ML20128Q537
| ML20128Q537 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 05/29/1985 |
| From: | Jackiw I NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| References | |
| 50-346-85-16, IEB-83-07, IEB-83-7, NUDOCS 8506040230 | |
| Download: ML20128Q537 (10) | |
See also: IR 05000346/1985016
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U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Report No. 50-346/85016(DRP)
Docket No. 50-346
License No. NPF-3
Licensee: Toledo Edison Company
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Edison Plaza, 300 Madison Avenue
Toledo, OH 43652
' Facility Name: . Davis-Besse 1
Inspection At: Oak Harbor, OH
Inspection Conducted: April 9 through May 13, 1985
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Inspectors:
W. G. Rogers
D. C. Kosloff
B. L. Burgess
' Approved By:
. Jac iw,
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Reactc: Projects Section 2B
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Inspection Summary
Inspection on April 9 through'May 13, 1985 (Report No. 50-346/85016(DRP))
Areas Inspected: Routine, unannounced inspection by resident inspectors of
licensee action on previous inspection findings, licensee event reports, opera-
tional safety, maintenance, surveillance, IE bulletins, operational events,
meeting with licensee, action-on~ regional requests and training. The inspec-
tion involved 209 inspector-hours onsite by three NRC inspectors including 49
inspector-hours'onsite during off-shifts.
Results: Of the ten areas inspected, no items of noncompliance or deviations
were identified in nine areas and one item of noncompliance was identified in
. the area of surveillance (failure to properly implement a procedure -
paragraph 6).
8506040230 850529
PDR ' ADOCK 05000346
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DETAILS
1.
Persons Contacted
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a.
Toledo Edison Company
R.'Crouse, Vice President Nuclear, SALP Improvement Task Force
Leader-
rFT. Murray,. Nuclear Mission Assistant Vice President, Acting
-Nuclear Mission Head
S. Quennoz, Plant Manager
- W. O' Conner, Operations Superintendent
- D. Lee, Maintenance Superintendent
. C. Daft, QA Director
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+J.
Faris, Administrative Coordinator
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J. Ligenfelter, Technical Superintendent
J. Syrowski,~ Nuclear Training Analysis and Evaluation Supervisor
+R. Peters,; Licensing Manager
- S. Wideman, Senior. Licensing Specialist
J. Wood, Facility Engineering General Supervisor
- B. Geddes, Acting Operationss QA Supervisor
- B.
Beyer, Nuclear Projects Director
b.
'NRC
+W.
Shafer, Branch Chief,.DRP
+J.
Haerison, Branch Chief, DRS
+C. Weil Investigation and Compliance Specialist
4H4. . Choules ,- Reactor Inspector, ' DRS
+I.~Jackiw..Section Chief, DRP
+*D._Kosloff,' Resident. Inspector
+ Denotes those personnel. attending the May 2, 1985 meeting in the
Region III offices to discuss erroneous information provided by-
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Toledo. Edison Company personnel on April 1, 1985.
- Denotes those personnel attending the' Hay 10,-1985 exit interview.
The inspectors also interviewe.d other licenses employees, including mem-
-bers of_the technical, operations, maintenance, I&C, training and health
physics staff.
- 2.
Licensee Action on Previous Inspection Findings
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(Closed)-Open Item (346/85004-14) Establishment of a Maintenance Training
. Supervisor .' A Maintenance Training Supervisor was appointed on March 1,
1985.
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(Open) Open Item (346/85004-07) Channel separation between Safety Features
Actuation system channels. On March 21, 1985,-NRR requested additional
information to determine the adequacy of the channel interconnections.
This item remains open.
(0 pen) Open Item (346/84004-05) Eddy current inspection of the No.1 steam
generator. The licensee provided the inspector with the results of the
special sample inspection of the #1 steam generator. The report has been
forwarded to the regional office for review and evaluation. Closure of
this item is dependent on that review.
No items of noncompliance or deviations were' identified.
