Similar Documents at Cook |
---|
Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
- _ - _ _ - _ _
. i N.R.C. OPERATING' DATA REPORT-DOCKET NO. 50-315 DATE 12/3/85 COMPLETED BY CLIMER.
TELEPHONE 616-465-5901 OPERATING STATUS
- 1. Unit Name D. C. Cook Unit 1 ---== - ------------
'2. Reporting Period NOV B5 Inotes !
- 3. Licensed Thermal-Power (MWt) 3250-l !
- 4. Name Plate Rating (Gross MWe) 1 1152 I t
- 5. Design Electrical Rating (Net NWe) 1030 t t
- 6. Maximum Dependable Capacity (GROSS MWe) 1056 I t
- 7. Maximum Dependable Capacity (Not MWe) 1020 --
- 8. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since Last Report Give Reasons __ _ - _ _ _ -----------------
- - = = ---
_=.
. - - - - - - - - - - - - - - - - - = - _ - - - - = = - - - - - - - - - - - - - - = .
- 9. Power Level To Which Restricted. If Any (Net MWe) _________________
- 10. Reasons For Restrictions. If Any:______ ____ ______ _------_
-==-=_ =------------------
u---------- ----------- - - - - - _ --- ----
This Mo. Yr. to Date Cumm.
- 11. Hours in Reporting Period 720.0 8016.0 95688.0
- 12. No. of Hrs. Reactor Was Critical 294.6 2162.6 67856.4
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 463.0
- 14. Hours Generator on Line 213.1 2069.3 66430.8
- 15. Unit Reserve Shutdown Hours 0.0 0.0 321.0
- 16. Gross Therm. Energy Gen. (MWH) 297751 5716272 193885776
- 17. Gross Elect. Energy Gen. (MWH) 86040 1847800 63619770
- 18. Net Elect. Energy Gen. (MWH) 78548 1773401 61204496
- 19. Unit Service Factor 29.6 25.8 70.8
- 20. Unit Availability Factor 29.6 25.8 70.8
- 21. Unit Capacity Factor (MDC Net) 10.7 21.7 64.0
- 22. Unit Capacity Factor (DER Net) 10.6 21.5 61.6
- 23. Unit Forced Outage Rate 3o.3 5.5 7.4
- 24. Shutdowns Scheduled over Next Six Months (Type,Date,and Duration):
- 25. Ii"5huI~Do n At 5nd'Ei RepoEt PeFI5d, 5AtINAt$d Date of StIrtup:~
~~ ~ ~ ~
UNIT SHUT DOWN FOR VALVE REPAIRS, EXPECTED STARTUP 12/13/85
- 26. Units in Test Status (Prior to Commercial Operation):
Forcast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION DR k
. \\\
.J
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO. 50-315 UNIT ONE DATE 12/3/85 COMPLETED BY CLIMER TELEPHONE 616-465-5901 MONTH NOV B5 AVERAGE DAILY AVERAGE DAILY l DAY POWER LEVEL DAY ' POWER LEVEL 1 0 17 138 2 0 18 207 3 0 19 210 l
4 0 20 204 5 0 21 391 6 0 22 427~
7 0 23 431 8 0 24 616 9 0 25 636 10 0 26 0 11 0 27 0 12 0 28 O 13 0 29 0 14 0 30 0 15 0 31 0 16 13 d
4
. e e
e IMM KET No. 50-315 llNITSilllllWIWNS ANilPOWEM ItElstR TIONS UNIT NAME D.C. Cook - Unit 1 IDA1E 12-6-85 COMPI ETEll gy B.A. Svensson Movember, 1985 Itiroit's MONiil 1El.FrlHINE 616/465-5901 .
PAGE 1 of 2
.$ E 3 'i
"# s. j i kcnsee g *,, 5"t g Cause A reuseceive H.e. Itaic k g g g livene g,o? g3 Atteam sie t- I g- )j ;{f, g Hepius
246 850406 S 382.1 B&C 2 N.A. ZZ ZZZZZZ The Unit was removed from service on Cont'd .
