:on 960830,functional Deficiency Was Noted in Setting of ECCS Throttle Valve Positions.Caused by Deficiency in Original Design Sys.Plant Mod Will Be Prepared to Resolve Pump Boost,Valve Clogging & Valve Erosion Issues| ML20129E948 |
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Millstone  |
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| Issue date: |
09/29/1996 |
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| From: |
Laudenat R NORTHEAST NUCLEAR ENERGY CO. |
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| To: |
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| Shared Package |
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| ML20129E946 |
List: |
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| References |
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| LER-96-029-02, LER-96-29-2, NUDOCS 9610010207 |
| Download: ML20129E948 (5) |
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text
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY oMB NO.3160-0104 44g53 EXPIRES 04/30/98 l yow?#?!"#1#$?o"#s!.Vr%s*"*J"ob"t"?^Rs L'ta"9o^"l4&"I "'!'an'a ToA=* iafe'Jo ^22 LICENSEE EVENT REPORT (LER) 18!T'a'=fM&fte,t4#J"st"? 'n?"!,3M"ei l?nu;?htaandi?leiL" EiW!k??ol"?nks'"*
R" (See reverse for required number of digits / characters for each block)
FACirTY NAME (1)
DOCKET NUMBER (2)
PAGE (3)
Millstone Nuclear Power Station Unit 3 05000423 1 of 5 TITLE (4)
Functional Deficiency in the Setting of the Emergency Core Cooling System Throttle Valve Positions EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACluTY NAME DOCKET NUMBER NUMBER 08 30 96 96 029 00 09 29 96 i
OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE (9) 5 20.2201(b) 20.2203(a)(2)(v) 50.73(a)(2)(i) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL (10) 000 20.2203(a)(2)(il 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv)
OTHER
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50.36(c)(1)
X Sc.i3(an2nv) 20.2203(a)(2)(iii) gc;v,. A strggelow g_
20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBFR (include Area Codel R. T. Laudenat, Nuclee.: Licerising Supervisor (8601444-5248 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE To NPRDS To NPROS i
A SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR SUBMISSION
[
YES NO
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(If yes, Complete EXPECTED SUBMISSION DATE).
ABSTRACT (Limit to 1400 spaces, i.e.. approximately 15 single-spaced typewritten lines) (16)
On August 30,1996, with the plant in Mode 5 at 0-percent power, an engineering evaluetion determined that a functional deficiency in the setting of the Emergency Core Cooling System (ECCS) throttle valve positions was a condition which alone could result in the loss of the Charging (CHS) and High Head Safety injection (SlH) safety 2
functions in the recirculation phase.
The positions of the throttle valves was established during original start-up testing to ensure adequate injection flows and prevent pump runout. This testing was conducted under injection conditions and therefore, the suction boost provided by the Containment Recirculation Spray System (RSS) pumps during recirculation was not considered in the setting of the throttle valves. Additionally, Westinghouse identified that the ECCS pump runout margin e.ssociated with the impellers used at the plant may be less than that assumed in the original system design. Coupled with the RSS pump boost, this could result in pump flow rates in excess of maximum limits during the recirculation phise, potentially leading to pump damage and inoperability. This condition was reported at 1128 on August 30, 1996, pursuant to 10CFR50.72(b)(2)(iii)(D) as a condition which alone could have prevented the CHS and SlH
)
systems from performing their safety function to mitigate the consequences of an accident.
Plant modifications will be implemented to ensure that the ECCS pumps will provide adequate injection flows and not runout during recirculation with RSS pump boost. The plant will be maintained in Mode 5 or lower until such time as the modifications have been completed.
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9610010207 960927 PDR ADOCK 05000423 S
PDR
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.U.S. NUCLEAR REGULATORY COMMISSIONl L4 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 2 of 5 96 029 00 TEKT filmore space is required, use additional copies of NRC Form 366A) (17) 1.
Descriotion of Event On August 30,1996, with the plant in Mode 5 at 0-percent power, an engineering evaluation determined that a functional deficiency in the setting of the Emergency Cnre Cooling System (ECCS) throttle valve positions was a condition which alone could result in the loss of the Charging (CHS) and High Head Safety injection (SlH) safety functions in the recirculation phase. The current ECCS throttle valve positions were established without considering the suction boost pressure of the Containment Recirculation Spray System (RSS) pumps which would be present during the recirculation phase. The throttle valve position, coupled with a reduction in ECCS pump runout margin available relative to original design conditions, would result in CHS and SlH pump flow rates in excess of maximum limits during the recirculation phase, potentially leading to pump damage and inoperability. This condison was reported at 1128 on August 30,1996, pursuant to 10CFR50.72(b)(2)(iii)(D),
es a condition which alone could have prevented the CHS and SlH safety systems from performing their safety functions to mitigate the consequences of an accident.
The licensing basis of the plant requires that the recirculation phase be sustainable for post accident long term cooling. The RSS suction boost coupled with a reduction in CHS and SlH pump runout margin could cause the CHS and SlH pumps to become inoperable early in the recirculation phase, in this condition, the ability of the pitnt to maintain sufficier.t flow during the recirculation phase would be significantly reduced such that the j
d: cay heat boil-off rate vrould rapidly exceed the heat remaval rate and thus compromise core cooling.
i 11.