3.
' Licensee Event Reports Followup
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Through direct observations, discussions with licensee personnel, and
review of_ records,.the following event reports were reviewed to determine
that reportability requirements were fulfilled, immediate corrective action
was accomplished, and corrective action to prevent recurrence had been
accomplished in accordance with technical specifications.
(Open) LER 85-005, Reactor Trip from 28 Percent Power'.
This LER will
remain open pending review of the licensee's change to the Plant Shutdown
Procedure, PP 1102.10 and the licensee's evaluation of the component fail-
ure that caused the trip.
(0 pen) LER 85-006, Failure of Control Rod Drive E-3 to Meet Trip Time.
This LER will remain open pending review of the corrective action included
in the scheduled revision to the LER.
(Open) LER 85-007, Auxiliary Feed-Pump Turbine Response Time 'roblems.
This LER will remain open pending review of the corrective action included
in the scheduled revision to the LER.
No items of noncompliance or deviations were identified.
4.
Operational Safety Verification
The inspector observed control room operations, reviewed applicable logs
and conducted discussions with control room operators during the months
of April and May. The inspector verified the operability of selected
emergency systems, reviewed tagout records and verified proper return to
servic9 of affected components. Tours of the auxiliary and turbine
buildings were conducted to observe plant equipment conditions, including
potential fire hazards, fluid leaks, and excessive vibrations and to
verify that maintenance requests had been initiated for equipment in need
of maintenance. The inspector by observation and direct interview
verified that tha physical security plan was being implemented in
accordance with the station security plan.
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The inspector observed plant housekeepiag/ cleanliness conditions and
verified implementation of radiation protection controls. During the
months of April and May, the inspector walked down the accessible portions
of the station battery and DC electrical distribution systems to verify
operability.
These reviews and observations were conducted to verify that facility
operations were in conformance with the requirements established under
' technical specifications, 10 CFR, and administrative procedures.
While reviewing the Unit Log on Apr31 3, 1985 the inspector noted that
the security and fire protection computer had been shut down for main-
tenance at 0915 and that the required fire watch patrols had not been
established until 1120. Technical Specification Limiting Condition for
Operation 3.3.3.8 requires specific fire detection instrumentation be
operable. Shutdown of the security and fire protection computer renders
'that instrumentation inoperable. -Technical Specification Action Statement
3.3.3.8 a. requires that fire watch patrols be established within one hour
to inspect the zones with inoperable instruments. The time limit estab-
lished by the action statement was exceeded by one hour and five minutes.
A discussion of the occurrence with the Shift Supervisor revealed that
although he had been informed that the security and fire protection com-
puter was to bc shutdown for maintenance that morning he was not notified
at the time the computer was actually shut down. He established the fire
watch patrols in accordance with existing plant procedures after his
independent discovery that the computer had been shut down. This item is
unresolved (346/85016-01) pending further review.
While touring the Startup Feedwater Pump / Auxiliary Feeduater Pump (SUFP/
AFWP) area on April 24, 1985 at approximately 1210 the inspector observed
that the only other person in the room was a sleeping unlicensed operator.
At this time the plant was in Mode 3 and the SUFP was in operation.
Paragraph 2.C.(3)(t) of Facility Operating License Number NPF-3 requires
that Toledo Edison station an operator in the SUFP/AFk'P area during opera-
tion of the SUFP to monitor SUFP and Turbine Plant Cooling Water (TPCW)
piping status in the AFWP Rooms.
In the event of SUFP/TPCW pipe leakage,
- the c perator is required to trip the SUFP locally or notify the Control
Room to trip the SUFP, and isolate the SUFP/TPCW piping. Another Toledo
Edison employee entered the area and the operator was awakened in the
presence of the inspector at approximately 1212. The inspector notified
the appropriate Toledo Edison supervisory personnel of the occurrence.
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The operator was relieved and disciplinary action was taken. This item
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is unresolved (346/85016-02) pending further review.
