Letter Sequence Other |
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MONTHYEARML20135E4851997-03-0505 March 1997 Responds to Requesting NRC Exercise Discretion Not to Enforce Compliance W/Actions Required in TS 4.5.2.f. Based on Evaluation of Request,Staff Concluded NOED Warranted Project stage: Other 1997-03-05
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20207G0621999-06-0404 June 1999 Forwards Insp Rept 50-346/98-21 on 980901-1201 & 990425-0513.Violations Identified & Licensee Being Provided Opportunity to Either Respond to Violations within 30 Days or Inform NRC That LER Rept Already Contain Info Requested ML20207B8161999-05-25025 May 1999 Confirms Discussion Between Members of Staffs to Have Mgt Meeting on 990608 in Oak Harbor,Oh to Discuss Recent Performance at Davis-Besse as Described in Plant Performance Review ML20207B3141999-05-24024 May 1999 Informs That in September 1998,Region III Received Revision 20 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Rev Submitted Under Provisions of 10CFR50.54(q) ML20206T0881999-05-18018 May 1999 Confirms 990517 Telcon Between Lindsey & M Bielby Re Arrangements Made for Administration of Licensing Exam at Facility for Week of 990913 ML20206N5311999-05-11011 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Aj Mendiola Will Be Section Chief for Davis-Besse Npp.Organization Chart Encl ML20206H2291999-05-0707 May 1999 Forwards Proposed Change to Plant,Unit 1,TS Bases Section 2.2.1, Limiting Safety Sys Settings - Reactor Protection Sys Instrumentation Setpoints - Rc Pressure - Low,High & Pressure Temp ML20206B8171999-04-27027 April 1999 Forwards Insp Rept 50-346/99-05 on 990405-09.No Violations Noted.Purpose of Insp Was to Examine on-line Maint Risk Assessment Program Recently Implemented in Response to Maint Work Control Weaknesses ML20205G5681999-03-26026 March 1999 Advises of Completion of Plant Performance Review on 990202 to Develop Integrated Understanding of Safety Performance. Overall Performance of Plant Acceptable.Plant Issues Matrix & Insp Plan Encl ML20207G1701999-03-0505 March 1999 Forwards Insp Rept 50-346/99-01 on 990102-0212.No Violations Noted ML20207D4351999-02-25025 February 1999 Forwards Insp Rept 50-346/99-02 on 990202-05.No Violations Noted.Examples of Deficiencies with Station Procedures, Similar to Those Identified Through Staff self-assessments & in Previous NRC Insps,Were Noted IR 05000346/19960141999-02-17017 February 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-346/96-14 on 970225.Ack That Due to Plant Events,There Has Been Delay in Completion of C/As for Violation 50-346/96-14c ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20206S0811999-01-22022 January 1999 Forwards Insp Rept 50-346/98-18 on 981110-990102.No Violations Identified.Conduct of Activities at Davis-Besse Generally Characterized by Conservative Plant Operations, & Effective Engineering Involvement in Plant Issues ML20199H5821999-01-20020 January 1999 Forwards SE Re Ampacity Derating Issues Due to Application of Thermo-Lag Fire Barrier Matl at Plant ML20198E6821998-12-17017 December 1998 Forwards Insp Rept 50-346/98-20 on 981116-20.No Violations Noted.Implementation of Licensed Operator Requalification Program Was Generally Characterized by Safety Conscious Operations & Sound Evaluation of Operator Performance ML20198C9881998-12-15015 December 1998 Informs That as Part of NRC PRA Implementation Plan, Commission Assigned Two SRAs to Each Regional Ofc.Sras Will Routinely Assess Licensee Event Repts,Plant Event,Insp Findings & EAs from Risk Perspective ML20198B5391998-12-0909 December 1998 Forwards Insp Rept 50-346/98-17 on 