ML20129B240
| ML20129B240 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 09/30/1996 |
| From: | Samuel M, Walker R TEXAS UTILITIES CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| TXX-96482, NUDOCS 9610220371 | |
| Download: ML20129B240 (9) | |
Text
.
Log # TXX 96482
==
File # 10010.2 1
4 7
Ref. # 10CFR50.36
_=
=__
October 15, 1996 7UELECTRIC C. lance Terry Group Vice Presided U. S. Nuclear Regulatory Commission Document Control Desk Washington. DC 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NOS. 50 445 AND 50 446 MONTHLY OPERATING REPORT FOR SEPTEMBER 1996 Gentlemen-Attached is the Monthly Operating Report for September 1996, prepared and submitted pursuant to Technical Specification 6.9.1.5 contained in Appendix A to the Comanche Peak Steam Electric Station Units 1 and 2, Operating License Nos. NPF 87 and NPF 89, respectively.
Should you have any questions, please contact Jacob M. Kulangara at (817) 897 0124.
Sincerely, N.
C. L. Terry
/-
By:
M Roger"D'. Walker Regulatory Affairs Manager JMK/jmk Attachment cc:
Mr. L. J. Callan, Region IV Mr. J. I. Tapia, Region IV Mr. T. J. Polich, NRR Resident Inspectors 9610220371 960930
/
ADOCK0500g4
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DR 2.?O103 P.O. Box 1002 Glen Rose. Texas 76043
Attachment to TXX 96482 Page 1 of 8 C0HANCHE PEAK STEAM ELECTRIC STATION UNIT 1 NRC HONTHLY OPERATING REPORT DOCKET NO.:
50 445 UNIT:
CPSES 1 DATE:
10/ 7/96 COMPLETED BY:
Mark Samuel TELEPHONE:
817 697-5793 OPERATING STATUS 4
1.
REPORTING PERIOD:
SEPTEMBER 1996 GROSS HOURS IN REPORTING PER00:
720 l
2.
CURRENTLY AUTHORIZED POWER LEVEL (HWt):
3411 MAX. DEPEND. CAPACITY (HWe Net):
1150 DESIGN ELECTRICAL RATING (HWe Net):
1150
.3.
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (HWe Net):
NONE 4
j 4.
REASON FOR RESTRICTION (IF ANY):
THIS HONTH YR TO DATE CUMULATIVE 5.
NUMBER OF HOURS REACTOR WAS CRITICAL 720 6.127 44,878 6.
REACTOR RESERVE SHUTDOWN HOURS 0
0 2.604 7.
HOURS GENERATOR ON LINE 720 6.083 44,272 8.
UNIT RESERVE SHUTD0'AN HOURS 0
0 0
9.
GROSS THERHAL ENERGY GENERATED (HWH) 2,449,157 20.211.833 143,637.085
- 10. GROSS ELECTRICAL ENERGY GENERATED (HWH) 818.306 6.833,706 47.899.909
- 11. NET ELECTRICAL ENERGY GENERATED (HWH) 785.257 6.535.569 45.702.762
- 12. REACTOR SERVICE FACTOR 100.0 93.2 83.5
- 13. REACTOR AVAll>BILITY FACTOR 100.0 93.2 88.3
- 14. UNIT SERVICE FACTOR 100.0 92.5 82.3
- 15. UNIT AVAILABILITY FACTOR 100.0 92.5 82.3
- 16. UNIT CAPACITY FACTOR (USING HDC) 94.8 86.4 73.9
- 17. UNIT CAPACITY FACTOR (USING DESIGN HWe) 94.8 86.4 73.9
- 18. UNIT FORCED OUTAGE RATE 0.0 7.5 4.9
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTliS (TYPE. DATE, AND DURATION OF EACH):
Rsfueling outage (1RF05) began on October 4.1996 with an estimated duration of 44 Days.