No items of noncompliance or deviation were identified.
5.
Monthly Maintenance Observation
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Station maintenance activities of safety related systems and components
listed below were observed / reviewed to ascertain that they were conducted
in accordance with approved procedures, regulatory guides and industry
codes or standards and in conformance with technical specifications.
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The following items were considered during this review:
the limiting
conditions for operation were met while components or systems were
removed'from_ service; approvals were obtained prior to initiating'the'
~ work; activities were. accomplished using approved procedures and.were
inspected as' applicable; functional testing and/or calibrations were
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performed prior.to returning components or systems to service; quality
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control records were maintained; activities were accomplished by qualified
personnel; parts and materials used were properly certified; radiological
controis were implemented; and, fire prevention controls were' implemented.
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Work requests were reviewed to determine status of outstanding jobs and
to' assure that priority is assigned to safety-related equipment mainte-
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nance which may affect _ system performance.
~The~following maintenance activities were observed / reviewed:
~ Installation of a_ fire wall.and fire doors in the auxiliary building
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Emergency diesel generator preventive maintenance
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Following-completion of maintenance on the-emergency diesel generator, the
inspector verified.that the system had been returned to service properly.
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No items of noncompliance or deviations were identified.
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Monthly. Surveillance Observation
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LThe inspector observed technical specifications required surveillance
testing _on the Control-Rod Drive System, ST.5013.02, Control Rod Assembly
Insertion Time Test, and verified that testing was performed in accordance
with adequate procedures, that test instrumentation was calibrated, that
limiting conditions for operation were met,-that removal and restoration
of the- affected components were accomplished, -that test results conformed
~ with technical specifications and procedure requirements and were reviewed
.by personnel'other than the individua1Ldirecting_the test, and that any
deficiencies identified during the testing were properly reviewed and
resolved by appropriate management personnel. While reviewing the test
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results the inspector noted minor errors in the' calculation of rod inser-
tion time. The inspector then reviewed the same calculations in the
record of the previous test.
Similar errors were noted. The inspector-
discussed these errors with the licensee and verified that.the errors did
not affect the results of the test'.
The inspectors also witnessed portions of the following test activities:
ST 5013.03
Control Rod Program Verification
ST 5030.02
Reactor Protection System Functional Test
ST 5081.01
Diesel Generator Monthly Test
ST 5031.14
Steam and Feedwater Rupture Control System
Monthly Test-
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While reviewing the results of the control rod program verification, the
inspector noted that there was no Test Deficiency List attached. Admin-
istrative Procedure AD 1838.02, Performance of Surveillance and Periodic
Tests, requires that a brief summary of any malfunctions be noted on a
Test Deficiency List and that the list be attached to the completed test.
Since several malfunctions had occurred during conduct of the test,
preparation and attachment of a Test Deficiency List was required. The
control rod program verification also requires that the reactor coolant
system (RCS) boron concentration be determined at least once per two hours
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during the verification of the rod program by control rod movement. The
test data sheet (enclosure 12 of ST 5013.03) shows that RCS boron concen-
tration was not verified within the time required on two occasions and the
test data sheet does not include any record of RCS boron concentration
verification during other times when the rod program was being verified by
control rod movement. The failure to prepare a Test Deficiency List and
the inadequate verification of RCS boron concentration are' considered
examples of an item of noncompliance for failure to properly implement
procedures (346/85016-03).
No other items of noncompliance or deviations were identified.
7.
IE Bulletin Followup
For the IE Bulletin listed below, the inspector verified that the written
response was within the time period stated in the bulletin, that the
written response included the information required to be reported, that
the written response included adequate corrective action commitments based
on information presented in the bulletin and the licensee'.s response, that
licensee management forwarded copies of the written response to the appro-
priate onsite' management representatives, that information discussed in
the licensee's written response was accurate, and that corrective action
taken by the licensee was as described in the written response.
