ML20133H464

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Notice of Violation from Insp on 850801-31
ML20133H464
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 10/03/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133H460 List:
References
50-313-85-22, 50-368-85-23, NUDOCS 8510170375
Download: ML20133H464 (2)


Text

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APPENDIX A NOTICE OF VIOLATION Arkansas Power & Light Company Dockets: 50-313/85-22 50-368/85-23 Arkansas Nuclear One, Units 1 & 2 Licenses: DPR-51 NPF-6 During an NRC inspection conducted during the period August 1-31, two violations of the NRC requirements were identified. The violations involved failure to perform a required surveillance and failure to maintain fire barriers functional. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985), the violations are listed below:

A. Unit 1 Technical Specification 4.20.1.b requires that the fire protection water system shall be demonstrated operable by verifying each valve in the flow path that is not sealed, is in its correct position at least once per 31 days.

Auxiliary System Operating Procedure 1104.32, " Fire Protection Systems Operation," has been established to implement this Technical Specification requirement.

Supplements IIIa and IIIc to Procedure 1104.32 provide a list of valves whose position is to be checked each month to verify system operability.

Contrary to the above, valves FS-121 and FS-122, isolation valves in the fire water supply to the Unit 1 emergency diesel generator fuel oil tank vault, were not sealed nor were the valves listed on Supplements IIIa or IIIc. Consequently, the valves were not verified to be in their correct-position each 31 days as required by Technical Specifications.

-This-is'a Severity Level IV violation (Supplement I.0) (313/8522-01).

B. Unit 2 Technical Specification 3.7.11 states, "All penetration fire barriers protecting safety-related areas shall be functional."

Contrary to the above, the NRC inspectors found fire doors 186 and 210

'not fully shut on August 14, 1985, and August 16, 1985, respectively.

This is a Severity Level IV violation (Supplement I.D)-(368/8523-01).

Pursuant the provisions of 10 CFR Part 12.201, Arkansas Power and Light Company is hereby required to submit to this Office within 30 days of the date of the letter-transmitting this Notice, a written statement or explanation in reply, 8510170375 851003 PDR ADOCK 05000313 G PDR

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including for each violation: -(1) the reason for the violation if admitted, <

(2) the corrective steps which have been taken and the results achieved, (3) "'

ithe-corrective steps which will be taken to avoid further violations, and (4)

" the date when full compliance'will be achieved. Where good cause is shown, '

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, consideration will be.given to extending the response time.

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t-Dated at'A'lington,-Texas-r

., this- Ja/ ~ day of get. , '1985 .

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