850406 for the scheduled Ten-Year ISI and Cycle VIII - IX Refueling /
Maintenance outage.. The outage work has been completed and initial criticality for Cycle V occurred on
. 851113. Low power physics testing was completed on 851115 and the Unit was paralleled to the System at 2206 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.39383e-4 months <br /> on 851116. The reactor power was increased to 30% for turbine warming prior to overspeed testing.
The total length of the outage was-5395.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />.
247 851117 S 3.5 B 1 N.A. ZZ ZZZZZZ At 1517 hours0.0176 days <br />0.421 hours <br />0.00251 weeks <br />5.772185e-4 months <br /> the Unit was removed ,
from service for turbine overspeed testing. The Unit was returned to service at 1850 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.03925e-4 months <br /> the same day.
The power ascension testing program i 2 3 4 1: Finced Itcasim: Meelie=I: Entwids G-Insesuctinais S: Stlecalideal A listuipmesu failme(f.aplain) 1 -Mappal fin l'sepasalkus of liasa 3 Maintenasice or Test 2 ManualSc aus. linesy Slicces few liensec C-Itefweling 3- Ausnemesic Soam. Evens Mcquweill'R1l'dcINilMIG-Ilitegulasewy Reusicske 4 Delics (Engelsin) 01(ill liOpesseew Tsaisdsiga ficcuse R mandinasbwi F-Adesiewssoasive 5 lishdo I - Same Sannic G Opesasiinial 1:esen llimplaint 08/17) II Helics (Engdaisil
. a e
INN:KEI NO. 50-315' - .
IINST SlHilllOWNS ANilrowl:H NElllfrilONS IINITNAME D.C. Cook - Unit 1 IBA1E 12-6-85 COMPI ETEll hy B.A. Svensson November, 1985 NI FOlll HinN HI 1EI.EPllONE 616/465-5901 PAGE 2 of 2 .
- jg 'k s..j i kcusce gg 5L g rauw A reusetsive N.i. Ilate b g* 4 ) 5 se liveset ET S3 Atslues I.*
9 ,2 - g Nepius
- N0 L' reevens Heemsence 247 was commenced, but was not completed Cont'd . .
due to a reactor trip.
248 851125 F 121.3 B 3 Latdr ZZ ZZZZZZ A reactor trip occurred from 78% re-actor power due to a negative rate trip. The trip resulted from one power range channel's bistable being
^
in the tripped position for surveil-lance testing and a spurious signal on a second power range channel while taking detector current read-ings for quadrant power tilt deter-mination. During a containment in-spection after the reactor trip, a-leak was discovered on No. 12 R.C.
Pump casing flange. To repair the ,
leak, the RCS had to be cooled down and' drained to half-loop. The Unit remained shut down in Mode 5 at the end of the month.
I 1 3 4 F: Feuixd lleasase: Meshimi: Emiselde G leesssucei.=is S: Sileedadeil A Fegesipussaa Fashne(Emplakel- l-Manual I.w reegiasatise nf ilata 3 Maiseleansece pai Test 2 Mamsal Scram. linesy Sects fin liensee r Refueling 3 Aessoonesic &saan . Event Nepewe ll.I'Rl File INilNI G-Illleguleseny Resssicsieme -4 Othes (lingdaint Gilil)
F Opesas w Isaiseing a licenw I maensiosasinee 5
F Adseiiedssoasive
- G Opceasinmal Essus IEmplaisel 1!xhdoit I Saene S mece rs/17) 11 Delees IEmplain)
.. Dockst No.: 50-315 Unit N me =D.C. Cook Unit 1 Completed By: D. A. Bruck Telephone: (616) 465-5901 Date: December 9, 1985 Page: 1 of 3 MONTHLY OPERATING ACTIVITIES - NOVEMBER, 1985 HIGHLIGHTS:
The reporting period began with the reactor' coolant system in Mode 3 and 536*F temperature.