Cause of Event
The cause of this event is a deficiency in the original design of the system coupled with inadequate start-up testing. The positions of the throttle valves were established during original start-up testing in accordance with Westinghouse specifications to ensure that the ECCS pumps would provide adequate injection flows and ECCS pumps would not runout. However, this testing was conducted under injection conditions and therefore, the boost from the RSS pumps which would exist during recirculation was not considered in the setting of these velve positions.
Whereas pump boost as a condition is not of itself necessarily harmful to the operation of the ECCS, it is the cumulative affect of the following conditions that results in a pump boost magnitude that makes it deleterious:
RSS pumps are used for the ECCS recirculation phase in lieu of the lower head Residual Heat Removal (RHR) pumps.
The as-built performance of each RSS pump is approximately 7 percent higher than the original design
- curve, The RSS heat exchangers have a flow limitation of 4600 gpm due to tube vibration concerns, even e
though the RSS pump maximum flow is 5100 gpm. To preclude RSS heat exchanger flows higher than 4600 gpm, direct RSS pump injection during cold leg recirculation and during hot leg recirculation was prohibited by plant procedures in 1986. While this action resolved the RSS heat exchanger flow limitation problem, it contibuted to the CHS and SlH suction boost problem.
Sand-cast type impellers are installed in the CHS and SlH pumps. Sand-cast impellers are generally more susceptible to cavitation at flows close to the specified runout flows. Based on information from Westinghouse, if an attempt is made to operate at or beyond the specified runout flow, cavitation will occur regardless of the Net Positive Suction Head Availible (NPSHA) at the suction of the pump.
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.U.S. NUCLEAR RE2ULA10.lY COMMISSION LICENSEE EVENT REPORT (LER) l l
TEXT CONTINUATION FACILITV NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE 13) f 2
YEAR SEQUENTIAL REVISION
(
j Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 3 of 5 96 029 00 i
l TEKT (If more space is required. use additionalcopies of NRC Form 366A) it 7) l I
Therefore, the specified runout flows should be treated as maximum allowable flows for ccceptable j
pump operation.
I I
The ECCS, as currently configured, is vulnerable to pump runout conditions during the recirculation phase. The 1
system is vulnerable to pump damage and ultimately system inoperability.
Ill. Analysis of Event J
This is being reported as a condition which alone could result in the loss of the CHS and SlH safety functions in ths ECCS recirculation phase, pursuant to 10CFR50.73(a)(2)(v)(D). Specifically, the setting of the ECCS branch lins throttle valves during start-up testing was not properly coupled to the RSS pump boost which would be available during the recirculation phase. The RSS pump boost available is of sufficient magnitude to result in CHS and SlH pump flow rates in excess of maximum limits, potentially leading to pump damage and eventual inoperability.
The potential for the ECCS to fail to meet the long-term cooling requirements was being investigated in response to industry reports that the throttle valves were susceptible to clogging and erosion during the recirculation phase. Initially, it was postulated that debris from containment, smaller than the sump screen 3/32" opening but larger than the clearance provided in the subject throttle valves, could become lodged in the valve passages and sufficiently reduce flow to below the minimum allowed to prevent core uncovery. It was subsequently dstermined that while the high velocities and differential pressures in the vicinity of these throttle valves would e:rve to provent blockage, the same high velocities and differential pressures would result in valve cavitation and subsequent valve seat erosion to the po:nt where eventually the throttling capacity of the valves could decrease.
This potential decrease in throttling capacity could result in ECCS pump runout and subsequent inoperability.
While irrestigating the ECCS branch line throttle valve clogging and erosion issues, it was determined that the position of these throttle valves were established during original start-up testing under injection conditions and thtrefore, did not consider RSS pump boost which would be available during recirculation. Due to the substantial magnitude of the RSS pump boost during recirculation, the current valve positions would not preclude the runout of either of the ECCS pumps at any time, independent of valve erosion, and the ECCS pumps would experience pump damage and eventualinoperability. This pump boost condition had previously bun identified in Westinghouse Letter NEU-91-611 dated October 1,1991.
Th3 Westinghom Letter also identified an issue regarding :he amount of runout margin available for the ECCS pumps manufactured by Dresser / Pacific Pumps utilized within the plant. It was previously assumed that the runout margin for the SlH and CHS pumps was 15 gpm or more beyond the specified design maximum flow rate.' The following guidelines were established in 1991 to assess the impact on the unit:
If an attempt is made to operate at or beyond the critical flow capacity of the impeller, cavitation would occur regardless of the NPSHA at the suction of the pump.
j These flow rates should be treated as maximum allowable flows for acceptable pump operation. These j
flow rates are acceptable only if the NPSHA satisfies the identified pump requirements.
For the SlH pumps, Dresser Pumps has determined that the asymptote is located beyond 675 gpm and cavitation probably occurs on the suction impeller. The original design runout flow was 670 gpm for i
SlH pump "A" and 650 gpm for SlH pump "B" as specified in Technical Specification 4.5.2.h.
