05000318/LER-1979-049-03, /03L-0:on 791221,during Steady State Operation, Channel B Thermocouple Taken Out of Svc Due to Erratic Indication.Caused by Broken Lead on Current Loop Resistor, Vishay Model S-106C.All Loop Connections Checked Quarterly

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/03L-0:on 791221,during Steady State Operation, Channel B Thermocouple Taken Out of Svc Due to Erratic Indication.Caused by Broken Lead on Current Loop Resistor, Vishay Model S-106C.All Loop Connections Checked Quarterly
ML20148B976
Person / Time
Site: Calvert Cliffs 
Issue date: 01/21/1980
From: Lagiewski J, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20148B975 List:
References
LER-79-049-03L-01, LER-79-49-3L-1, NUDOCS 8001240425
Download: ML20148B976 (2)


LER-1979-049, /03L-0:on 791221,during Steady State Operation, Channel B Thermocouple Taken Out of Svc Due to Erratic Indication.Caused by Broken Lead on Current Loop Resistor, Vishay Model S-106C.All Loop Connections Checked Quarterly
Event date:
Report date:
3181979049R03 - NRC Website

text

v.nu LICENSEE EVENT REPORT l

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61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10 l a i l During steady state operation at 0920, channel B Tc was taken out of I

io i31 I service due to erratic indication. Channel B high power, thermal margin /

1 to ta i l low pressure, and axial flux offset trip units were bypassed per the I

l o I s l I reouirements of T.S. 3.3.1.1.

Channel B hiah power, thermal margin / low.

I io is i i pressure, and axial flux offset trip units were returned to service at 1020 on I

l o l 71 l 12/21/79. Three redundant RPS channels remained operable throughout this 1

Ioi8l l event. LER 77-39 (U-2) describes a sim_ilar event.

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CODE TYPE NO.

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44 47 CAUsE DESCRIPTION AND CORRECTIVE ACTIONS h li lo l l The cause of erratic indication was a broken lead on a current loop resistor, I

li li l I (Vishav Model #S-106C) which develoos a signal voltage for one Tc innut tn I

ii l2j I the Reactor Protective System. All 1000 connections. including this resis tnr.

I l i 131 l are checked cuarterlv undor tho ovis ting Provantivo Wintenanco Drngram.

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79-49/3L DOCKET NO.

50-318 EVENT DATE 12/21/79 REPORT DATE 01/21/80 ATTACHMENT CAUSE DESCRIPTION AND CORRECTIVE ACTIONS:

(CONTINUED)

Since implementing this check, the occurrence rate for resistor failures in service has been greatly reduced. No further preventive action is being considered at this time.

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