980918-1109 & NOV Re Inadequate Maint Work Order Used by Electrician During Removal of Primary Water Storage Tank Temp Indicator ML20196G1621998-12-0303 December 1998 Submits Response to Request for TS Interpretation Re Surveillance Interval Extension Allowances ML20196H4411998-12-0303 December 1998 Confirms Plans to Hold Meeting on 981216 in Lisle,Il,To Discuss Recent Performance at Davis-Besse & Actions Being Implemented by Licensee ML20198B1511998-12-0202 December 1998 Forwards Insp Activity Plan for Next 6 Months & Plant Issues Matrix.Infor Provided to Minimize Resource Impact on Staff & to Allow for Scheduling Conflicts & Personnel Availability to Be Resolved in Advance of Inspector Arrival Onsite ML20196J5111998-12-0101 December 1998 Fowards Year 2000 Readiness Audit Rept,Which Documents Results of NRR Audit Conducted at Facility from 981027-29 ML20196D4371998-11-25025 November 1998 Discusses Concerns Re Announced Asset Transfer Between Firstenergy Corp & Duquesne Light Co ML20196C6491998-11-20020 November 1998 Forwards Insp Rept 50-346/98-19 on 981014-23.No Violations Noted.Inspectors Reviewed Circumstances Surrounding Events Leading Up to & Following Reactor Trip IR 05000346/19983011998-11-0909 November 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-346/98-301OL Issued on 980923.Effectiveness of C/A Will Be Reviewed Following Submittal of Root Cause Investigation Results ML20155J1471998-11-0303 November 1998 Informs That on 981007,NRC Administered GFE Section of Written Operator Licensing Exam to Employees of Facility. Exam Answer Key for Forms a & B,Grading Results & Individual Answer Sheets Encl.Without Encl ML20155B6641998-10-28028 October 1998 Forwards Safety Evaluation Re Request for Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154Q6711998-10-16016 October 1998 Forwards Insp Rept 50-346/98-15 on 980914-18.No Violations Noted.Emergency Preparedness Program Effectively Implemented During 980624 Tornado Event & Station Personnel Responded Well to Event ML20154Q5891998-10-14014 October 1998 Forwards Insp Rept 50-346/98-14 on 980808-0918.No Violations Noted.Online Safety Equipment Outages Were Performed Well & IAW Established Procedures ML20154H0241998-10-0606 October 1998 Discusses Arrangements Made During 980924 Telcon for Insp of Licensed Operator Requalification Program at Davis Besse Nuclear Power Station During Wk of 981116 ML20154D1801998-09-30030 September 1998 Forwards Insp Rept 50-346/98-16 on 980831-0904.No Violations Noted 1999-09-07
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C Ctau p 1 UNITED STATES
, g j NUCLEAR REGULATORY COMMISSION g WASHINGTON D.C. 2006H001 March 5, 1997 Mr. John K. Wood Vice President - Nuclear, Davis-Besse '
Centerior Service Company c/o Toledo Edison Company Davis-Besse Nuclear Power Station ,
5501 North State Route 2 i Oak Harbor, Ohio 43449-9760
SUBJECT:
NOTICE OF ENFORCEMENT DISCRETION FOR TOLED0 EDIS0N COMPANY, CENTERIOR SERVICE COMPANY, AND THE CLEVELAND ELECTRIC ILLUMINATING COMPANY REGARDING DAVIS-BESSE NUCLEAR POWER STATION, UNIT N0. 1 l (TAC NO. M97941, N0ED NO. 97-6-003)
Dear Mr. Wood:
By letter dated February 13, 1997, you requested that the NRC exercise discretion not to enforce compliance with the actions required in Technical Specification (TS) Surveillance Requirement 4.5.2.f. This surveillance requirement requires each Emergency Core Cooling System subsystem to be demonstrated operable by performing a vacuum leakage rate test of the valve pit leaktight enclosure for valves DH-11 and DH-12 to assure that the motor operators on these valves will not be flooded for at least 7 days following a loss-of-coolant accident.