The low power physics testing began on 11-13-85 with the reactor being critical for the first time in Cycle IX at 1605 hours0.0186 days <br />0.446 hours <br />0.00265 weeks <br />6.107025e-4 months <br />. The low power physics testing was completed at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on 11-15-85 and the generator was paralleled to the grid at 2206 on 11-16-85.
On 11-17-85, the unit was removed from service to perform turbine overspeed testing. The unit was returned to service the same-day.
On 11-20-85, reactor power was increased to 48%. On 11-24-85, reactor power was increased to 68%. On ll-25-85, a reactor power increase to 80% began. A reactor trip occurred from 78% due to an inadvertant negative rate trip.
On 11-26-85, a reactor coolant system cooldown was started to repair leaks on the No. 12 reactor coolant pump flange. Mode 4 was entered on 11-26-85 and Mode 5 was entered on 11-27-85.
The reporting period ended with the reactor coolant system in Mode 5, cold shutdown.
Gross electrical generation for the month of November was 86,040 MWH.
SUMMARY
11-04-85 At 1631, an inadvertant source range reactor trip, while in Mode 3 occurred while performing surveillance tests.
11-06-85 At 0251, the Turbine Driven Auxiliary Feed Pump failed to start for surveillance testing due to erratic governor control.
11-09-85 At 0548, the Turbine Driven Auxiliary Feed Pump was declared operable.
3- -
' ~
Dock 0t Na.^ 50-315
^
> 'UnitLNemes D.C. Cook-Unite 11 Completed By: D. A. Bruck
- Telephone: (616)1465-5901-Date: December 9, 1985 Page:~ 2 of 3-
- 11-12-85 At 0230, a' turbine trip-occurred while in Mode 3,fdue to Hi-Hi steam generator ~ level.
At 1024, an inadvertantiESF actuation from highLateam line flow coincident with Lo-Lo Tave occurred which resulted infa safety injection actuation and' steam;line +
isolation. The cause was simultaneous surveillance testing of high steam line flow channels requiring bistables to be tripped and an auxiliary feedwater ,
system test adding _ water to the steam generators, resulting in RCS cooldown to the Lo-Lo Tave value, 11-13-85 At'1605, the reactor-became critical for the first time in Cycle IX.
11-14-85 At 0915, a power' increase began,; stabilizing at 2% at 1150. "
11-15-85 At 2300, low power physics testing was completed.
11-16-85 At 1300, a power increase began and the reactor entered ,
Mode 1 at 1320.
At 1426, the main turbine was rolled.
At 1540, the main turbine experienced high vibration and a shutdown was begun.
At 1555, the main turbine tripped on high vibration.
At 2000, a power increase began and the reactor entered Mode 1 at 2018.
At 2050, the main turbine was rolled.
At 2206, the generator was paralleled to the grid.
11-17-85 At 0150, the power increase stopped at 30%.
At 0210, a unit shutdown was begun <per Tech. Spec.
3.0.3 due to MFC-110'and MFC-111 being inoperable.
At 0436, MFC-110 was declared operable and a power increase began, stabilizing at'29% at 0720. .
I w.
F
, Dock;t No.: 50-315 Unit N:me: D.C. Cook Unit 1 Completed.By: D. A. Bruck Telephone: (616) 465-5901 Date: December 9, 1985 Page: 3 of 3 11-17-85 At 1250, a reactor power decrease to perform turbine overspeed testing began.
At 1415, an inadvertant Engineered Safety Features actuation occurred due to high alarms on containment radiation monitors 1401 and 1409.
At 1517, the generator was disconnected from the grid to perform turbine overspeed testing.
At 1532, the turbine tripped on high vibration.
At 1850, the generator was paralleled with the grid and power was stabilized at 29% at 0100.
11-20-85 At 1900, the Turbine Driven Auxiliary ree:1 Pump was declared inoperable due to governor oil leaking.
At 2245, a power increase began, stabilizing at 48% at 0534.
11-23-85 At 1312, the Turbine Driven Auxiliary Feed Pump was declared operable.
11-24-85 At 0006, a power increase began, stabilizing at 68% at 0924.