- 20. IF SHUTDOWN AT END OF REPORTING PERIOD. ESTIMATED DATE OF STARTUP:
- 21. UNITS IN TEST STATUS (FAIOR TO COMMERCIAL OPERATION):
ACHIEVED COMMERCIAL OPERATION:
900813 ESTIMATED
4 Attachment to TXX 96482 Page 2 of 8 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.:
50 445 UNIT:
CPSES 1
DATE:
10/ 7/%
COMPLETED BY:
Mark Samuel TELEPHONE:
817 897 5793 MONTH:
SEPTEMER 1996 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe Net)
DAY (MWe Net) 1 1010 17 1092 2
1091 18 1093 3
1091 19 1093 4
1091 20 1095 5
1091 21 1097 6
1090 22 1098 7
1089 23 1097 8
1088 24 1098 9
1088 25 1101 10 1089 26 1098 11 1088 27 1100 12 1090 28 1102 13 1087 29 1102 14 1087 30 1102 15 1089 16 1092 l
i i
l 1
i Attachment to TXX 96482
. Page 3 of 8 f
SUMMARY
OF OPERATING D PERIENCE FOR THE MONTH l
I DOCKET NO.:
50 445 UNIT:
CPSES 1
DATE:
10/ 7/%
1 COMPLETED BY:
Mark Samuel TELEPHONE:
817 897 5793 MONTH:
SEPTEMBER 19%
(
DAY TIME REMARK / MODE 09/01 0000 Unit began the month at 801 power for performance of routine turbine stop and control valve testing.
1040 Unit returned to 1001 power.
d 09/30 2400 Unit ended the month at 100* power.
4 4
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Attachment to TXX-96482 Page 4 of 8 UNIT SHUTDOWNS AE POER REDUCTIONS DOCKET NO.:
50-445 UNIT:
CPSES 1
DATE:
10/ 7/%
COMPLETED BY:
Mark Samuel TELEPHONE:
817-897-5793 REPORT MONTH:
SEPTEEER 1996 l
ETHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER CORRECTIVE ACTIONS /C0194ENTS NONE 1)
REASON 2)
METHOD A:
EQUIPMENT FAILURE (EXPLAIN)
E:
OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B:
MAINT OR TEST F:
ADMINISTRATIVE 2: MANUAL SCRAM C:
REFUELING G:
OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D:
REGULATORY RESTRICTION H:
OTHER (EXPLAIN) 4: OTHER (EXPLAIN)
I t
. Attache *nt to TXX 96482 Page 5 of 8 COMANCHE PEAK STEAM ELECTRIC STATION, UNIT 2 NRC HONTHLY OPERATING REPORT DOCKET NO.:
50 446 UNIT:
CPSES 2 DATE:
10/ 7/%
COMPLETED BY:
Mark Samuel TELEPHONE:
817 897 5793 OPERATING STATUS 1.
REPORTING PERIOD:
SEPTEMBER 19%
GROSS HOURS IN REPORTING PER00.
720 2,
CURRENTLY AUTHORIZED POWER LEVEL (HWt):
3411 MAX. DEPEND. CAPACITY (HWe Net):
1150 DESIGN ELECTRICAL RATING (HWe Net):
1150 3.
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (HWe Net):
NONE j
4.
REASON FOR RESTRICTION (IF ANY):
THIS HONTH YR TO DATE CUMULATIVE 5.
NUMBER OF HOURS REACTOR WAS CRITICAL 685 4,775 22.319 i
6.
REACTOR RESERVE SHUTDOWN HOURS 0
0 2,229 7.
HOURS GENERATOR ON LINE 655 4,734 22,056 j
8.
UNIT RESERVE SHUTDOWN HOURS 0
0 0
4 9.