IEB 83-07, Fraudulent Material Supplied by Ray Miller, Inc.
U.S. Steel
stated that no Ray Miller material was supplied from U.S. Steel.to Toledo
Edison.
Reynolds Aluminum stated that they were unable to determine if
any material from Ray Miller was supplied from Reynolds Aluminum to Toledo
Edison. The licensee researched the material supplied from Reynolds
Aluminum to Toledo Edison and determined that none of the material was for
safety-related application. This bulletin is considered closed.
No items of noncompliance or deviation were identified.
8.
Followup on Operational Event-
On April 17 and May 13, 1985, the licensee observed evidence of water
hammer in the auxiliary feedwater steam supply lines. This water hammer
problem is the subject of Inspection Report 85013 and was also addressed
in a Confirmatory Action Letter on April 26, 1985.
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<0n April 30 and May-1, 1985, the licensee experienced Level 1 Safety
Features'Actuations due to spurious trips of the' Channel 4 containment
radiation monitor.
In each case, a single channel containment radiation
monitor trip was sufficient to cause a Level 1 actuation because the
Channel:1 'contsinment radiation monitor had been declared inoperable and
placed in_the tripped condition on April 30, 1985. All. systems responded-
as expected during each actuation except for one Emergency Core Cooling
System-Room Ventilation Damper (RV 5716). After the April 30 actuation,
NV-5716 was manually-closed and power to it was removed. All other-
affected equipment was restored to normal ~following identification of the
cause of each actuation.
On May 5, 1985, the licensee declared an unusual event when the meteoro-
. logical tower lost electrical power. The normal power supply was lost
when-a breaker tripped due to a ground. The meteorological tower auto-
- matic transfer switch did not-automatically transfer to the backup power-
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- supply. 1The unusual event was terminated approximately one hour later
-when_the transfer switch was: manually transferred to the alternate power
- supply._ The~ ground was eliminated from the normal power supply and the.
normal _ feeder was energized. When the alternate power supp1v was deener-
gized the _ automatic transfer switch performed its function and ttwnsferred
automatically to the normal power supply.
Following the plant trip on April 24, 1985 the inspector ascertained the
~ status of the reactor and safety systems by observation of control room
indicators and discussions with licensee personnel concerning plant
parameters, emergency' system status and reactor coolant chemistry.
The
inspector verified the establishment- of proper communications and reviewed
the corrective actions taken by the licensee.
All systems responded as expected, except for aut unexplained steam genera-
-tor;10w level trip on one channel of-the Steam and Feedwater Rupture
- Control System and an unexplained trip of one. Main Feedwater Pump. The
trip was caused by overly conservative flux-to-flow setpoints'in the
flux / delta flux / flow module of the Reactor Protection System (RPS), an -
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overly conservative calibration of the flux inputs to the RPS and fluctua-
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tions in the reactor coolant flow input _to the RPS. The details of this
trip are discussed in Inspection Report 85009. -After determining the
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cause of the trip the plant was returned to operation on April 25.
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licensee.is restricting reactor power to 90% until the optimum setpoints
for the flux / delta. flux / flow trip are determined.
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'No items of noncompliance or deviations were identified.
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9.
-Meeting with Licensee
On May 2, the NRC met with the licensee in the Region III offices to dis-
cuss an. apparent miscommunication between_the NRC and licensee personnel
on April 1, 1985. On April 1, licensee personnel told the NRC that the
Control Rod Drive Mechanism leadscrew nut assembly leaf springs had been
exercised. The inspector later determined that the exercising had 'not
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been done. On May 2 the licensee presented the results of their investi-
gation of the false statement and their corrective actions. The informa-
tion presented showed that the miscommunication was the unintentional
result of the licensee's poor internal communications. The corrective
actions taken'by the licensee appear to be sufficient to prevent future
communications failures. This item is considered closed.
.No items of noncompliance or deviations were identified.
10. Regions! hequests
Due to problems experienced at other licensed facilities, the region
requested verification that:
a.
