ML20132F625

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Monthly Operating Rept for June 1985
ML20132F625
Person / Time
Site: Robinson 
Issue date: 06/30/1985
From: Morgan R, Scott A
CAROLINA POWER & LIGHT CO.
To: Taylor J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
RNPD-85-1523, NUDOCS 8507180618
Download: ML20132F625 (4)


Text

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RNPD/85-1523 W gd ?,of 3

  • CP&L Cn PI At> f I'h!U URMANCL DA1A UY6lLM PALE 1

RUN DATE 0//01/8S Ui'LR A 61NL DAIA RLI(n.'

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U N.l I N A tiL R UU l tJSUN UNlI ?

l NU I ES There are presently 222 1

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POWLR LEVEL IU Ull1CH RL" ( R I C I ED 11 A t4 Y (NEI MWL )

None

10. PEA 3UN3 FOR REGIRICIIUN IF ANY: None IHlb YR IU CUNUL NUtJ TH DAIE AifVE i1. II(IURS IN RL'i'UR 1 I NG PERIUD

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  • CP&L CO PLANT PliR F UR M At4CE DATA SYSTEM PAGE 1

-RUN DAIE O//01/05 APPLNDIX D - AVERAGE DAILY POWER LEVL't.

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HUN IIME 1.4:33:03 ROUlt430N UNIT 2 DOUKLi flu. 050-0261 cot 1PLEILD BY A.

E.

SCOTT l Et E. PHOT 4E (003)383-4524 JUNE i'705 DAY AVG. DAILY POWER LEVEL DAY AVG. DAILY PUWIR LE~/Li.

(MWE-NE!)

(NUE-ULi) 1.

/24 1/

/23 2

li Y 10

/24 3

720 iY

/24 4

'/ 23 20

/23 S

723 21 l':' O 6

64Y 22

/20 7

721 23 721 0

722 24

/21 9

720 25 720 10

/20 26

/17 11 702 2/

71 3 12 723 20 713 13 724 2V 713 14 724 30 li 2 15 6Y4 i >>

618

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050-0261 DOCKET NO.

UNIT SHUTDOWNS AND POWER REDUCTIONS,

H.

5.

Kobinson UNIT MAME u /-uz-to DATE Anita E. Scott N SY une REPORT MONTH TELEPHONE 803-383-4524 "L

o c

_] g 3

  • Y5 Licensee

,Eg

{*L Cause & Corrective No.

Date k

3=

(

2g&

Event g'ir pV Action to fI e

j gg g Report a mO Prevent Recurrence I-g d

0601 850606 F

H 4

ZZ ZZZZZZ Severe thunderstorm caused a sudden loss of system load which resulted in a turbine runback.

System load was reestablished and the unit was returned to full power.

0602 850611 F

G 4

HI ELECON In order to replace a relay on the RCS Makeup System, the breaker supplying relay power was opened. Since the breaker also supplied power to a turbine runback circuit, a turbine runback resulted. The breaker was closed removing the runback signal and the unit returned to full load. A caution tag was placed on the circuit breaker as an interim corrective action s

0603 850615 S

B 1

ZZ TURBIN Reactor power reduced to perform turbine valve test.

I 2

3 4

F: Forced Reason:

S: Scheduled A Equipment Failure (Explain).

Method:

Exhibit G. Instructions 1-Manual for Preparation of Data n

B-Maintenance of Test 2-Manual Scram.

Entry Sheets for Licensee C-Refueling 3-Automatic Scram.

Event Report (LER) File (NUREG.

mo D-Regulatory Restriction 4Gher (Explain) 0161)

E-Operator Training & Ucense Examination m

F Administrative 5

a "Sc G-Operational Error (Explain)

Exhibit I. Same Source

  • S (9/77)

IlOher(Explain) 9

/ b-CP&L Carolina Power & Light Company ROBINSON NUCLEAR PROJECT DEPARTMENT POST OFFICE BOX 790 HARTSVILLE, SOUTH CAROLINA 29550 JUL 9 115 5 Robinson File:

15505 Serial:

RNPD/85-1523 Mr. James M. Taylor, Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, D. C.

20555 ROBINSON NUCLEAR PROJECT DEPARTMENT UNIT NO. 2 DOCKET NO. 50-261 LICENSE NO. DPR-23 MONTHLY OPERATIONS REPORT

Dear Mr. Taylor:

In accordance with Technical Specifications 6.9.1.c for the H. B. Robinson Steam Electric Plant, Unit No. 2, Carolina Power & Light Company herewith submits the report of operation statistics and shutdown experience for the month of June, 1985.

Very truly yours,

/

6 R. E. M an General Manager H. B. Robinson SEG Plant AES/tk Enclosure cc:

R. A. Hartfield (2)

J. N. Grace (1)

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