|
---|
Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20235S2441989-02-16016 February 1989 Suppl to 880104 Special Rept Re Inoperability of High Pressure Svc Water Diesel 1B.Fuel Supplu Sys Was Source of Problem.Fuel Supply Sys Will Be Replaced W/Above Ground Tanks for Both Diesels ML20237C6781987-11-30030 November 1987 Special Rept:On 871118,internal Portion of Fire Suppression Water Sys Removed from Svc to Replace Section of Piping.On 871120,piping Successfully Hydrostatically Tested & Fire Suppression Sys Returned to Svc ML20236W2731987-11-23023 November 1987 Special Rept:On 871028,following Initiation of 24 H Run for 18-month Diesel Generator Test,Emergency Diesel Generator 1B Stopped Running.No Cause for Trip Determined.Procedure Will Be Revised So Alarm Conditions Tested Before Run ML20236X0081987-11-18018 November 1987 Special Rept Re Inoperability of Fire Suppression Water Sys. Internal Portion of Sys Removed from Svc on 871118 to Replace Section of Piping.Initially Reported on 871118.Plant Permanently Shut Down & Reactor Defueled ML20236Y2151987-05-15015 May 1987 Special Rept 87-02:on 870216,reactor Manually Scrammed Due to Erroneous Indication of Low Voltage on Turbine Bldg MCC1A.On 870406,reactor Power Dropped Following Trip of 1A Forced Circulation Pump ML20211E4971986-06-0404 June 1986 Special Rept 86-02:on 860307 & 0525,thermal Power Changed by Greater than 15% of Rated Thermal Power within 1 H on Three Occasions.Caused by Bus 1B Power Loss,Reactor Forced Circulation Pump Trip & Control Air Sys ML20138B7861986-03-11011 March 1986 Special Rept:On 860311,internal Portion of High Pressure Svc Water Sys Which Supplies Fire Suppression Sys Removed from Svc to Replace Valve Required to Be Tested by Inservice Testing Program ML20141P1241986-03-0606 March 1986 Incident Rept DPC-86-1:on 860104,seal Inject Supply Line Separated at Swagelock Fitting,Spraying Water & Resulting in Reactor Shutdown.Cause Unknown.Mechanical Seal on CRD 2 Reworked ML20138L8431985-10-21021 October 1985 Special Rept 85-02:on 850725,0909 & 14,reactor Thermal Power Changed by More than 15% of Rated Thermal Power within 1 H. Power History,Fuel Burnup,Cleanup Flow History,Offgas Activity Levels & Gross Alpha Activity Levels Discussed ML20138L7451985-10-0808 October 1985 Special Rept:Discusses Circumstances Which Led to Inaccuracies in Personnel Cumulative Lifetime Dose Records. Cumulative Permanent Doses in Radiation Dosimetry Rept Do Not Agree W/Records Maintained in Computer File ML20128N9141985-07-18018 July 1985 Special Rept 85-01:providing Results of Sampling & Analysis Actions & Addl Operational Info for Six Occasions When Reactor Thermal Power Changed by More than 15% of Rated Thermal Power within 1 H ML20062D1601982-07-26026 July 1982 Ro:On 820726,internal Portion of Fire Suppression Water Sys Removed from Svc in Order to Replace Fire Hose Cabinets Rendering Fire Suppression Water Sys Inoperable.Backup Capability Provided ML20054F1711982-06-0707 June 1982 RO 82-14:on 820605,w/reactor in Operating Condition 2 at 50 X 10-6% Power,Review of Shift Supervisor Log Revealed Primary Water Alpha Activity of 7.46 X 10-6 Uci/Gm.Reactor Shutdown Conducted 820605 in Accordance W/Tech Spec 1989-02-16
