ML20128L361

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Insp Rept 50-298/96-19 on 960728-0907.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20128L361
Person / Time
Site: Cooper Entergy icon.png
Issue date: 10/07/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20128L329 List:
References
50-298-96-19, NUDOCS 9610150033
Download: ML20128L361 (20)


See also: IR 05000298/1996019

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ENCLOSURE 2

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U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

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Docket No.

50-298

License No.-

DPR-46

Report No.:

50-298/96-19

Licensee:

Nebraska Public Power District

Facility:

Cooper Nuclear Station

Location:

P.O. Box 98

Brownville, Nebraska

Dates:

July 28 through September 7,1996

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Inspectors:

Mary Miller, Senior Resident inspector

Chris Skinner, Resident inspector

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Ray Azua, Reactor Inspector, Region IV

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Approved By:

Elmo Collins, Chief, Project Branch C

Division of Reactor Projects

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ATTACHMENT:

Supplemental Information

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9610150033 961007

PDR

ADOCK 05000298

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EXECUTIVE SUMMARY

Cooper Nuclear Station

NRC Inspection Report 50-298/96-19

This routine, announced inspection included aspects ,f licensee operations, engineering,

modifications and testing, maintenance, plant suppon. and Updated Safety Analysis

Report. The report covers a 6 week period of residen 1spections.

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Operations

Routine operations were generally professional and well controlled. Operators

questioned risk assessment by maintenance planning, and generally maintained

strong ownership and support of the plant. Control room response to a reactor

water cleanup pump trip was strong.

Operators demonstrated a strong questioning attitude regarding plant activities.

Operators identified that a work package from maintenance for replacement of a

primary containment boundary valve did not have the correct postmaintenance test.

Also, operators identified that interim instructions provided to address a fire were

technically incorrect and may have needed approval by the station operations

review committee. One noteworthy exception was that operations did not identify

the need for an operability assessment for installation of an unqualified relay and

housing in 4160V vital bus undervoltage circuitry. The effect of this relay on the

operability of plant systems was not fully understood until questioned by the

inspector.

Maintenance

Maintenance activities were performed in a generally effective manner.

Inspectors identified two examples of violations, one associated with the high

pressure core injection turbine stop valve and one associated with the diesel

generators, in which the test equipment was not removed prior to declaring the

equipment operable.

During replacement of the emergency transformer undervoltage relay, the inspectors

identified a violation in that maintenance activities resulted in jumper installation on

operable Vital Bus F undervoltage circuitry without an evaluation or operability

assessment.

Inspectors found that some minor performance weaknesses associated with

preventive maintenance would not have been addressed by the Phase ill preventive

maintenance improvement.

Initial corrective actions to address a maintenance work package which did not

contain proper postmaintenance testing were weak. After inspector questioning,

additional actions were initiated.

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Inspectors found that technical support for electrical maintenance was weak in that

incomplete evaluations were performed. These resulted in the impact of

maintenance activities on operability not being fully understood.

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Engineering was proactive in identifying issues and was effectively addressing them

from a safety perspective. Also, the licensee continued to identify and address

discrepancies between USAR descriptions and the plant.

Plant Support

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Initiallicensee review of a switch found out of position was incomplete in that

security reporting and investigation were not conside,ed until questioned by the

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inspectors. Subsequent corrective actions were strong.

Technical Support Center and Emergency Operations Facility ventilation and

electrical boundaries appeared appropriate.

The response by health physics to the reactor cleanup pump trip and coupling leak

was good.

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Report Details

I. Operations

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Conduct of Operations

01.1 General Comments (71707)

Inspectors observed that routine operations were generally professional and well

controlled. Shift turnovers were thorough and addressed relevant plant conditions.

Operators questioned risk assessment by maintenance planning and generally

maintained strong ownership and support of the plant.

01.2 Reactor Water Cleanuo Isolation

a.

Inspection Scope (71707)

The inspectors rewewed control room response to a reactor water cleanup pump

trip. Inspectors also reviewed applicable procedures, logs, and drawings related to

the reactor water cleanup pump trip and interviewed the control room operators,

b.

