ML20134H316

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Forwards Proposed License Amend to App A,Ts of Licenses NPF-35 & NPF-52 for Plants.Change Would Eliminate During Shutdown Restriction for 18 Month Standby Shutdown Sys DG Insp TS Surveillance 4.7.13.1.c
ML20134H316
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 11/04/1996
From: Mccollum W
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20134H318 List:
References
NUDOCS 9611140054
Download: ML20134H316 (4)


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[] uke Pou etCompany WwerR McCotnv JR Catonha Nudear Generation Department Vicehesident 4800 ConcordRoad (8031831JD) Office York, SC39745 (8W)M314t% Fax DU90? POWER November 4, 1996 U.

S. Nuclear Regulatory Commission ATTN:

Document Control Desk Washington, D.

C.

20555

Subject:

Catawba Nuclear Station, Units 1 and 2 Docket Nos. 50-413 and 50-414 Proposed Technical Specifications (TS) Change Pursuant to 10 CFR 50.4 and 10 CFR 50.90, attached is a proposed license amendment to Appendix A, Technical Specifications, of Facility Operating Licenses NPF 35 and NPF 52 for Catawba Nuclear Station Units 1 and 2, respectively.

The proposed change would eliminate the "during shutdown" restriction for the 18 month Standby Shutdown System (SSS) diesel genen. tor inspection Technical Specification surveillance 4.7.13.1.c.

During a review of this Technical Specification Surveillance Requirement, it was recognized that performance of the surveillance was required "during shutdown".

Further review has determinded that the "during shutdown" requirement has not l

always been met.

Performance of past surveillance inspections

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has been completed under the action statement for the SSS system, as defined in Technical Specification 3.7.13.

The action statment provides an allowable outage time of 7 days as given in the Limiting Condition For Operation.

Past surveillance

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inspections have been completed within this time frame, otherwise i

both units would have been in Hot Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in at least Hot Shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> as i

required by the Limiting Condition For Operation. Therefore, restricting the surveillance inspection to be performed only during shutdown of one or both units has been unnecessary. contains the marked up Technical Specification pages of Catawba Technical Specifications as affected by the enclosed requested amendment. contains a background, description and technical justification of the enclosed requested amendment.

Pursuant to 10 CFR 50.91, Attachment 3 provides the analysis performed in accordance_with the standards contained in 10 CFR 50.92 which concludes that the requested amendment does not involve a significant cafety hazards consideration. also contains an environmental impact analysis for i

the requested amendment.

Duke Power Company is forwarding a copy of this snendment request' package to the appropriate South l

Carolina state official, 00l j,a 9611140054 961104 PDR ADOCK 05000413 P

PDR Rewom mycwwk

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U.

S. Nuclear Regulatory Commission Novembek 4, 1996 i

Page 2 l

The Catawba Updated Final Safety Analysis Report (UFSAR) was reviewed for changes required by this proposed change to the Technical Specifications, and none were identified.

This proposed change to the Technical Specifications has been reviewed and approved by the Catawba Plant Operations Review Committee and the Nuclear Safety Review Board.

The 18 month Standby Shutdown System (SSS) diesel generator inspection surveillance required by Technical Specification 4.7.13.1.c will be due on May 29, 1997 (does not include maximum i

allowable extension).

Therefore, it is requested that the review i

and approval of this proposed amendment be completed by April 1, 1997.

Should there be any questions or should additional information be required, please contact Devereux Tower at 803-831-3419.

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l Sincerely, l

C,s

W.

R. McCollum, J Attachments j

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S.

D.

Ebnecer, Regional Administrator l

U.

8. Nuclear Regulatory Commission Region II 101 Marietta Street, NW - Suite 2900

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Atlanta, Georgia 30323 l

i R. J.

Freudenburger Senior Resident Inspector Catawba Nuclear Station P.

S. Tam, Project Manager l

Office of Nuclear Reactor Regulation U.

S. Nuclear Regulatory Commission Mail Stop 14H25, OWFN washington, D. C.

20555 Max Batavia, Chief Bureau of Radiological Health S. C.

Department of Health and Environmental Control 2600 Bull Street Columbia, South Carolina 29207 1

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U. S. Nuclear Regulatory Commission l

Novembdr 4, 1996 Page 3 i

W. R. McCollum Jr., being duly sworn, states that he is Vice-President of Duke Power Company, Catawba Nuclear Station; that he l

is authorized on the part of said Company to sign and file with l

the Nuclear Regulatory Commission this revision to the Catawba Nuclear Station License Nos. NPF-35 and NPF-52 and that all statements and matters set forth therein are true and correct to the best of his knowledge.

4 W. R. McCollum, Jr Vice-President, Catawba Nuclear Station l

Subscribed and sworn to before me this 4th day of November, 1996.

M.

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I-Notary Public My commission expires:

AMa6M RA 2005 i

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U. S. Nuclear Regulatory Commission Novembir 4, 1996 Page 4 i

i bxc: ELL EC050 J. E.

Snyder MC01RC J.

E. Burchfield ONO3RC 1

R. M. Glover CNO3CE A.

S. Bhatnagar CN020PS P. R. Newton PB05E M. S. Kitlan, Jr.

CN01RC 1

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L.

Lowery CN01RC l

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E. Crawford CNO3SE L

NCMPA-1 NCEMC PMPA SREC l

Document Control File CN-801.01 Group File CN-801.01 l

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