GROSS THERHAL ENERGY GENERATED (HWH) 2,011,807 15,401.212 70,964.123
- 10. GROSS ELECTRICAL ENERGY GENERATED (HWH) 671,025 5.188,663 23,893,284
- 11. NET ELECTRICAL ENERGY GENERATED (HWH) 638,507 4,968,005 22,826,363
- 12. REACTOR SERVICE FACTOR 95.1 72.6 80.5
- 13. REACTOR AVAILABILITY FACTOR 95.1 72.6 88.6
- 14. UNIT SERVICE FACTOR 90.9 72.0 79.6
- 15. UNIT AVAILABILITY FACTOR 90.9 72.0 79.6 i
- 16. UNIT CAPACITY FACTOR (USING HDC) 77.1 65.7 71.6
- 17. UNIT CAPACITY FACTOR (USING DESIGN HWe) 77.1 65.7 71.6
- 18. UNIT FORCED OUTAGE RATE 9.1 10.6 8.0 1
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 HONTHS (TYPE, DATE. AND DURATION OF EACH)-
l
- 20. IF SHUTDOWN AT END OF REPORTING PERIOD. ESTIMATED DATE OF STARRIP:
- 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
ACHIEVED COMMERCIAL OPERATION:
930803 ESTIMATED
)
Attachment to TXX 96482 Page 6 of 8 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.:
50 446 UNIT:
CPSES 2
DATE:
10/ 7/96 COMPLETED BY:
Mark Samuel TELEPHONE:
817 897 5793 HONTH:
SEPTEMBER 1996 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (HWe Net)
DAY (HWe Net) 1 1110 17 1105 2
1109 18 574 3
1109 19 0
4 1109 20 0
5 1108 21 175 6
1107 22 542 7
1106 23 516 8
1106 24 516 9
1105 25 516 10 1105 26 603 11 1105 27 1093 12 1105 28 1117 13 1103 29 1117 14 1104 30 1116 15 1104 16 1105
E.
4 Attachment to TXX %482 Page 7 of 8
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH 00CKET NO.:
50 446 UNIT:
CPSES 2
DATE:
10/ 7/%
COMPLETED BY:
Mark Samuel TELEPHONE:
817 897-5793 HONTH:
SEPTEMBER 1996 DAY TIME REMARX/H00E 09/01 0000 Unit started the month at 100% power.
09/18 1245 Unit tripped after a reactor coolant system instrument spike that resulted from a lightning strike. Unit entered Mode 3.
09/20 2257 Commenced reactor startup, 2351 Unit in Mode 2.
Reactor entered criticality.
09/21 0517 Unit entered Mode 1.
0608 Unit synchronized to the grid: unit began ramping up power.
09/22 0354 Unit held at 61t power due to high bearing temperature of Heater Drain Pump 2 02. Began overhaul of Heater Drain Pump 2-02.
1407 Reduced power to 56% due to Main Feedwater Pump 2 01 high bearing temperature. Power maintained at 56% to repair the bearing on the Main Feedwater Pump. Also during this time Turbine Plant Cooling Water Pump 2 02 was realigned to resolve high bearing temperature on this pump.
09/26 1650 Repairs completed on all pumps and initiated unit ramp up.
09/27 0553 Unit achieved 100% power.
09/30 2400 Unit ended the month at 100% power.
~ -.
Attachment to TXX-96482 Page 8 of 8 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.:
50-446 UNIT:
CPSES 2
DATE:
10/ 7/%
COMPLETED BY:
Mark Samuel TELEPHONE:
817-897-5793 REPORT MONTH:
SEPTE)BER 1996 METHOD OF TYPE SHUTTING DOW F: FORCED DURATION THE REACTOR OR
-NO DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER COPRECTIVE ACTIONS /COPMENTS 8
% 0918 F
65.4 H
3 Reactor tripped due to lightning strike causing reactor coolant system instrument spike.
Reference:
LER 446/%-006.
9
% 0922 F
A 4
While rasping up, held power at 611 due to Heater Drain Pump 2-02 high bearing temperature.
Reduced power level to 56% due to high bearing temperature on Main Feedwater Pump 2-01.
Continued the power ramp up after completing all the pump repairs.See previous page for additional details.
1)
REASON 2)
METHOD A:
EQUIPMENT FAILURE (EXPLAIN)
E:
OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B:
MAINT OR TEST F:
ADMINISTRATIVE 2: MANUAL SCRAM C:
REFUELING G:
OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D:
REGULATORY RESTRICTION H:
OTHER (EXPLAIN) 4: OTHER (EXPLAIN)
-