Directives or procedures exist that clearly define "at the controls"
for a reactor or senior reactor operator.
b.
Directivesaor procedures exist implementing the requirement for an
operator or senior operator to be present in the control room at
all times.
The inspector reviewed Administrative Procedure AD 1839.00, Station
Operations, and determined that sections 5.1.1 and 5.1.2 along with the
sketch of enclosure II of the procedure provide adequate direction with
regard to a. and b. above.
Due to a problem experienced at the Byron Nuclear Power Station, the
region requested the inspector determine the:
a.
Installed configuration of the main steam isolation valves (MSIV).
b.
MSIVs' manufacturer.
c.
Methodology utilized by the licensee to demonstrate the operability
of the MSIVs.
This information was compiled and provided to regional management on
April 17, 1985. While compiling the information on the MSIVs (MS100 and
MS101), the inspector discovered an apparent deficiency in the integrated
Steam and Feedwater Rupture Control System (SFRCS) Test, ST5031.18. The
test 'only verifies operability of part of the solenoids and associated
air-system for actuation Channel 1 to MS101 and for actuation Channel 2
to MS100. This item will remain unresolved (346/85016-04) pending review
by NRR.
Due to a seismic qualification problem identified by Commonwealth Edison
Company, regional management requested the inspector to inspect all safety-
related batteries and:
a.
Determine whether the licensee received any notification of this prob-
lem from GNB Batteries, Inc. (GNB).
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b.
If the licensee did receive notification, determine what action was
taken to resolve this issue.
c.
Measure and ensure that the end gap on each end of a rack is between
1/8" to 1/4" maximum.
d.
Measure and ensure that the distance between the rack side stringers
and the battery cells is no greater than 1/4".
The inspector determined that the licensee did not receive any notification
of this problem from GNB. However, they were made aware of the problem
during an inspection by the NRC Vendor Programs Branch. At the time the
inspector inspected the batteries, the licensee had modified their battery
racks in acco~ dance with directions they had received after initiating con-
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tact with GNB. The end gaps on each rack are now all less than 1/4" and
the distance between all rack side stringers and the battery cells is no
greater than 1/4".
Regional management requested that the inspector verify that the safety
evaluation for IEB 80-06, Engineered Safety Features Reset Controls, was
consistent with the licensee's submittal on'the bulletin. The inspector
reviewed the safety evaluation and the licensee's responses to the
bulletin and determined that they were consistent.
No items of noncompliance or deviations were identified.
11.
Training
The inspector conducted a followup inspection of the training department
with respect to the Performance Appraisal Section (PAS) findings and items
previously identified in Inspection Reports 50-346/84019 and 50-346/85004.
The inspection included a review of training department.and administrative
procedures and interviews with members of the training and maintenance
departments. Of the seven items reviewed, two were ready for closure.
One item is documented in paragraph 2 of this report and the other item
was addressed as follows:
Report 50-346/84-19, Non-Operator Training Observation 1.c.(2) (Closed)
Maintenance personnel were trained on material handling and storage
requirements for nuclear safety-related material in accordance with
Administrative Procedure AD 1847.00, Station Materials Control. The
training was conducted in conjunction with other procedures during
February and March of 1985. Also, job task analyses were completed to
-determine specific training requirements for maintenance personnel.
No items of noncompliance or deviations were identified.
12.
Unresolved Items
Unresolved items are matters about which more information is required in
order to ascertain whether they are acceptable items, items of noncompli-
ance, or deviations. Unresolved items disclosed during the inspection are
discussed in paragraphs 4 and 6.
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13.
Exit Interview
The inspector: met with licensee representatives (denoted in Paragraph 1)
throughout the month and at the conclusion of the inspection on May-10,
1985, and summarized ~the scope and-findings of the inspection activities.
The licensee acknowledged the findings. After discussions with the
licensee, the inspectors have-determined there is no proprietary data
contained in this inspection report.
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