Your letter documented information previously discussed with the NRC in telephone conversations during the evening (between approximately 5:00 p.m.
and 8:00 p.m.) of February 12, 1997. You stated.during those conversations that the Davis-Besse Nuclear Power Station was not in compliance with surveillance requirement 4.5.2.f, and that TS 3.0.3, which requires a plant shutdown to begin in I hour, had been entered at 9:15 that morning. You further stated that TS 4.0.3 had also been entered, which allows you to delay the actions of TS 3.0.3 for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> so the surveillance requirement can be completed. At 2:35 p.m., you determined that the surveillance requirement could not be performed at power. This determination is based on the fact that the surveillance includes a test which draws a vacuum on the leaktight enclosure, and if a loss-of-coolant accident were to occur during the test, the pressure in the area of the enclosure combined with the vacuum inside the enclosure would fail the pit cover, potentially flooding the valve operators.
Therefore, you exited TS 4.0.3, and a plant shutdown was begun at 3:21 p.m.,
in accordance with TS 3.0.3.
You requested that a Notice of Enforcement Discretion (NOED) be issued pursuant to the NRC's policy regarding exercise of discretion for an operating facility, set out in Section VII.c of the " General Statement of Policy and Procedures for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600. You requested that the N0ED be effective immediately and remain in force until the NRC approves your license amendment request (submitted by letter dated February 14,1997) to revise the TS requirements, or until Davis-Besse enters Mode 4 in an outage of sufficient duration to perform the required test.
NRC FE CENTER CDP 7 p* "
9703070092 970305 PDR ADOCK 05000346 G PDR
O J. Wood 1 i
In your letter, you stated that a plant modification was completed in 1986 on the decay heat valve pit to install level switches and to add an inspection port to the pit leaktight enclosure. One use of the inspection port is for insertion of a camera during performance of American Society of Mechanical '
Engineers Boiler and Pressure Vessel Code-required visual inspections, which, at Davis-Besse, must be performed in Mode 3. You previously had concluded that the port could be opened and closed without the need to perform surveillance requirement 4.5.2.f after closure. On February 11, 1997, Davis-Besse staff identified the concera regarding whether opening and subsequent closure of the decay heat valve pit port constituted a breach in the leaktight enclosure, hence requiring performance of surveillance requirement 4.5.2.f.
Followup by plant staff discovered that the port had been opened and closed since the last performance of surveillance requirement 4.5.2.f. At that time, TS 3.0.3 was entered, as discussed above.
Your safety rationale for requesting the N0ED was based on the design and previous test performance of the special coupling that was employed in the ,
port design, and the compensatory measures that you have taken. This coupling is designed for a temperature of 380*F and a pressure of 150 psig, significantly above the temperature and pressure expected in the area of the port post-accident. In addition, no sealing problems have been identified with the port coupling during the survei'llance requirement 4.5.2.f tests that have been conducted since the port was installed in 1986. Further, the proper closure of the port is always verified after usage in accordance with plant procedures. As a compensatory measure, after entering TS 3.0.3, the port was '
opened and inspected, found to be in good condition, and then verified to be properly closed.
The valve pit serves as a leaktight enclosure for motor-operated valves DH-11 and DH-12 in the " drop" line that connects the reactor coolant system loop I hot leg to the decay heat pump suction connections. These valves are normally closed. They must be opened in order to establish the shutdown cooling mode of operation. They would also be opened under loss-of-coolant accident recovery procedures, for the boron dilution mode of operation, an action that would be taken to reduce the possibility of boron precipitation in the core region. If the pit enclosure is not leaktight, the high water level in containment that results from a loss-of-coolant accident could flood the DH-11/12 electric motor operators and thereby preclude their opening. The enclosure is provided with non-safety, high and high-high water level switches. An alternate method of boron dilution is available by use of auxiliary spray as described in FSAR Section 6.3.3.1.2.
