ML20132D106

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Responds to NRC Re Violations Noted in Insp Repts 50-259/84-52,50-260/84-52 & 50-296/84-52.Corrective Actions: Motor Pinion Gear replaced,36 ECCS Valves inspected,EMI-18 Revised & Training Classes Conducted
ML20132D106
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 03/15/1985
From: Domer J
TENNESSEE VALLEY AUTHORITY
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18029A715 List:
References
NUDOCS 8506210481
Download: ML20132D106 (3)


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TENNESSEE VALLEY AUTHORITY CHATTANOOGA. TENNESSEE 37401 1630 Chestnut Street Tower II B5 MAR el o g : 5g March 15, 1985 U.S. Nuclear Regulatory Commission' Region II.

ATTN: Dr. J. Nelson Grace, Regional Administrator 101 Marietta Street, NW, Suite 2900' Atlanta, Georgia 30323

Dear Dr. Grace:

Enclosed is our response to R. D. Walker's February 13, 1985 letter to H. G. Parris transmitting IE Inspection Report Nos. 50-259/84-52,

-260/84-52, -296/84-52 for our Browns Ferry Nuclear Plant which appeared to have been in violation of NRC regulations. If you have any questions, please call R. E. Alsup at FTS 858-2725.

To the best of my knowledge, I declare the statements contained  ;

herein are complete and true.

Very truly yours, TENNESSEKVALLEYAUTHORITY

. -] M J. A. Domer Nuclear Engineer Enclosure oc (Enclosure):

Mr. James Taylor, Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission

  • Washington, D.C. 20555 Records Center Institute of Nuclear Power Operations 1100 Circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 I g5062-@ %s  ;

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di 3 60I h An Equal Opportunity Employer

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RESPONSE

NRC INSPECTION REPORT NOS.

50-259/84-52, 50-260/84-52, AND 50-296/84-52 ROGER D. WALKER'S LETTER TO H. G. PARRIS DATED FEBRUARY 13, 1985 Enclosure 1 Item 1 - (50-250/260/296/84-52-01) ,

The following violations were identified during an inspection conducted on December 3-6, 1984. The Severity Levels were assigned in accordance with the NRC Enforcement Policy (10 CFR Part 2, Appendix C).

10 CFR 50, Appendix B, Criterion XVI, as implemented by the -~

licensee's approved quality assurance program, requires that measures established to correct conditions adverse to quality shall assure that the cause of the condition is identified and corrective action is taken to preclude repetition.

Contrary to the above, following the identification of a problem with pinion gear orientations in 1981, the licensee failed to adequately establish procedures and controls to ensure that the Limitorque Valve

-Operator pinion gear for safety related valve 3-FCV-73-3 was properly installed following electrical maintenance on August 2,1982.

This is a Severity Level IV violation (Supplement I).

1. Admission or Denial of the Alleged Violation TVA admits the violation occurred as stated.
2. Reasons For the Violation

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The motor pinion gear on this valve was verified as installed correctly in .

1981 during inspections prompted by IE Circular 79-04. Review of -

maintenance records since that time indicates that the gear was most likely ..

reversed following electrical maintenance work on the valve motor. The governing electrical maintenance instruction (EMI-18) covers changeout of ,

the motor but does not detail pinion gear replacement. Plant procedures were deficient in that the electrical and mechanical maintenance instructions were not adequately linked together.

3 Corrective Steos Which Have Been Taken and Results Achieved The motor pinion gear was replaced with a new gear in the proper orientation. A 20 percent sample (36 valves total) of emergency core cooling system valves was inspected, and no pinion gears were found reversed.

I (Item 1 259/260/296/84-52 continued) Page 2 EMI-18.has been revised to reference the pertinent mechanical maintenance instruction (MMI-87) for pinion gear replacement. Revisions to MMI-87 have been approved to include second party verification on pinion gear ,

orientation. Also, training classes for machinists and engineers have been conducted to discuss this situation. l )

4.. Corrective Steos Which Will Be Taken to Avoid Further Violations l N .

'ir No further action is necessary.

5. Date When Full Como11ance Will Be Achieved Full compliance has been achieved.

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