ML20134G100

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-458/96-15
ML20134G100
Person / Time
Site: River Bend Entergy icon.png
Issue date: 02/03/1997
From: Dyer J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Mcgaha J
ENTERGY OPERATIONS, INC.
References
NUDOCS 9702100272
Download: ML20134G100 (5)


See also: IR 05000458/1996015

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611 RY AN PL AZA oRIVE, SUITE 400

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ARLINGTON, TEXAS 76011 8064

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FEB - 31997

John R. McGaha, Vice President Operations

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River Bend Station

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Entergy Operations, Inc.

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P.O. Box 220

St. Francisville, Louisiana 70775

SUBJECT: NRC INSPECTION REPORT 50-458/96-15

Thank you for your letter of January 24,1997,in response to our letter and Notice

of Violation dated December 2,1996. We have reviewed your reply and find it responsive

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to the concerns raised in our Notice of Violation. We will review the implementation of

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your corrective actions during a future inspection to determine that full compliance has

been achieved and will be maintained.

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Sin

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J. E. Dyer, D' ector

Division of R

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Docket No.: 50-458

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License No.: NPF-47

cc:

Executive Vice President and

Chief Operating Officer

Entergy Operations, Inc.

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P.O. Box 31995

Jackson, Mississippi 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

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P.O. Box 31995

Jackson, Mississippi 39286-1995

9702100272 970203

PDR

ADOCK 05000458

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Entergy Operations, Inc.

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General Manager

Plant Operations

River Bend Station

Entergy. Operations, Inc.

P O. Box 220

St. Francisville, Louisiana 70775

Director Nuclear Safety

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River Bend Station

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Entergy Operations, Inc.

P.O. Box 220

St. Francisville, Louisiana 70775

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Wise, Carter, Child & Caraway

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P.O. Box 651

Jackson, Mississippi 39205

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Mark J. Watterhahn, Esq.

Winston & Strawn

1401 L Street, N.W.

Washington, D.C. 20005-3502

Manager - Licensing

River Bend Station

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Entergy Operations, Inc.

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P.O. Box 220

St. Francisville, Louisiana 70775

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.The Honorable Richard P. leyoub

~ Attorney General

P.O. Box 94095

Baton Rouge, Louisiana 70804-9095

H. Anne Plettinger

3456 Villa Rose Drive

Baton Rouge, Louisiana 70806

President of West Feliciana

Police Jury-

P.O. Box 1921

St. Francisville, Louisiana 70775

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Entergy Operations, Inc.

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Larry G. Johnson, Director

Systems Engineering

Cajun Electric Power Coop. Inc.

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10719 Airline Highway

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P.O. Box 15540

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Baton Rouge, Louisiana 70895

William H. Spell, Administrator

Louisiana Radiation Protection Division

P.O. Box 82135

Baton Rouge, Louisiana 70884-2135

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Leah Tremper (OC/LFDCB, MS: TWFN 9E10)

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DOCUMENT NAME: R:\\_RB\\RB615AK.LAK

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W3F1-97-0002

A4.05

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January 21,1997

JM P. 2

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U.S. Nuclear Regulatory Commission

ATTN: Document Control Desk

Washington, D.C. 20555

Subject:

Waterford 3 SES

Docket No. 50-382

License No. NPF-38

NRC Inspection Report 50-382/96-13

Reply to Notice of Violation

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Gentlemen:

In accordance with 10CFR2.201, Entergy Operations, Inc. hereby submits in

Attachment 1 the response to the violations identified in Enclosure 1 of the subject

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Inspection Report.

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Waterford 3 acknowledges the three concerns expressed in the cover letter to the

inspection report: (1) operators failed to follow procedures regarding configuration

control, (2) operators failed to recognize that the wet cooling tower fans were

rendered inoperable during a maintenance activity and failed to enter appropriate

Technical Specification (TS) Limiting Conditions for Operation, and (3) review of the

Inservice Test (IST) program did not identify the need to perform testing on the dry

cooling tower isolation valves which are required to be repositioned during the design

basis tornado event.

Regarding the first concern, Waterford 3 has previously identified an increasing trend

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in the number of human performance violations. Our comprehensive corrective

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actions to address that trend are detailed in Letter W3F1-96-0213 dated 12/13/96.

We believe those corrective actions, in concert with the actions detailed in

Attachment 1, will help prevent similar violations from recurring and will improve

operator attentiveness.