Observations and Findinas

On August 22,1996, the control room operators responded to a reactor water

cleanup pump trip. During the event, the control room supervisor implemented the

following procedures: Procedure 5.8, " Emergency Operating Procedures," Flow

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Chart 5A (high temperature in the Reactor Water Cleanup Pump Room A),

Procedure 2.4.2.5.1," Reactor Water Cleanup System Failure," due to the filter

demineralizer and pump trip, and Procedure 2.4.2.1.2,"Small Leak Outside Primary

Containment." The licensee investigated the potential for a mechanical seal leak, a

bonnet leak on the discharge valve, and a leak on the discharge piping. Operators

determined that the pump mechanical seal had f ailed. Within 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, operations

had backwashed and precoated the filter demineralizers and had Pump B in service.

The inspectors found that operators wrote problem identification reports to

document the event in accordance with the corrective action program. The

inspectors developed a time line from observations, interviews with the operators,

review of control room logs, and the alarm printout and found no discrepancies.

c.

Conclusion

The operator's response to the reactor water cleanup pump trip was appropriate and

the event was documented accurately.

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04

Operator Knowledge and Performance

04.1 4160V Bus F Undervoltaae Circuitry Maintenance

a.

Inspection Scope (71707)

On September 5,1996, at approximately 7 a.m., the inspector observed the

replacement of Relay EE-REL-(27-ET3), the Division I emergency transformer second

level undervoltage relay.

b.

Observations and Findinas

The relay functions as a permissive to allow the emergency transformer breaker to

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close to supply electrical power to the 4160V vital bus if sufficient voltage is

available from the emergency transformer. The inspector found that operations had

entered the Technical Specification action statement associated with the emergency

transformer power supply to vital Bus F.

The licensee identified that the replacement relay supplier was not certified for

essential equipment. The licensee decided to release the relay from the warehouse

in a hold status and install the relay while they completed determining the

qualification status of the supplier. Problem Identification Report 2-03758 was

initiated to document the qualification status of the relay, and the relay and housing

were then installed.

The inspectors found that the review to evaluate the effect of the installation of the

unqualified relay and housing on operability had not considered the dc power to the

relay. Problem Identification Report 2 00861 was written to address the lack of an

evaluation of the dc relay power circuit, and to determine the operability of the DC

power circuit loop, during relay replacement. The relay replacement had been

completed at about 7:15 a.m. on September 6. The inspector identified the concern

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about 10:30 a.m. The licensee informed the control room of the potential

operability concern about 2 p.m., and started a 24-hour period for preparation of an

operability assessment. The relay qualification was completed within the following

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The assessment addressed the time for which the action statement had

not been entered and concluded that the relay and housing were operable.

Technical Specification 1.0.J applies for inoperable second level undervoltage

protection function for a vital 4160V bus and is a 6-hour shutdown action

statement.

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting

quality shall be prescribed by documented instructions or procedures, of a type

appropriate to the circumstances, and shall be accomplished in accordance with

these instructions or procedures. Procedure 0.5, " Problem identification and

Resolution," Revision 8, Step 4.4.3, states, in part, that an operability assessment

is required for conditions which could potentially affect the operability of structures,

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systems, and components. The f ailure to perform an operability assessment to

address Prob lem identification Report 2-03758 regarding the installation of the

unqualified relay and housing is a violation (298/96019-01).

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c.

Conclusions

The inspector identified that no operability evaluation had been performed to

address the installation of an unqualified relay and housing in the operable 4160V

Vital Bus F undervoltage protection circuit. The effect of this relay on the

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operability of plant systems was not fully understood. This is a violation. The

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subsequent evaluation found that the relay and housing were operable.

04.2 Appendix R instructions

8nspection Scope (71707)

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The inspector assessed the control room actions associated with compensatory

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nstructions to cope with a fire.

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b.

Observations and Findinas

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On August 20,1996, the inspector reviewed the instructions provided to the

control room by engineering concerning recently identified Appendix R circuit

vulnerabilities. The control room supervision had returned the instructions to

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engineering since the instructions were not technically complete and did not

properly address overriding interlocked cabinet doors. The control room also did not

accept the information from engineering because it involved multiple step

instructions, which had not been approved by the Station Operations Review

Committee. Further discussion with engineering resulted in more appropriate

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guidance being pro.ided to the control room.

c.

