05000315/LER-1985-033, :on 850725,during Insp of Containment,Senior Reactor Operator Noticed Condensation Backed Up Due to Open Floor Drain Valve.Caused by Employee Error.Valve Immediately Closed

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:on 850725,during Insp of Containment,Senior Reactor Operator Noticed Condensation Backed Up Due to Open Floor Drain Valve.Caused by Employee Error.Valve Immediately Closed
ML20137F878
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 08/23/1985
From: Baker K
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20137F864 List:
References
LER-85-033, LER-85-33, NUDOCS 8508270113
Download: ML20137F878 (1)


LER-1985-033, on 850725,during Insp of Containment,Senior Reactor Operator Noticed Condensation Backed Up Due to Open Floor Drain Valve.Caused by Employee Error.Valve Immediately Closed
Event date:
Report date:
3151985033R00 - NRC Website

text

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D U S. NUCLEAGI f.EIULATOAV COMMesSION sRC Form 3e4 LPPROVED OMS NO 3150 4104

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LICENSEE EVENT REPORT (LER)

  1. AGE i3i DOCKET NUMSER (21 D. C. COOK NUCLEAR PLANT, UNIT 1 0 15Io1010131115 1 loFl Oil FACILITY NAME 11)

'flTLE 141 CONTAINMENT INTEGRITY DURING CORE ALTERATIONS OTHER FACILITIES INv0LVED IS)

EVENT DATE 484 LER NUMSER 46)

REPORT DATE 17)

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ON JULY 25, 1985 K

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.) THE T ACTOR OPERAIC CORE ALTERATI00-

A) COND AN. 1i UF I; INT AND NOTICEi.

CONDENSATION F OUE TO ZD FLn

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1LOOR DRAIN WAS E.

23 TO BE CLOSED ~

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fY Dl'hlM ALTEE SINCE GRE ALTU.10NS ERE STOPP!"

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LOW T CONDENSATE TO DRAlN.

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TO REC: ;E IT EDIATELY AFhs TfE DENSATION ILE lRAINE!;

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':D THE VALVE.

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SONNEL AT 1453 HOURS 3 WAS IMMEDIA :LY C:

a J RESUMED).

.alS WAS NOT A VIOLi 0F REQUIRED CONTAIN?ENT ISu F

.R SEAL PIM INT!!'

AN ATMOSPIERE TO AT':

IRE PATH. TIE POTENTI AL EXE HOW d A SIMILiR EVENT WHICH COULD HAVE CA' A LOSS OF INTEGRITY A W IS T10 SIS F6 1HIS REPORT.

WE ARE DEVE T NG AD.M 's ik. VE CONTROLS WHICH WILL

NIMIZF E POTENTIAL FOR s P t'RRENCE Im TF TYPE '

'tN E~.1 ; f. THESE CONTROLS WIL:- :E ESTA: :SHED PRIOR TO L H tNITS

. UEI,IN UTAGE (DECEMBER,1985).

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