05000315/LER-1985-068, :on 851213,unexpected Stream Line Isolation Occurred.Caused by Natural Sequence During Performance of Approved Surveillance Test Procedure & Technician Failure to Warn Operators of Event

From kanterella
(Redirected from ML20141F356)
Jump to navigation Jump to search
:on 851213,unexpected Stream Line Isolation Occurred.Caused by Natural Sequence During Performance of Approved Surveillance Test Procedure & Technician Failure to Warn Operators of Event
ML20141F356
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/02/1986
From: Lauren Gibson
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20141F349 List:
References
LER-85-068, LER-85-68, NUDOCS 8601090256
Download: ML20141F356 (1)


LER-1985-068, on 851213,unexpected Stream Line Isolation Occurred.Caused by Natural Sequence During Performance of Approved Surveillance Test Procedure & Technician Failure to Warn Operators of Event
Event date:
Report date:
3151985068R00 - NRC Website

text

.

NR Form 386 U S. NCLEQQ CEGULOTOQY i.OMMISSION g

I APPROVED OMB NO.3150 0104 LICENSEE EVENT REPORT (LER)

EXPIRES 8 31 se F ACILITY NAME HD DOCKET NUMBER (28 PAGEi3.

TITLE ( Al lOFl011 D.

C. COOK PLANT) UNIT 1 015tololol,]3lq i

ESF MTUATION EVENT DATE (5) j LER NLeeSER tel

% li REPORT DATE 178 OTHER F ACILITIES INVOLVED ISI MONTH oAv vEAR

, WAR 5'gge

Qvy,y,;

uONTH oAv iEAR

  • Acitivv ~ Aves oOcnET =UusER:s>

0 15101010 1 l l 1l2 1l 3 85 d5 0 l6 l8

- 0l0 0l1 0l2 8l6 o isio p o i oi I i THIS REPORT 18 $USMITTED PURSUANT TO THE REQUIREM*NTS OF 10 CFR {- TChece one or more of ree fono*>asl IIII OPERATING MODEIM 1

20 402f th 20.4061st y

50.734e H2 H el 73.711bl R

20.40SteH1HG 50.3SieHil 60.73teH2Hel 73.71 tel HO)

(j () i ()

20 easteH1Hdi I

50.38ieH2) 50.73teH2ilwe)

HE pec en A8 20.eOSteH1Hd61 80.73deH2Hil 60.73!aH2HvedH A) 356U 20.400teH1Hiel 50.73teH2Het 60.73ieH21tvMigl 20.405EaH1Hel 60.73EeH2Hieil 60.7he t2Hal LICENGEE CONTACT FOR TH18 LER 412)

NCME TELEPFONE Nvv8ER ARE A CODE L. S. GIBSCN, TECHNICAL ENGINEERING SUPERINTENDENT 61116 4 16151-15191011 COMPLETE ONE LIP 61 FOR EACH @%ENT F AILURE DESCRIBED IN THIS REPORT 1136

CAUSE

SYSTEM COMPONENT f

yo PRO's AE ORTAOLE

CAUSE

System COvPONENT E

pp f

I I I I I I I I

I I !

I I I I

l i I I I I I

l l I I l l SUPPLEMW tL REPORT EXPECTED tien MONT **

CAv VEAR g

Sv944 SSION

~

YES UfPoe. eemoore dMPECTIO Suherission ONis NO l

l l

A T R ACT <t.m., M rom es.m.. e

,e.-,

,,ae

..,,, e.ec. -r e. i H.,

ON DECEMBER 13, 1985, WITH UNIT 1 IN MODE 3 (HOT STANDBY), A STEAMLINE ISOLATIC',i OCCURRED WHICH IS AN ACTUATION OF THE ENGINEERED SAFETY FEATURES (ESF) SYSTEM.

THE EVENT WAS THE RESULT OF A NATURAL SEQUENCE DURING THE PERFORMANCE OF AN APPRO7ED SURVEILLANCE TEST PROCEDURE.

THE PROCEDURE INCLUDED A GRECAUTION THAT A STEAM LINE ISOLATION COULD OCCUR, HOWEVER,,7THE TECHNICIAN DID NOT INFORM THL CONTROL ROOM PERSONNEL OF THIS POSSIBILITY.

CONSEQUENTLY, WHILE AN ACKNOWLEDGED RESULT OF THE EVOLUTION IN PROGRESS,THE EVENT WAS UNEXTECTED BY THE OPERATORS, MAKING IT REPORTABLE.

OPERATIONS AND TECHNICAL PbRSONNEL TOOK IMMEDIATE CORRECTIVE ACTION TO RESTORE THE UNIT TO PRE-EVENT STATUS.

THERE WERE NO ADVERSE CONSEO.UENCES FROM THE EVENT.

s AS PREVENTIVE' ACTION, THE PROCEDURE WAS CHANGED TO REQUIRE AN OPERATOR SIGN-OFF ACKNOWLEDGING AWARENESS OF THE POSSIBLE ESF ACTUATION.

\\;

t, B601090256 860102 PDR ADOCK 05000315 S

PDFi,.

4 NRC form 306 T 83++\\ g?

8