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Reply to Notice of Violation (IR 96-13)

W3F1-97-0002

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January 21,1997

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In addition to the corrective actions detailed in Attachment 1 for the second concern,

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we are continuing to implement corrective actions from the FOCUS plan (reference

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Letter W3F1-96-0130 dated 8/19/96) to improve our performance in the area of TS

implementation. These actions include enhancing the procedure process, utilizing

assessments as a tool to identify additional improvement opportunities, improving

operator awareness of plant conditions prior to approving maintenance activities, and

establishing specific guidance concerning the control of work and pre-job briefings to

ensure proper Operations oversight. Furthermore, Waterford 3 management has

placed significant focus on assuring that the culture and policy for implementing

Technical Specifications are conservative from a safety standpoint and comply with

regulatory requirements.

Regarding the third concern, the dry cooling tower isolation valves will be added to

the IST plan. Furthermore, we are developing a document that details the design

basis tornado event. This document should increase the probability that similar

conditions, if they exist, are identified and corrected.

Should you have any questions concerning this response, please contact

me at (504) 739-6666 or Jeff Thomas at (504) 739-6531.

Very truly yours,

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T.J. Gaudet

Acting Director,

Nuclear Safety & Regulatory Affairs

TJG/GCS/tjs

Attachment

cc:

E.W. Merschoff (NRC Region IV)

C.P. Patel (NRC-NRR)

R.B. McGehee

N.S. Reynolds

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NRC Resident inspectors Office

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Attachm:mt to

W3F1-97-0002

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Page 1 of 8

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ATTACHMENT 1

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ENTERGY OPERATIONS. INC RESPONSE TO THE VIOLATION IDENTIFIED IN

ENCLOSURE 1 OF INSPECTION REPORT 96-13

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VIOLATION NO. 9613-01

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Technical Specification 6.8.1.a requires, in part, that written

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procedures shall be implemented covering applicable procedures recommended in

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Appendix A of Regulatory guide 1.33, Revision 2, February 1978. Appendix A,

Section 3, requires that the licensee have procedures for operation of safety related

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systems.

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Procedure OP-002-010. " Reactor Auxiliary Building HVAC and Containment

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Purge," Revision 11, Section 6.6, required that the airbome radioactivity

removal system be secured when stopping containment purge.

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Contrary to the above, on October 1,1996, the licensee failed to secure the

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airborne radioactivity removal system after stopping containment purge. The

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airborne radioactivity removal system was not secured until observed in the

abnormal configuration on October 20,1996, a period of 19 days.

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2.

Procedure OP-002-003, " System Operating Procedure - Component Cooling

Water System," Revision 10, Section 6.0, " Normal Operations," required the

dry cooling tower fan control switches be in the AUTO position.

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Contrary to the above, on October 19,1996, at 3:37.a.m., operators

inadvertently placed the Dry Cooling Tower Fan 13-B control switch in the

OFF position. The switch remained in the OFF position until observed in the

abnormal configuration at 4:40 p.m. on October 20, a period of 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

3.

Procedure OP-903-121, " Safety Systems Quarterly IST Valves Tests,"

Revision 1, Section 7.2, " Safety injection Train B," requires that Valve S11398

be closed following inservice testing.

Contrary to the above, on November 19,1996, at 1:42 a.m., operators failed

to close Valve SI-1398 following inservice testing. Valve SI-139B was not

closed until operators observed the abnormal configuration at 4 p.m. on

November 21,1996, a period of 62 hours7.175926e-4 days <br />0.0172 hours <br />1.025132e-4 weeks <br />2.3591e-5 months <br />.

This is a Seve@ Level IV violation (Supplement 1). (50-382/9613-01)

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W3F1-97-0002

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RESPONSE

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Reason for the Violation

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This violation was due to personnel error and inattention to detail in that

operators involved with each of the occurrences failed to follow procedures

and failed to closely monitor activities that were taking place on the control

board. The operators are required to be cognizant of activities on all the -

control panels and the attention given to the control panels with the incorrect

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configurations was not adequate. The operations shift turnover on the plant

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configuration was inadequate in that configuration errors existed over several

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shifts and were never discussed or identified by the oncoming shifts until 19

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days for example 1,36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> for example 2 and 62 hours7.175926e-4 days <br />0.0172 hours <br />1.025132e-4 weeks <br />2.3591e-5 months <br /> for example 3 of the

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violation. In addition, Operations supervisory personnel (Control Room

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Supervisor (CRS) and Shift Superintendent [SS) ) did not provide adequate

oversight of the activities taking place on the control panels.

