ML20132H223
| ML20132H223 | |
| Person / Time | |
|---|---|
| Site: | Columbia |
| Issue date: | 07/31/1985 |
| From: | Hutchison L, Powers C WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| NUDOCS 8510020096 | |
| Download: ML20132H223 (5) | |
Text
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4 OPERATING DATA REPORT WNP-2 01-Aug-85 1.
DOCKET: 50-397 2.
REPORTING PERIOD:
Jul-85 OUTAGE +0N-LINE HOURS 744 3.
UTILITY CONTACT:'
LEONARD HUTCHISON (509) 377-2501 EXT-2486 4.
LICENSED THERMAL POWER (MWt):
3323
~5.
NAMEPLATE RATING (GROSS MWe):
1200.1 6.
DESIGN ELECTRICAL RATING (NET MWe):
1100 7.
-MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):
1140 C.
MAXIMUM DEPENDABLE CAPACITY (NET MWe):
1095 9.
IF CHANGES OCCUR ABOVE SINCE LAST REPORT, GIVE REASONS:
=
_ = - - - - - - - - - -
- 10. POWER TO WHICH RESTRICTED, IF ANY (NET MWe):
775 MWe Net RRC Pump inoperable.
-11. REASONS FOR RESTRICTIONS, IF ANY:
MONTH YEAR CUMULATIVE
- 12. REPORT PERIOD HOURS 744 5087 5527.2
- 13. HOURS REACTOR CRITICAL 692.5 3335.7 3752.2
- 10. RX RESERVE SHTDWN HRS 0.0 1029.9 1029.9
- 15. HRS GENERATOR ON LINE 661.9 3092.8 3491.3
- 16. UNIT RESERVE SHUTDOWN HOURS 0.0 1046.9 1046.9
- 17. GROSS THERMAL ENERGY (MWH) 1189200 8021643 9235271
- 10. GROSS ELECTRICAL ENERGY (MWH) 389620 2624060 3050990 19.. NET ELECTRICAL ENERGY (MWH) 369564 2515023 2925409
- 20. UNIT SERVICE FACTOR 89.0%
60.8%
63.2%
- 21. UNIT AVAILABILITY FACTOR 89.0%
81.4%
82.1%
- 22. UNIT CAPACITY FACTOR (MDC NET) 45.4%
45.2%
48.3%
- 23. UNIT CAPACITY FACTOR (DER NET) 45.2%
44.9%
48.1%
- 24. UNIT FORCED OUTAGE RATE 10.0%
16.7%
15.9%
- 25. FORCED OUTAGE HOURS 73.9 619.1 660.8
- 23. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE,DATE, DURATION):
- _ - - -=__--- -
_=---- --------------
- 27. IF CURRENTLY BHUTDOWN ESTIMATED STARTUP DATE:
k.. N 8510020096 850731 PDR ADOCK 050 7
l[j R
AVERAGE DA3LY UNIT POWER LEVEL 50-397 DOCKET NO.
UNIT WNP-2 8/1/85 DATE COMPLETED BY L.B. Hutchison TELEPHONE (509) 377-2501 A4'f 00 JULY 1985 MONTri DAY AVERAGE DAILY POWER LEVEL-DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(Mwe. Net) 10 1
0 17 199 116 2
18 3
379 18 481 4
563 20
-492 g
601 21 490 6
O 22 288
.7 624 23 623 a
612 24 9
596 651 25 603 to 720 26 486 11 27 732 486 12 A91 13 726 29-492 34 722 20 489 15 739 31 341 16
.a.,
I INSTRUCTIONS On this form, list the average daily unit power level in MWe. Net for each dr.y in the reper:ing month.Compu:e to th nea:est whole megawatt.
)
Taese figures will be ured to plot a graph for each reporung month. Note that when r.aximum dependable :apacity used for the net electncal rating of the unit, there may be occasions when the daily average power !cvel exceeds the
- 00?*c line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explairt the apparent anomaly.
DOCKET NO.