The port closure device is a Kamlok cap which consists of an adapter that is welded to a 4-inch pipe that rises from the pit cover, and a cap and gasket assembly that clamps over the adapter. To seal the cap in place, it is placed on the adapter and two levers are positioned such that cams on the levers engage a groove in the adapter while compressing the gasket in the cap. If the gasket is in place and the levers properly psitioned, gasket compression, and thus tight sealing, is assured. The licensee's procedures verify that the cap is correctly reinstalled.
The staff considered the design features and test history of the Kamlok cap, as described by the licensee, and concluded that it provides a high degree of assurance of proper sealing. The staff also determined the consequences of
- - . = _ _ . . .
- J. Wood failure of the cap to seal under post-loss-of-coolant accident conditions and noted that any failure of leaktightness would not affect the short-term cour.se of the event, and that for the longer-term boron dilution capability, an alternate method is available. The staff also considered the compensatory measures taken to ensure that the port is currently properly closed. Based on these considerations, the N0ED was granted at 8:05 p.m. on February 12, 1997, under Criteria 1(a) of NUREG-1600, to avoid undesirable transients as a result of forcing compliance with a license condition and, thus, to minimize -
potential safety consequences and operational risks.
On the basis of the staff's evaluation of your request, the staff has concluded that an N0E0 is warranted because we are clearly satisfied that this !
action involves minimal or no safety impact and has no adverse radiological impact on public health and safety. Therefore, it is our intention to exercise discretion not to enforce compliance with TS surveillance requirement 4.5.2.f for the period from February 12, 1997, 8:05 p.m. ET, until the NRC j approves your license amendment request to revise the TS requirements, or !
until Davis-Besse enters Mode 4 in an outage of sufficient duration to perform the required surveillance test. I This letter documents our telephone conversations during the evening (between approximately 5:00 p.m. and 8:00 p.m.) of February 12, 1997, when we orally issued this N0ED. However, as stated in the Enforcement Policy, action will normally be taken, to the extent that violations were involved, for the root 4 cause that led to the noncompliance for which this N0ED was necessary.
Sincerely, Original signed by:
Jack W. Roe, Director Division of Reactor Projects III/IV Office of Nuclear Reactor Regulation Docket No. 50-346 cc. See next page Distribution:
Docket File PUBLIC PDIII-3 R/F G. Hill (2 cys)
S. Collins /F. Miraglia C. Grimes ACRS W. Long R. Zimmerman A. Thadani J. Caldwell, RIII J. Lieberman J. Roe E. Adensam G. Marcus DEDR & DRPE TA OGC EMail - N0ED TGD -
DOCUMENT NAME:G:\DAVISBES\DB97941.LTR
- See previous concurrence Te receive a copy of this document, indicate in the box: "C" = Copy without enclosures "E" = Copy with enclosures "N" = No copy 0FFICE LA:PDIII-3 l C PM:PDIII-M C SCSB:DSSA l SRXB:DSSA D:PD III-3 l NAME EBarnhill CP( AHanseryfdMf CBerlinger
- DATE 03/06/97 03/ 5 /V 2/19/97 A 2/19/97 2/18/97 0FFICE D:DRP: Rill C D:DSSA D:QRPW,3 DI NAME JGrobe (Phone) GHolahan
- JRof DATE 2/19/97 3/5/97 3/ F/97 0FFICIAL RECORD COPY
J. Wood .
, failure of the cap to seal under post-loss-of-coolant accident conditions and noted that any failure of leaktightness would not affect the short-term course of the event, and that for the longer-term boron dilution capability, an alternate method is available. The staff also considered the compensatory measures taken to ensure that the port is currently properly closed. Based on these considerations, the N0ED was granted at 8:05 p.m. on February 12, 1997, under Criteria 1(a) of NUREG-1600, to avold undesirable transients as a result of forcing compliance with a license condition and, thus, to minimize -
potential safety consequences and operational risks.