Conclusions

Control room personnel show a good questioning attitude and high standards by

refusing to accept incomplete instructions.

04.3 Postmaintenance Test for Primary Containment Valve

a.

Inspection Scope (71707)

The inspector assessed the actions of control room personnel associated with a

maintenance work package.

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b.

Observations and Findings

While reviewing a maintenance work package to replace a primary containinent

valve, the control room shif t supervisoi identified that the package did not include

the proper postmaintenance testing requirement of 58 psi. The supervisor returned

the package to maintenance and initiated a problem identification report to

document the problem. The work to replace the valve was postponed to an outage.

No primary containment boundary work was actually accomplished using the work

package. The corrective actions for the problem identification report are discussed

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Conclusions

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Control rocm personnel demonstrated a strong awareness of primary containment

testing requirements.

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04.4 River Level Measurements

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a.

Inspection Scope (71707)

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The inspector reviewed logs and the emergency procedure associated with high

river level,

b.

Observations and Findinas

On August 12,1996, while in the flood emergency procedure, the inspector noted a

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logged early morning river level of 889 feet,6 inches. About 10 a.m., the inspector

was informed by the shif t supervisor that the river level was 888 feet, 2 inches.

The inspector questioned the validity of the measurements, based on the drop of

over a foot in a fe a hours. The control room staff identified that river level was

taken from variour bays without clear procedural controls.

The licensee stated that the safety significance of the discrepancy was minimal

since the major procedure response steps such as a plant shutdown occur at river

levels above the tops of the bays and the level could be measured on the sides of

buildings as occurred during 1993. At the end of the inspection period, the licensee

was evaluating whether other plant parameters were not measured in a consistent

manner. None had been identified,

c.

Conclusions

The lack of consistent measurement of river level was considered a weakness. The

licensee response to this issue was appropriate.

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Quality Assurance in Operations

07.1 Safety Review and Assessment Board (SRABJ

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Inspection Scope (71707)

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The inspector observed the SRAB meeting conducted in July 1996.

b.

Observations and Findinas

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The inspector observed that the focus of SRAB activities involved efforts beyond a

compliance-based perspective. Items addressed included 10 CFR Part 50,

Appendix R, activities, quality assurance and line organization relationships, possible

precursor events,10 CFR 50.59 program vulnerabilities,10 CFR Part 50

Criterion XVI problem identification activities, SRAB involvement in evaluating plant

processes, SRAB member observations of crew chiefs and maintenance

management involvement in plant activities, and SRAB member observations during

a procedure compliance standdown.

c.

Conclusions

SRAB deliberations were generally safety-focused.

II. Maintenance

M1

Conduct of Maintenance

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M 1.1 General Comments

a.

Inspection Scope (62706 and 61726)

The inspectors observed all or portions of the followinc, work activities:

Procedure

Title

MWP 96-1398

Relay Replacement and Calibration

6.1 ADS.304

ADS Water Level

6.1 RPS.307

Calibration and Functional (Division 1)

MWP 96-1362

Reactor Building Ventilation Flow Monitor

Maintenance

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MP 96-112

Appendix R Modification to Diesel Generator 2

circuitry

MP 96-113

Appendix R Modification to RCIC Safe Shutdown

Circuitry

MWR 96-1374

Torque nut on High Pressure Coolant injection

Stop Valve, HPCI-HO-HOV10, Coupling

(Maintenance Procedure 7.2.71).

SP 6.HPCI.103

HPCI IST and Quarterly Test Mode Surveillance

Operation

MWR 96-1398

Troubleshooting and Replacement of EE-REL-(27-

ET3), Emergency Transformer Undervoltage

Relay

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b.

Findinas and Observations

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Inspectors observed that procedures were followed and activities were properly

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controlled. Staff knowledge and performance were good with exceptions noted

later in this report,

c.

Conclusion

Maintenance activities were performed in a generally effective manner.