50-397 011T !WiE WNP-2 DATE 8/1/85 lt4IT SIUTDGWNS / REDUCTIONS COMPLETED BY L.B. Hutchison flEI' ORT PERIOD JULY 19 85 PAGE 1 of 2 TELEPilotE ( 509) 377-2501 ext 2486
- month, yea'r NO.
DATE lYlf 100lls itEASON METii0D LER nut 0ER SYSlEM C(t.1PUNEllf CAUSE & CORftECTIVE ACfl0N 10 tilEVENT RECUltRENCE 85-12 7/1/85 F
29.6 A
3 85-047 HA VALVEX Reactor Scram during startup due to failure of limit switches on throttle valves #1 & #4 to reset when valves were opened.The switches were recalibrated and the plant returned to service.
'i " RFW Pump out of service due to bearing failure 85-02P 7/1/85 F 0
A 5
CB PUf1PXX B
CH PUf1PXX with resultant pump damage which limited power output to a maximum of approximately 82%.
Also, "B" RRC Pump failed on 7/3/85 due to motor CT failure and high vibration..This limited power output to. 50% ontil 7/19 when A Tech Spec change authorized increase power output on single loop operation as determined i'
by core stability which permitted approximately 70 to 72% power output.
j l
i 1-I l SuttARY l TYPE REASON METil0D SYSTEM & COMP 0 TENT F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H j
S-Sched B4 taint or Test G-Oper Error 2-Manual Scram Instructions for C-Refueling Il-Other 3-Auto Scram Preparation of-D-RcGulatory Restriction 4-Continued Data Entry Sheet E-Operator Training 5-Reduced Load Licensee Event Report
& License Examination 9-Other (LER) File (NUREG-0161)
C.
- i DOCKET. ti0.
50-397 UNIT iW:E WriP-2 j
DATE 8/1/85 UllT SIUIDOWil5 / REDUCT10t4S COMPLElED BY L.B. Hutchison REfm T PERIOD JULY 19C5 PAGE 2 of 2 TELEPil0NE (509) 377-2501 ext 2486 j
- month, year j
NO. ' DAIL lYl'E IUURS ItEAStYI METHUD LER nut 43ER SYSlut CU tPONDTI CAUSE & C010ECTIVE ACf10N 10 litEVENI ItECUf alt!i; 85-13 7/7/85 S
8.2 A
1 fi/A CB PUf1PXX Plant was shutdown because of A current transforr:e i
failure on
'B' RRC motor due to a failed i
termina tion.
Repairs were made and plant returned i to service.
However, excessive vibration preventec operating pump on 60 Hz.
i
!85-14 7/16/85 F 43.4 A
1 LATER CH VALVEXX Plant was shutdown due to excessive unidentified leakage in drywell. The leakage was identified as a feed water check valve hinae oasket.
Repairs were completed and plant returned to i
i service.
!85-15 7/18/85 F 0.8 G
9 HJ If4STRU Generator tripped during startup due to high j
f1SR level.
Upon investigation it was determined that level controller was not in proper mode.
\\
i
^
1 I
r I
l-I i
l St#f tARY l 1
i TYPE REAS0tl METil0D SYSTEM & COMP 0 TENT l
5 F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H S :S* cried B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refueling II-Other 3-Auto Scram Preparation of l
D-Regulatory Restriction 4-Continued Data Entry Sheet
{
E-Operator Training 5-Reduced Load Licensee Event Report
& License Examination 9-Other (LER) File (NUREG-0161) 7
Washington Public Power Supply System 3000GeorgeWashingtonWay P.O. Box 968 Richland, Washington 99352-0968 (509)372-5000 August 6, 1985 l
Director Office of Resource Management U. S. Nuclear Regulatory Conunission Washington, D. C.
20555
Dear Sir:
Subject:
NUCLEAR PLANT NO. 2 MONTHLY OPERATING REPORT Transmitted herewith is the Monthly Operating Report for July 1985 as required by our Technical Specifications 6.9.1.6.
Very truly yours.
Okham C. M. Powers WNP-2 Plant Manager CMP /p1 l
l I
Enclosure cc: Mr. John B. Martin - NRC, Region V Mr. A. D. Toth
- WNP-2 Site Ms. Dottie Sherman - ANI, Farmington CT f