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20210A6361999-04-30030 April 1999 Rev 13 to Quality Assurance Program Description ML20206J3751999-04-29029 April 1999 Rev 13 to QA Program Description ML20207A9591999-01-31031 January 1999 Revised LACBWR Decommissioning Plan ML20196G0751998-12-31031 December 1998 1998 Annual Rept for Dairyland Power Cooperative ML20204D8371998-12-31031 December 1998 Annual Rept for 1998 - Rept of Changes,Tests & Experiments for Lacbwr. with ML20237E2701998-07-31031 July 1998 Rev 12 to QA Program Description ML20196A9241998-07-31031 July 1998 Rev 12 to LACBWR QA Program Description (Qapd) ML20202J0691998-01-31031 January 1998 Revised LACBWR Decommissioning Plan ML20202J0781998-01-31031 January 1998 Revised LACBWR Initial Site Characterization Survey for Safstor ML20203K0041997-12-31031 December 1997 Annual Operating Rept for 1997 - Rept of Changes,Tests & Experiments ML20249B7101997-12-31031 December 1997 Navigating for Our Future Dairyland Power 1997 Annual Rept. W/O Ltr ML20138B7771997-04-25025 April 1997 Corrected Page 8 of SE for Amend 69 to La Crosse Boiling Water Reactor License ML20137R7731997-04-11011 April 1997 Safety Evaluation Approving Changes to QAP Description ML20149K2071996-12-31031 December 1996 Conquering New Frontiers,Dairyland Power Cooperative 1996 Annual Rept ML20135C3901996-12-31031 December 1996 Annual Rept for 1996 - Rept of Changes,Tests & Experiments ML20132F8721996-10-31031 October 1996 Revised LACBWR Decommissioning Plan ML20134M2531996-02-20020 February 1996 Revised Rev 11 to QA Program Description ML18012A9001995-12-31031 December 1995 Annual Rept - 1995 of Changes,Tests & Experiments. W/ 960220 Ltr ML18011B1461995-04-20020 April 1995 LER 95-001-00:on 950417,noted That HPSW to Containment Building Isolated.Caused by Momentary LOP Due to Operational Test of 1A Edg.Procedures for Test Being Modified to Include Instructions to Verify Value Being open.W/950420 Ltr ML20056E2631993-08-10010 August 1993 LACBWR Containment Bldg Structural Analysis. W/One Oversize Drawing ML20056E2621993-07-31031 July 1993 Nonproprietary Analysis of Potential Blast Effects on LACBWR Reactor Bldg Due to 16 Inch Natural Gas Pipeline Failure,Suppl Analysis for Fast Closing Valve ML20127D3901993-01-13013 January 1993 SE Supporting Amend 67 to License DPR-45 ML20128K6011992-12-31031 December 1992 Corrected App a Re Std Format for Reporting Number of Personnel & man-rem by Work & Job Function,To Annual Rept for 1992 - Rept of Changes,Tests & Experiments ML20128D3421992-12-31031 December 1992 LACBWR Annual Rept 1992 ML20062B4761990-09-30030 September 1990 Monthly Operating Rept for Sept 1990 for LACBWR ML20248D0941989-08-31031 August 1989 Monthly Operating Rept for Aug 1989 for LACBWR ML20245G6571989-07-31031 July 1989 Monthly Operating Rept for Jul 1989 for LACBWR ML20245F9681989-06-30030 June 1989 Monthly Operating Rept for June 1989 for LACBWR ML20245J7351989-04-26026 April 1989 Safety Evaluation Supporting Amend 65 to License DPR-45 ML20245F8241989-02-28028 February 1989 Monthly Operating Rept for Feb 1989 for La Crosse Bwr.W/ ML20235S2441989-02-16016 February 1989 Suppl to 880104 Special Rept Re Inoperability of High Pressure Svc Water Diesel 1B.Fuel Supplu Sys Was