ML20136G784

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Monthly Operating Rept for Oct 1985
ML20136G784
Person / Time
Site: Callaway Ameren icon.png
Issue date: 10/31/1985
From: Miltenberger S, Pratte D
UNION ELECTRIC CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
ULNRC-1204, NUDOCS 8601080558
Download: ML20136G784 (6)


Text

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i: e s 7_ t MONTHLY OPERATING REPORT p h 4 DOCKET NO. 50-483 E UNIT NAME CALLAWAY UNIT 1 h DATE NOVEMBER 13, 1985 C COMPLsIsu BY D. B '. PRATTE [5 TELEPHONE M14) 676-8745 [ { PART A OPERATIONS

SUMMARY

[ 4~3 OCTOBER 1985 h. g The unit was operated at full power for the month of October with the following h f! exceptions: .. w,

1. On 10/2/85 the unit tripped due to a personnel error during sruveillance ij testing of an RCS temperature loop.

n. On 10/7/85 the turbine generator was manually taken off line due to EHC

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tubing line failure to a main turbine control valve. s

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3. On 10/18/85 power was reduced to approximate 1v 68% to perform maintenance E Yl on secondarv system equipment.
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PART B PORV AND SAFETY VALVE

SUMMARY

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U l-1, Part C AVERAGE DAILY UNIT POWER LEVEL .. C p. DOCKET NO. 50-483 UNIT Callaway DATE NOVEMBER 13, 1985 f/ COMPLETED By f _. B. PRATTE . pz TELEPHONE (314) 676-8745 p; L:

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L: MONTH OCTOBER 1985 l,5 R DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL f (MWe-Net) (M.We-Net) p 1 1125 17 1107 2 855 ' gg 1097 h b, 3 11 j,, 756  :; pi. 4 725 20 852 E ra 1116 1111 5 21

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7 872 1113 23 8 0 24 1110 ,j 9 394 25 1118 f-10 991 1122 k 26 11 1104 27 1167 1094 g 1124 h 12 13 1099 3 1124 14 1105 1123 30 15 1122 31 1123 16 1111 O j'. ff C 0[ 4 Page 2 of 4 QDP-ZZ-04204 E M25_.o_. .p: n- r . =gtf- , . ,,ggj :,, y _

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k, Part D f. OPERATING DATA REPORT h DOCKET NO. 50-483 UNIT Callaway DATE NOVEMBER 13,-1985 D. B. PME COMPLETED BY i TELEPHONE (314) 676-R745 ( h i OPERATING STATUS

1. REPORTING PERIOD:

OCTOBER 1985 Gross HOURS IN REPORTING PERIOD: 745 e

2. CURRENTLY AUTHORIZED POWER LEVEL (Mwti: 3411 MAX. DEPEND. CAPACITY (MWo.Neti: 1170 OESIGN ELECTRICAL RATING IMWo.Neti: 1171* At Stretch reactor power level which is
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not currently authorized under the operating license. 5

3. POWER LEVEL TO WHICH RESTRICTED flF ANY) (MWo. Net):

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4. REASONS FOR RESTRICTION IIP ANY): .-

b THIS MONTH YR TO DATE CUMULATIVE

5. NUMSER OF HOURS REACTOR WAS CRITICAL . .. . .

716.8 6768.8 7071'.3 h i 6. REACTOR RESERVE SHUTDOWN HOURS . ..... 0 0 0 f 669.3 6603.6 6906.1

7. HOURS GENERATOR ON LINE . .. .. . .

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8. UNIT RESERVE SHUTDOWN HOURS . .. . . .

0 0 0

9. GROSS THERMAL ENERGY GENERATED IMWHI .... .... .7.906.146 70.R69 612 91 R AA 1 s7 lq
10. GROSS ELECTRICAL ENERGY GENERATED (MWM) . . . .. ..

758,545 7.045.187 7.384 367 b

11. NET ELECTRICAL ENERGY GENERATED (MWH) ...... ... .

720.034 6.686.596 7.004.619

12. REACTOR SERVICE FACTOR ....... ....... . ,,

96.2% 92.R% ol_1% [

13. REACTOR AVAILA81LITY FACTOR . ...... .... . .

96.2% 92.87. 41_1%

14. UNIT SERV 6CE FACTOR . . . .... .......... ..... . 89.8% 90.5% 40 o%
15. UNIT AVAILAGILITY FACTOR ,. .... ,.... .. .. ..

89.8% 90.5% 90.9%

16. UNIT CAPACITY FACTOR IUsene MDCI . ................

86.3% 81.8% 82.4%

17. UNIT CAPACITY FACTOR (Usene Dessen Mml . . . . . . . . . . . . . . ..

82.5%* 78.3%* 78.R%* 1s. UNIT FORCED OUTAGE RATE ,. ..............,....... *.8% 5.1% 4 4%

19. SHUTDOWNS SCHEDULED OVER NEXT 4 MONTHS (TYPE. DATE. ANO OURATION OF EACHt:

Refuel, 2/28/85, approximately 42 days. 7

20. IF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OP STARTUP:

j, 9 h c,

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                                                                                                                                                                .4 Part E                                   DOCKET NO.      50-483 il                                                   UNIT SHUTDOWNS AND POWER REDUCTIONS                           UNIT NAME      callaway NOVEMBER 13, 1985 I) ATE   ,

COMPLETED BY D. B. PRATTE OCTOBER 1985 TELEPiiONE (314) 676-8745 REPORT MONTIl METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO. DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS 21 851002 F 23.7 G 3 Unit tripped while I&C was performing h troubleshooting in conjunction with a RTD cross calibration procedure. LER 85-042-00. 22 651007 F 10 A 4 Turbine generator was taken off line due to an EHC oil leak on main turbine control valve #2.  ! 23 851018 S 42 B 1 Unit load reduced to 68% to perform II maintenance on secondary system equip-ment.

',            Es - R Y:                                                                                                                                                 l REASON                               IETMOD A: EQUlFMENT FAILURE (EXPLAIN)       3: MANUAL.

R: MAINT.OR TEST 2: MANUAL 3 CRAM C: REFUELING 3: ABITOMATIC SCRAM i D: REGULATORY RESTRKTION 4: OTIGER (EXPLAIN) E: OPERATOR TRAINING AND LICENSE EXAMINATION F: ADMINISTRATIVE G OPERATIONAL ERROR (EXPLAIN) CA-#804 It OTHER(EXPLAINI 05/09/84 Page 4 of 4 QDP-ZZ-04204

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P ,, c' Wand UNION ELECTRIC COMPANY Callag Plant November 13, 1985 Director, Resource Management Nuclear Regulatory Commission Washington, DC 20555 ULNRC-1204

Dear Sir:

DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT I FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT OCTOBER 1985 The enclosed Monthly Operating Report for October 1985 is submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications. S. E. Miltenberger vNf

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Manager, Callaway Plant

             ?[# G2C Q MET /IIRC/DBP/drs Enclosure cc: Distribution attached O

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Mailing Address: P.O. Box 620 Fulton, MO 65251

cc distribution for ULNRC-1204 with enclosures Mr. James G. Keppler Regional Administrator Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, DC 20555 NRC Resident Inspector I l M}}