M1.2 4160V Undervoltaae Circuit Relav Replacement

Inspect on Scope (62707)

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a.

On September 5,1996, at approximately 7 a.m., the inspector observed the

replacement of Relay EE-REL-(27-ET3), the Division i emergency transformer second

level undervoltage relay,

b.

Observations and Findinas

Work Package 96-1398 included procedures for relay replacement, calibration, and

instructions to identify and install electrical jumpers to provide continuity on the

relay circuits as needed. Jumpers were needed to provide power to the

downstream relays in the de circuit and were installed using a jumper control log.

The inspector questioned the potential effects of the jumpers on other components

in the circuit, since, based on review of the drawings, several additional relays

appeared to be affected. Section 04.1 discusses that the effects of the unqualified

relay and housing were not properly considered.

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The licensee confirmed that additional relays were affected by the installed jumpers.

These relays included the Bus F Second Level Undervoltage Relays (27-1F2 and A2)

and the load shed lockout relay and timers for the 4160V bus undervoltage

essential functions. Failure of this circuit due to a blown fuse could prevent the

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second level undervoltage relay function from actuating on the Division 14160V

bus.

At the end of the inspection period, the licensee had not determined the effects of

the jumper installation on operability. Problem identification Report 2-00861,

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written to address the lack of an evaluation of the dc relay power circuit and to

determine the operability of the dc power circuit loop during relay replacement, will

track the licensee's evaluation of the impact of the jumpers. The jumpers were only

installed for about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. They were removed after relay installation, at about

7:15 a.m. on September 6.

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10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting

quality shall be prescribed by documented instructions or procedures, of a type

appropriate to the circumstances, and shall be accomplished in accordance with

these instructions or procedures. Procedure 7.3.16, Revision 8, " Replacement of

Low Voltage Relays," Step 6.1, directed engineering, with operations, to evaluate

jumpers required to perform the replacement and to determine the extent of circuits

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affected. This evaluation was not performed appropriately. Jumpers were installed

in essential undervoltage relay circuity with neither an operability evaluation nor

entry into appropriate Limiting Condition For Operations. The installation of jumpers

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to f acilitate replacement of a relay and its associated huusing, without fully

researching and evaluating potential interactions with respect to operability, is a

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violation (298/96019-01).

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Conclusion

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The inspector identified that procedures had not been followed when jumpers were

installed on operable 4160V Vital Bus F undervoltage protection circuitry without

proper evaluation. This is a violation.

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M1.3 Hinh Pressure Core Iniection (HPCI) Svstem Test Eauioment

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Inspection Scope (61726)

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On August 27,1996, inspectors observed performance of Surveillance

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Procedure 6.HPCI.103, "HPCI IST and Quarterly Test Mode Surveillance Operation,"

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Revision 2, and followed up on the completion of the surveillance test. Discussions

were held with maintenance workers, system engineers, control room operators,

and supervisors.

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b.

Observations and Findinas

At 6:15 a.m. on August 28,1996, while touring the control room, the inspectors

found that the surveillance test procedure was still open. The inspectors also found

from the shif t supervisor's log that the HPCI system had been declared operable

following the completion of the surveillance test. Licensee personnel stated that, on

August 27, during the restoration section of the procedure, an operator identified a

step reference number error in Step 9.2. This step directed the removal of a lanyard

potentiometer from the stop valve. The shift supervisor was informed of the

procedural error and put the procedure on hold until the error could be corrected.

Step 9.2 was not completed. The shift supervisor subsequently reviewed the

results of the surveillance test and declared the high pressure coolant injection

system operable at 4 p.m. on August 27 with the lanyard potentiometer installed.

Discussions with the shift supervisor indicated that no evaluation had been

performed which demonstrated that the system was operable with the lanyard

potentiometer installed. The inspectors found that the system engineer had not

been informed and was not aware of these activities. The test equipment had been

installed for 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> on the system without an evaluation of the affect on

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operability.