Source of Problem.Fuel Supply Sys Will Be Replaced W/Above Ground Tanks for Both Diesels ML20245F7771989-01-31031 January 1989 Monthly Operating Rept for Jan 1989 for LACBWR ML20246H8771988-12-31031 December 1988 1988 Dairyland Power Cooperative Annual Rept ML20205T1271988-10-31031 October 1988 Monthly Operating Rept for Oct 1988 for La Crosse Bwr.W/ ML20151T0991988-08-0808 August 1988 Safety Evaluation Supporting Approval of Util Rev 10 to Emergency Plan ML20150D7051988-07-0808 July 1988 Safety Evaluation Supporting Rev 10 to Emergency Plan ML20155F9161988-05-31031 May 1988 Safety Evaluation Supporting Amend 62 to License DPR-45 ML20151G0591988-04-11011 April 1988 Safety Evaluation Supporting Amend 60 to Provisional License DPR-45 ML20148C3941988-03-15015 March 1988 Safety Evaluation Supporting Amend 59 to License DPR-45 ML20149G0711988-01-0404 January 1988 Safety Evaluation Supporting Amend 58 to License DPR-45 ML20147A9731987-12-31031 December 1987 Decommissioning Plan ML20149J3441987-12-31031 December 1987 LACBWR Annual Rept 1987 ML20195D7811987-12-31031 December 1987 1987 Dairyland Power Cooperative Annual Rept ML20237C6781987-11-30030 November 1987 Special Rept:On 871118,internal Portion of Fire Suppression Water Sys Removed from Svc to Replace Section of Piping.On 871120,piping Successfully Hydrostatically Tested & Fire Suppression Sys Returned to Svc ML20236W2731987-11-23023 November 1987 Special Rept:On 871028,following Initiation of 24 H Run for 18-month Diesel Generator Test,Emergency Diesel Generator 1B Stopped Running.No Cause for Trip Determined.Procedure Will Be Revised So Alarm Conditions Tested Before Run ML20236X0081987-11-18018 November 1987 Special Rept Re Inoperability of Fire Suppression Water Sys. Internal Portion of Sys Removed from Svc on 871118 to Replace Section of Piping.Initially Reported on 871118.Plant Permanently Shut Down & Reactor Defueled ML20234C3931987-10-20020 October 1987 Rev 5 to QA Program Description ML20151B2351987-10-20020 October 1987 Revised Rev 5 to QA Program Description ML20235R0531987-09-30030 September 1987 Determination of Potential Radiological Consequences to Members of Public from Fuel Handling Accident at La Crosse Nuclear Facility ML20235B5711987-09-15015 September 1987 Safety Evaluation Supporting Amend 57 to License DPR-45 1999-04-30
[Table view] |
Text
.
's D DA/RYLAND h k COOPERAT/VE LA CROSSE BOILING WATER REACTOR (LACBWR)
- P.O. BOX 275 GENOA, WISCONSIN 54632 + (608) 689-2331 March 6,1986 In reply, please refer to LAC 11452 DOCKET NO. 50-409 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555
Subject:
DAIRYLAND POWER COOPERATIVE LA CROSSE BOILING WATER REACTOR (LACBWR)
PROVISIONAL OPERATING LICENSE NO. DPR-45 INFORMATIONAL INTERNAL INCIDENT REPORT l
Gentlemen:
Enclosed is an information copy of LACBWR Internal Incident Report No. 86-1. The circumstances of the incident do not meet the criteria for a Licensee Event. The Resident Inspector, however, requested that we submit a copy of our Internal Incident Report for information only. Therefore, this report is being submitted. It is not a Licensee Event Report.
- If there are any questions, please contact us.
Sincerely, DAIRYLAND POWER COOPERATIVE
///VS
/
8o03190035 DR 860306 .