11-25-85 At 1850, a power increase to 80% began.
At 2243, with reactor power at 78%, the reactor tripped due to a negative rate trip. The trip resulted from one NIS power range channel's bistables being in the tripped position for surveillance testing and a spurious signal on a second power range channel while taking detector current readings for quadrant power tilt determination. A At 2300, the Turbine Driven Auxiliary Feed Pump was declared inoperable due to a broken control air line to the speed controller.
11-26-85 At 1623, a cooldown of the re' actor coolant system was started, entering Mode 4 at 2220.
11-27-85 At 1854, the reactor coolant system entered Mode 5.
e
> ~ ~
g _..
'4 o* -
, 3 y
DOCKET'NO. 150 - 315 UNIT NAME D. C. Cook - Unit'No. 1~.
DATE 6 COMPLETED BY .B. A. Svensson-TELEPHONE. (616) 465-5901 3 PAGE 1 of 1 l
MAJOR SAFETY-RELATED MAINTENANCE
-1 NOVEMBER, 1985 M-1 Reactor trip bypass breaker "B" would not close when racked into the test position. The fuse block. stabs were found to be spread open. The gap between the stabs was closed and the fuse block-reinstalled. The breaker now operates properly.
! M-2 Turbine Driven _ Auxiliary Feed Pump Trip and Throttle Valve was leaking by. Replaced internals and bonnet. Valve tested okay l after repsirs.
M-3 Found water in oil supply for Turbine Driven Auxiliary Feed Pump l governor. Removed governor, drained and flushed system. New governor was installed temporarily. Old governor was repaired by manufacturer and reinstalled on November 23, 1985.
C&I-l NIS, source range channel N-31, was reading erratic. Found source range preamplifier bad. Replaced source range preamplifier with new preamplifier. Performed' source range calibration and surveil-lance test and declared N-31 operable.
l C&I-2 Reactor coolant wide range Thot on loop 2 has a large deviation l compared to the other three loops.
Found R/I NTR-220, I/I NTR-120A and recorder out of calibration.
Recalibrated R/I, I/I and recorder. I/I NTR-120 could not be calibrated and had to be replaced. Loop 2 now agrees.with the other three loops.
C&I-3 Loop 1 wide range That is reading 20*F higher than the other three channels.
i Found R/I NIR-110 to be out of calibration high. Recalibrated the I/I. The four channels now agree with each other.
C&I-4 NPP-152, pressurizer pressure indication channel 11 is reading 35 to 40 psig lower than the other two channels.
Transmitter was found to be out of specification and could not be brought within specifications. Replaced with new transmitter; recalibrated and returned to service.
C&I-5 Steam generator #1 steam flow indication channels MFC-110 and 111 I were exhibiting low readings. The square root extractor for MFC-110 was replaced and MFC-lll's transmitter was recalibrated to restore correct flow indication to the channels.
_ g. , -
j *: ,'.
j* '
\
~
c.__,,,- . .,.,., e, 1u,,-
Donald C. Cc3 Nucteer Plant P.o. Som 450, Bridgman. Mchgen 49106 i
- Jecccher 6, 1985 i Director, Office Of Managemt.nt Information and Program Control U. S. Nuclear Regulatory Commission Washington, D. C. 205'55 Gentlemen:
Pursuant to the requirements of Donald'C. Cook Nuclear Plant Unit 1 Technical Specification 6.9.1.6, the attached Monthly Operating Report for the Month of November, 1985 is submitted.
Sircerely, t
W. G.
Yh' dth, Jr.
Plant rianager WGS:ab
\
Attachments l
's .
x cc: J. E. Dolan 9 \
M. P. Alexich '-
R. W. Jurgensen NRC Region III B. L. Jorgensen R. O. Bruggee
, R. C. Callen y SS. J. Hierzwa
P. D. Rennix ,
D. R. Hahn Z. Cordero J. J. Markowsky J. F. Stietzel PNSRC File INPO Records Center-ANI Nuclear Engineering Department
. ,