On the basis of the staff's evaluation of your request, the staff has concluded that an N0ED is warranted because we are clearly satisfied that this action involves minimal or no safety impact and has no adverse radiological impact on public health and safety. Therefore, it is our intention to exercise discretion not to enforce compliance with TS surveillance requirement 4.5.2.f for the period from February 12, 1997, 8:05 p.m. ET, until the NRC approves your license amendment request to revise the TS requirements, or until Davis-Besse enters Mode 4 in an outage of sufficient duration to perform the required surveillance test.
This letter documents our telephone conversations during the evening (between >
approximately 5:00 p.m. and 8:00 p.m.) of February 12, 1997, when we orally l issued this N0ED. However, as stated in the Enforcement Policy, action will normally be taken, to the extent that violations were involved, for the root cause that led to the noncompliance for which this N0ED was necessary. l Sincerely, .
Original signed by:
Jack W. Roe, Director Division of Reactor Projects III/IV Office of Nuclear Reactor Regulation Docket No. 50-346 4
cc. See next page Distribution:
Docket File PUBLIC PDIII-3 R/F G. Hill (2 cys)
S. Collins /F. Miraglia C. Griines ACRS W. Long R. Zimmerman A. Thadani J. Caldwell, RIII J. Lieberman J. Roe E. Adensam G. Marcus DEDR & DRPE TA OGC EMail - NOED TGD -
DOCUMENT NAME:G:\DAVISBES\DB97941.LTR
- See previous concurrence Ta receive a copy of this docurnent, indicate in the box: "C" = Copy without enclosures *E' = Copy wrth enclosures *N" = No copy 0FFICE LA:PDIII-3 C PM:PDIII-M C SCSB:DSSA SRXB:DSSA l D:PD III-3 l NAME EBarnhill C H AHansepfC4f CBerlinger
- umans names s'im !am aus 0FFICE D:DRP:RIII C D:DSSA D:QBPW-NAME JGrobe (Phone) GHolahan
- JRof DATE 2/19/97 3/5/97 3/ F/97 0FFICIAL RECORD COPY
Mr. John K. Wood Davis-Besse Nuclear Power Station l Toledo Edison Company Unit No. 1 CC: ,
Mary E. O'Reilly Robert E. Owen, Chief !
Centerior Energy Corporation Bureau of Radiological Health 300 Madison Avenue Service Toledo, Ohio 43652 Ohio Department of Health ,
P. O. Box 118 l Mr. James L. Freels Columbus, Ohio 43266-0118 !
Manager - Regulatory Affairs l Toledo Edison Company l
Davis-Besse Nuclear Power Station Attorney General I 5501 North State - Route 2 Department of Attorney Oak Harbor, Ohio 43449-9760 30 East Broad Street Columbus, Ohio 43216 Gerald Charnoff, Esq. ;
Shaw, Pittman, Potts Mr. James W. Harris, Director i and Trowbridge Division of Power Generation 2300 N Street, N.W. Ohio Department of Industrial Washington, D.C. 20037 Regulations P. O. Box 825 Regional Administrator Columbus, Ohio 43216 U.S. NRC, Region III 801 Warrenville Road Ohio Environmental Protection Agency Lisle, Illinois 60523-4351 DERR--Compliance Unit ATTN: Zack A. Clayton Mr. Robert B. Borsum P. O. Box 1049 ,
i Babcock & Wilcox Columbus, Ohio 43266-0149 Nuclear Dower Generation Division 1700 Rockville Pike, Suite 525 State of Ohio l Rockville, Maryland 20852 Public Utilities Commission '
180 East Broad Street i Resident Inspector Columbus, Ohio 43266-0573 U. S. Nuclear Regulatory Commission l 5503 N. State Route 2 Mr. James R. Williams Oak Harbor, Ohio 43449 , Chief of Staff Ohio Emergency Management Agency !
Mr. James H. Lash, Plant Manager 2855 West Dublin Granville Road '
Toledo Edison Company Columbus, Ohio 43235-2206 Davis-Besse Nuclear Power Station 5501 North State Route 2 President, Board of County Oak Harbor, Ohio 43449-9760 Commissioner of Ottawa County Port Clinton, Ohio 43452