James W. Tayh r' ADDCK 05000409 General Manager PDR i
JWT/LSG/ lam
! Attachment cc: J. G. Keppler, NRC Reg. III NRC Resident Inspector b l N j J. Stung pc2-6.7
\
DA!RYLAND POWER COOPEPATIVE CORPORATE HEADOUARTERS.P O BOX 817 LA CROSSE WISCONSIN 54601 *(608J 788 4000
LACBWR INCIDENT REPORT 1.0 Report No. DPC-86-1 2.0 Date and Time of Incident 01/04/86 at 2059 3.0 Incident Subject Upper Control Rod Drive No. 2/ Seal Inject Leak Resulting in Reactor Shutdown 4.0 Component that Failed Swagelock Fitting Seal Inject Supply to #2 CRD and Upper Control Rod Drive (UCRD) #2 Mechanical Seal 5.0 Similar Occurrences None 6.0 Operating Conditions at Time of Incident Condition I Reactor Power 94% Generator Output 49 MWe other:
7.0 Description of Incident Prior shifts had experienced sharp increase in #2 CRD effluent temperature and excessive seal water leakage from its malfunction leakoff. The swing shift crew was able to reduce temperature to as low as 210o F, but leakage would not stop. Reducing temperature involved cycling seal inject (SI) supply valves, adjusting other rod temperatures, increasing SI flow to rods and tapping on SI supply line to #2 CRD which redistributed crud in the line and affected seal water flow. It was while tapping on the supply line that the line separated at a Swagelock fitting, spraying seal inject water.
8.0 Immediate Evaluation, Corrective Action and Results The Shift Supervisor called the Control Room and told them to commence reactor shutdown using all rod insert. He called the Health Physics (HP) Technician and had the technician bring a wetsuit to sub-basement. He put wetsuit on and was able to shut seal inject supply valve to #2 CRD. The leak stopped immediately. Reactor power was held at 30 percent. The auxiliary operator isolated #2 CRD j
j effluent valve. A mechanic was called in. He repaired the Swagelock fitting. No primary water leaked from the separated line. There is a check valve in each seal inject supply line.
I pc2-6.6
=_, ._ _ - - . _ . - , . ..- , - - - _ _ _ - , -
e Seal inject supply was cut back into #2 CRD slowly over a matter of hours to limit the cooldown effects on the CRD upper flange. The leakage from CRD #2 was monitored closely. No flange leak developed.
The reactor engineer was called regarding control rod programming. The rods had been inserted to approximately 40 inches (18 and 12/16 inches
- Rod 1) with the all rod insert pushbotton, except for Rod 2, which was electrically disabled. Rod 2 had been energized and driven to approximately 40 inches following the all rod insert. He recommended that power be reduced to less than 25 percent for the return to rod programming. He authorized a withdrawal rate of greater than one inch per hour per procedure. Conttol rods we re moved within procedure limitations to start re establishing rod programming. On January 5, '
the Reactor Engineer further authorized a withdrawal rate for the return to rod programming of I 8 inches /haur, as long as power remained below 25 percent.
On January 5. CRD 2's effluent temperature and leakage increased. A trough was rigged to divert some water from splashing other control rod drives. The seal wccer leak rate was approximately 1.2 gpm on the morning of January 5. It was decided to proceed with reactor shutdown.
At 1050, the shutdown commenced from 23 percent power. The plant was off the line at 1305, with all control rods in at 1309. The activity of a sample of the water leakage demonstrated that it was essentially seal inject water.
9.0 Abnormal System or Fouipment Response None Is the incident radiological in nature? YES X NO 10.0 {E] Supt. or Desig. Alternate Notified Paul C. Moon 01/04/86
_ S/S Date
[_] NRC Report Not Required
_ S/S Date
[_] Requires Ops. Engr. Determination
_ S/S Date
[X] NRC Report Not Required L.S. Goodnan 01/05/86 except for >152/ hour Operations Eng. Date spectat report
((]NRCReportRequired: 1 Hour 4 Hours 30 Days Part 21
((]l-or4-HourNotif.Made: Date Time Notification Made By
[E] Public Service Date 01/06/86 Poon Commission Report: Time 0850 Individual Contacted pc2-6.6
9 11.0 Perlmanent Corrective Action An analysis was perforised which verified that power distribution limits were not exceeded following the all rod insertion.
The mechanical seal on CRD #2 was reworked.
-i
.) ed. /$ .~
J..D./ Parkyn, LA6BWR Superintendent Reviewed by ORC 2 5 16 Date JDP:LSG: lam DISTRIBUTION: SRC ORC (Ltd.) NRC Resident Inspector INPO File R5g 1
i pc2-6.6 i '
. _ _ -