I
.U.S. NUCLEAR REIULATORY COMMISSION 14-951 l
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 4 of 5 l
96 029 00 l
TEXT (11more space is required. use additionalcopies of NRC form 366A) (17)
For the CHS pumps, Dresser Pumps has determined that the asymptota is located beyond 560 gpm.
l e
The original design runout flow was 560 gpm as specified in Technical Specification 4.5.2.h.
t l
Th:refore, the design objectives for an acceptable solution to ensure that the ECCS is capable of meeting its dzsign safety function are as follows i
l 1.
Meet or exceed the minimum injection flow requirements delineated in the technical specifications during the injection phase.
l 2.
Ensure maximum pump flows are maintained below those specified in Technical Specification 4.5.2.h during recirculation with boost from the RSS pumps considered.
3.
Ensure minimum throttle valve clearances are greater than 3/32".
l 4.
Ensure maximum throttle valve velocities are below that at which significant valve erosion would occur.
l Thz colution to both the clogging and valve erosion issues is to reduce the throttling burden on the valves such j
thtt the revised valve clearances would be larger than the sump screen mesh clearance and would have l
associated fluid velocities below which significant erosion will not occur. The required reductlcn in the throttling l
burden on the valves could be accomplished through the installation of flow orifices in series w?. each throttling vilva, thus maintaining the same net ECCS hydraulic resistance and original flow balance.
l In order to address the RSS pump boost issue, the ECCS hydraulic resistance must be increased; however, it cin only be increased in such a manner that does not result in deliverable flows less than the required injection flows for core recovery delineated in the technical specifications. To this end, the additional resistance required j
for pump boost may only be partially addressed by increasing the hydraulic resistance in the branch lines beyond that required to relieve the valve throttling burden to the extent allowed by the current system flow margin in tha injection phase. The balance of the resistance must be derived from supplemental resistance only in the r circulation flow path.
l
IV. Corrective Action
A plant modification is being prepared to resolve the pump boost, valve clogging, and valve errosion issues.
Tha proposed modifications will:
l l
Install restrictive orifices in selected ECCS branch lines to relieve the throttling burden on the branch line I
throttling valves. This will permit the valves to be set in more open positions while still satisfying the minimum required deliverable flows during the injection phase.
Install restrictiva orifices in the suction supply headers to the CHS pumps from the RSS pumps to l
mitigate RSS pump boost.
l l
The plant will be maintained in Mode 5 or lower until such time as all modifications have been completed and j
l tha issues resolved.
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NRC.F6RM 366A U.S. NUCLEAR RE ULATORY COMMISSION (4 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 5 of 5 96 029 00 TEXT fif more space is required, use additional copies of NRC Form 366A) (17)
V.
Additional Information
Similar Events None Manufacturer Data Ells System Code Chemical and Volume Control System - CB High Pressure Safety injection System - BQ NAC FORM 366A (4-95)
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| 05000336/LER-1996-001, :on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program |
- on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-001-02, :on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power |
- on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-002, :on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash |
- on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000423/LER-1996-002-02, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) | | 05000423/LER-1996-002, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1996-003, :on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements |
- on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2)(viii) | | 05000336/LER-1996-003-01, :on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys |
- on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000245/LER-1996-003-02, Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-003-01, :on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised |
- on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-004-01, :on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment |
- on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1996-004, :on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented |
- on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000423/LER-1996-004-02, :on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements |
- on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-005-01, :on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability |
- on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-005-02, :on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated |
- on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(s)(2) | | 05000423/LER-1996-005-03, :on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised |
- on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-006-01, :on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established |
- on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-006-02, :on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner |
- on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000423/LER-1996-007, :on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed |
- on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-007, :on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised |
- on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised
| | | 05000423/LER-1996-007-01, :on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable |
- on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-007-02, Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000336/LER-1996-008, :on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced |
- on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced
| | | 05000423/LER-1996-008-01, :on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism |
- on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1996-009, :on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint |
- on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1996-009-01, :on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed |
- on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-009-01, :on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change |
- on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-009-02, Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-010, :on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised |
- on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised
| | | 05000423/LER-1996-010-02, :on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted |
- on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000336/LER-1996-011-01, :on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised |
- on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised
| | | 05000423/LER-1996-011-02, :on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/ |
- on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-012, :on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/ |
- on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-012-01, :on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected |
- on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1996-012-02, :on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits |
- on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000423/LER-1996-013, :on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified |
- on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000336/LER-1996-013-01, :on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply |
- on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-013-02, :on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement |
- on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000336/LER-1996-014-01, :on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3 |
- on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1996-014-02, :on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown |
- on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-015-05, Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000423/LER-1996-015-04, Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1996-015-01, :on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures |
- on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-015-02, Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-016-02, :on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches |
- on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches
| | | 05000336/LER-1996-016-01, :on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested |
- on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-017, :on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified |
- on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-017-02, :on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised |
- on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000336/LER-1996-018-01, Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1996-018, :on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced |
- on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-019-02, :on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept |
- on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) |
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