05000366/LER-1978-046-03, /03L-0:on 780926,rated Flow W/Two Pumps Running in Loop 1 Could Not Be Achieved for Either Loop of RHR Svc Water Pump.Caused by Damaged Cavitrol V Trims & 10 Inch Fisher Valves

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/03L-0:on 780926,rated Flow W/Two Pumps Running in Loop 1 Could Not Be Achieved for Either Loop of RHR Svc Water Pump.Caused by Damaged Cavitrol V Trims & 10 Inch Fisher Valves
ML20147E793
Person / Time
Site: Hatch 
Issue date: 10/09/1978
From: Thomas Greene
GEORGIA POWER CO.
To:
Shared Package
ML20147E771 List:
References
LER-78-046-03L, LER-78-46-3L, NUDOCS 7810180024
Download: ML20147E793 (2)


LER-1978-046, /03L-0:on 780926,rated Flow W/Two Pumps Running in Loop 1 Could Not Be Achieved for Either Loop of RHR Svc Water Pump.Caused by Damaged Cavitrol V Trims & 10 Inch Fisher Valves
Event date:
Report date:
3661978046R03 - NRC Website

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Page Two Georgia Peacr Conpany E.1. llatch tluclear Plant Llaxley, Georgia 31513 Reportable Occurrence ?!o. 50-366/1978-46completion of this inr.tallat ion by 10/10/78.

This is a temporary fix until new trinG can be procured.

We expect the new trims to be installed by 11/10/78.

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