclear Regulatory Ccmnission ATTN: Doctment Control Desk January 21, 1988 Washington, DC 20555
Subject:
Peach Bottom Atomic Power Station Units 2 S 3 L
I.E.Bulletin 85-03, "Motor Operated Valve Ccmnon Mode Failure During Plant Transler,ts Due to Improper Switch Settings" 5
Reference:
J. S. Kemper (PECo) letter to T. E. Murley (USNRC),
dated Novst>er 3,1986
Dear Mr. Russell:
r The purpose of this letter on the subject 1.E.Bulletin 85-03 program at our Peach Bottom Station is two-fold.
First, submitted herewith is our report which partially satisfies the bullettn's reporting requirements and describes our Peach Bottcm IEB 85-03 Program and plans for future work.
Secondly, it discusses the schedule aspects of the progran with respect to our plans to restart Peach Bottcm Units 2 & 3.
The referenced letter provided our Initial response to the subject bulletin.
The attached report provides a conplete response to I.E.Bulletin 85-03 action items a), b) & d) and a partial response to action item c) as related to Unit 2 specific test results.
All general and unit specific program elements identified in the attached report, with the exception of the Unit 2 differential pressure testing, will be ccxmleted prior to the restart of each unit. The Unit 2 final I.E.Bulletin 85-03 response, containing the differential pressure testing results, will be submitted within three (3) nonths after testing conpletion folicwing Unit 2 restart. This is necessary since nest planned differential pressure testing requires the use of nuclear steam. Because the planned Unit 3 program does not incitxfe any differential pressure testing, its final response will be submitted before restart,
\\
8801270129 880121
\\
DR ADOCK 050 7
If you have any questions or require any additional Infonnation regarding our I. E.Bulletin 85-03 program, please do not hesitate to contact us.
Sincerely, d'$./Y~[
TSN/pd12148708 Enclosure Report Copy to:
T. P. Johnson, Resident Site Inspector USNRC, Docunent Control Desk Washington, DC 20555
.~ -. - - _ -
,.I m;.
L i
n 1
C050NWEALTH OF PEbNSYLVANIA I ss.
COUNTY OF PHILADELPHIA'
~ '
i
.J.' S. ' Kenper, being first duly sworn, deposes and says:
That helIs-Senior Vice President of' Philadelphia Electric -
-Conpany; that he has read the foregoing response to NRC I.E. Bulletin-
. 85-03 and knows the contents thereof; and that the ' statements and matters set forth therein are true and correct to the best of his-i knowledge, Information and belief.
~
4
-$?,bf$ h ----
'ntor Vice President Subscribed and sworn to Before me this 2 / _ofday of January, 1988
.L &
2* MA Notary Pubile idELANIE R. CAMPANELLX-Notary Pubuc, Philadehhia, Philadelphis Co.
My Commission Expires february 12.1990 TSN/aud/12318706
.n e.
y
,-w,,.,ve,,...wim.w-.-.-
,. ~,,.- -,
r y.<
.,i.<-
,