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Contributing to the failure to follow procedure OP-002-010, " Reactor Auxiliary

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Building HVAC and Containment Purge," to secure the airborne radioactivity

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removal system was an inadequate place keeping method in procedure OP-

002-010. This procedure does not have sign-offs for each action step

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delineated. Consequently, steps in the procedure, such as those sccuring the

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airborne radioactivity system, may be overlooked due to a sign-off not being

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required. In addition, Operations supentisory personnel (Control Roam

Supervisor (CRS] and Shift Superintendent [SS) ) did not provide adequate

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oversight of the activities taking place on the control panels.

Contributing to the failure to follow procedure OP-002-003, " System Operating

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Procedure- Component Cooling Water System," which requires the Dry

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Cooling Tower Fan 13-B control switch to be in Auto position was that there is

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no difference in light indication on the DCT fan control switch when the switch

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is in auto position compared with the off position. The operators rely on the

position of the control knob pointer to determine the position of the control

switch. In addition, Operations supervisory personnel did not provide

adequate oversight of the activities taking place on the control panels.

Contributing to the failure to follow Section 7.2, " Safety injection Train B," of -

procedure OP-903-121, " Safety Systems Quarterly IST Valves Tests," was

that the operators, who should have closed valve SI-139 from the control

board, were involved with another activity which distracted their attention and

caused them to overlook the position of valve SI-139. Even though

distractions are a cue to self checking, proper self checking was not done. In

addition, Operations supervisory personnel did not provide the proper work

environment to minimize these distractions.

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Attachm:nt to

W3F1-97-0002

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Page 3 of 8

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(2)

Corrective Steos That Have Been Taken and the Results Achieved

1.

Condition reports 96-1639,96-1640 and 96-1847 were generated for

each one of the self-identified occurrences.

2.

All the components were placed in their correct configuration.

3.

All the operators involved with the failure to restore the plant to its

correct configuration have been counseled.

4.

Operations Manager reinforced the operators requirement to perform

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thorough control board walkdowns.

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All control room operators are required to sign a new addendum sheet

to the shift log indicating completion of control board panel walkdowns.

(3)

Corrective Steos Which Will Be Taken to Avoid Further Violations

1.

The Operations Manager will issue a letter to all Shift Superintendent

and Contro! Room Supervisors which will emphasize the importance of

properly prioritizing tasks to avoid excessive operator work load.

2.

The Operations Manager will clarify to operations supervisory

personnel the expectation that licensed operators have responsibility

for monitoring plant controls. The supervisory personnel will convey

these expectations to the operations staff.

3.

The Operations department will form a team to review and improve, if

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appropriate, the current method used for shift turnover. A review of the

inadequacy of reviewing shift logs will also be performed.

4.

A review will be performed on normal operating procedures to

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determine if the method for place keeping in procedures can be

improved.

(4)

Date When Full Comoliance Will Be Achieved

Waterford 3 is in full compliance. Items 1,2, and 3 will be completed by

2/28/97 and item 4 will be completed by 7/1/97.

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Attachment to

W3F1-97-0002

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ATTACHMENT 1

ENTERGY OPERATIONS. INC. RESPONSE TO THE VIOLATION IDENTIFIED IN

ENCLOSURE 1 OF INSPECTION REPORT 96-13

VIOLATION NO. 9613-03

Technical Specification 3.7.4.f requires, in part, that, with more than one wet cooling

tower fan inoperable and the outside air temperature greater than 70 degrees F, the

dry bulb temperature must be determined at least once every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

Contrary to the above, between May 5 and 9,1996, with more than one wet cooling

tower fan inoperable and the outside air temperature greater than 70 degrees F, the

licensee did not determine the dry bulb temperature at least once every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

This is a Severity Level IV violation (Supplement 1). (50-382/9613-03)

RESPONSE

(1)

Reason for the Violation

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Entergy Operations admits this violation and believes that the root cause is

inadequate work controls in that the method used in the engineering

evaluations was not standardized. There was no standard method or process

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to establish administrative controls for the format, required level of

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review / approval, and operations interface of the evaluation that was used to

document the inoperability of the _ wet cooling tower fans. Guidance on the use

of engineering input to evaluate work that may impact operabilty of safety

related or technical specification equipment was inadequate. As a result, an

adequate level of review of the engineering evaluation was not performed and

the fact that the wet cooling tower fans would be rendered inoperable while

netting was placed around the wet cooling tower basin was not clearly

communicated to operations. As a result of operations not being cognizant of

the wet cooling tower fans inoperability, the required actions per Technical Specification 3.7.4.f was not performed.

(2)

Corrective Steos That Have Been Taken and the Results Achieved

1.

Condition report 96-729 was generated to document and address this

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matter.

2.

LER 96-005 Revision 0 was issued to report this occurrence.

3.

The temporary netting that rendered the fans inoperable was removed.

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Attachment to

W3F1-97-0002

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Page 5 of 8

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4.

Operations Administrative Procedure OP-100-014, " Technical

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Specification Compliance," has been revised to require the following:

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a.

If any system, sub-system, or component becomes unable to

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perform its intended safety function due to surveillance,

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calibration, or maintenance, then declare that equipment

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inoperable and enter the appropriate Tech / Spec TRM (Technical

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Requirements Manual) action.

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b.

If a component is thought to be Inoperable enter the appropriate

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Tech Spec /TRM action and initiate LCO tracking in accordance

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with OP-100-010, " Equipment Out of Service."

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c.

The engineering guidance should have at least two signatures

on it indicating that a technical review has been performed.

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d.

The engineering guidance must be specifically bounded against

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any applicable Tech Specs. All engineering guidance

parameters must be bounded by Tech Spec parameters, and in

all cases, operators will adhere to the Tech Specs.

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e.

The STA should perform a review of the engineering guidance

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and provide a recommendation to the SS concerning the

adequacy of the guidance.

5.

Plant Administrative Procedure UNT 007-053 " Engineering Work

Authorization," has been revised to specify the following:

a.

An engineering input will not be used to make operability

determinations for technical specifications or safety related

equipment, nor will it be used to implement configuration '

changes.

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b.

. All nonconformance conditions are addressed by Corrective

Action Site Directive, W2.501,

c.

Engineering inputs are only used to facilitate work such as

bolting, torquing, gasketing, material condition improvements,

troubleshooting and venting requirements.

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d.

All engineering inputs require a technical reviewer signature.

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W3F1-97-0002

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(3)

Corrective Steos Which Will Be Taken to Avoid Further Violations

The Engineering Request process will replace the Problem

Evaluation /Information Request (PElR) for the purpose of engineering

evaluations.

(4)

Date When Full Comoliance Will Be Achieved

Waterford 3 is currently in full compliance. The above corrective action will be

completed by 9/30/97.

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Attachment to

W3F1-97-0002

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ATTACHMENT 1

ENTERGY OPERATIONS. INC. RESPONSE TO THE VIOLATION IDENTIFIED IN

ENCLOSURE 1 OF INSPECTION REPORT 96-13

VIOLATION NO. 9613-04

10 CFR 50.55a(g) requires, in part, that inservice testing to verify operational

readiness of pumps and valves whose function is required for safety be

accomplished in accordance with Section XI of the ASME Boiler and Pressure Vessel

Code.

Contrary to the above, as of October 29,1996, the licensee failed to verify the

operational readiness of certain valves whose function is required for safety in

accordance with Section XI of the ASME Boiler and Pressure Vessel Code.

Specifically, the licensee failed to perform testing which ensured the operational

readiness of manually operated dry cooling tower isolation valves used to maintain

the safety function of the ultimate heat sink during the design basis tornado event.

This is a Severity Level IV violation (Supplement 1). (50-382/9613-04)

RESPONSE

(1)

Reason for the Violation

The root cause of this violation is believed to be insufficiently explicit design-

basis tornado event documentation. The documentation was not specific

enough to readily allow the IST plan reviewers to conclude that the Dry

Cooling Tower inlet and outlet valves had a safety function and should be

included in the IST program for testing. These valves were not included in the

IST plan during initial IST plan development, during the IST design basis

document (DBD 24) review, or during the current (although not completed)

review of all ASME Class 1,2, and 3 valves.

A contributing cause for this violation was that the reviewer did not examine all

of the available design basis tornado event documentation during the current

IST plan review process. It is believed that had the reviewer examined the

calculation related to the design basis tornado event, he would have

concluded that the Dry Cooling Tower inlet and outlet valves should have

been in the IST plan.

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Attachm:nt to

W3F1-97-0002

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Page 8 of 8

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(2)

Corrective Steos That Have Been Taken and the Results Achieved

The Dry Cooling Tower manual inlet and outlet valves were successfully

tested per IST requirements on 12/7/96.

(3)

Corrective Steos Which Will Be Taken to Avoid Further Violations

1.

The Dry Cooling Tower Manual inlet and outlet valves will be included

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in the IST program.

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2.

A review of the design basis tornado event will be performed and the

design basis documents will be revised, as necessary, based on the

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results of the review.

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3.

The IST basis document will be reviewed by the appropriate design

engineering disciplines in support of the development of the IST plan

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for the second ten interval.

(4)

Date When Full Comoliance Will Be Achieved

Waterford 3 is in full compliance. Item 1 will be completed by 1/31/97, item 2

will be completed by 8/31/97 and item 3 will be completed by 12/1/97.

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