10 CFR Part 50, Appendix B, Criterion V, requires that activities affecting quality

shall be prescribed by documented instructions or procedures, of a type appropriate

to the circumstances, and shall be accomplished in accordance with these

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instructions or procedures. Surveillance Procedure 6.HPCl.103, "HPCI IST and

Quarterly Test Mode Surveillance Operation," Revision 2, Step 9.2, specified to

remove the lanyard potentiometer. The f ailure to remove the potentiometer prior to

declaring the high pressure coolant injection system operable is an example of a

violation of 10 CFR Part 50, Appendix B, Criterion V (298/96019-02).

The procedural error was corrected on August 28, when the test equipment was

removed and the surveillance procedure was completed at 8 a.m. Engineering

subsequently determined that the stop valve had been operable with the lanyard

potentiometer attached.

c.

Conclusion

The inspectors identified that procedures were not followed when test equipment

was not removed with the high pressure coolant injection system considered

operable. This is a violation.

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M1.4 Diesel Generator Test Eauipment

a.

Inspection Scope (62707)

On August 28,1996, the inspectors monitored portions of the maintenance activity

performed on Diesel Generator 2. On August 29, the inspectors performed a

postmaintenance walkdown.

b.

Observations and Findinas

During the post maintenance walkdown, the inspectors identified that a motion

encoder, bracket, and extension piece used with surveillance test equipment were

lef t installed on the diesel generator from the testing the day before. The shift

supervisor indicated that removal or installation of test equipment in advance of

and/or after the allowed outage time for the performance of a surveillance test was

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a common practice. System engineers also indicated this was common. The

inspectors found that the 10 CFR 50.59 safety evaluation performed for

Procedure 7.2.53.7, " Operation of Engine Analysis Equiupment," Revision 0.2,

stated that the test equipment should only be installed within the allowed outage

time or when the diesel generator was inoperable. These requirements were not

incorporated into the procedure and allowed the emergency diesel generators to be

considered operable with the test equipment installed.

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting

quality shall be prescribed by documented instructions or procedures, of a type

appropriate to the circumstances, and shall be accomplished in accordance with

these instructions or procedures. The f ailure to incorporate procedure instruction to

have the test equipment removed prior to declaring Diesel Generator 2 operable,

consistent with the safety evaluation, is a violation (298/96019-02). Licensee

evaluation later concluded that the equipment was operable with the test equipment

installed.

c.

Conclusions

The inspectors identified that the emergency diesel generator test procedures were

not appropriate in that no instructions were provided to ensure that test equipment

was remnved before considering the equipment operable. This is a violation.

M6

Maintenance Organization and Administration

M6.1 Phase lll Preventive Maintenance improvement Procram

a.

insoection Scone (62707)

Inspectors reviewed the Phase ll1 Improvement Plan for actions associated with

preventive maintenance in view of recent performance weaknesses.

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b.

Observations and Findinas

The inspectors had noted several minor performance weaknesses in preventive

maintenance activities for items not directly associated with plant systems. These

included inventories, emergency operating procedure contingency materials, and

preventive maintenance accomplished as corrective maintenance activities.

The improvement plan actions included integrating the preventive maintenance for

plant systems and did not address the types of performance weaknesses noted

above. The licensee acknowledged that these weaknesses should be addressed and

stated that they planned to enhance the Phase ill plan to include preventive

maintenance which was not directly associated with plant systems,

c.

Conclusions

Inspectors found that the Phase lli improvement Plan only addressed preventive

maintenance activities for plant systems. Inspectors had previously identified minor

performance weaknesses in preventive maintenance activities not directly

associated with plant systems.

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Quality Assurance in Maintenance Activities

M 7.1 Primary Containment Testina Reauirements

a.

Inspection Scope (62707)

On September 6,1996, the inspector evaluated the status of corrective actions to

preclude maintenance on primary containment valves without adequate primary

containment pressure testing.

b.

Observations and Findings

Section 04.3 of this report discusses a control room review of a primary

containment work package which identified inadequate postmaintenance testing

requirements. The problem identification report written to address this occurrence

had been categorized as a work item only, with the work deferred to the following

outage. The inspector found that the problem identification report was closed after

rescheduling the maintenance. No corrective actions had been taken or planned to

address the cause of inadequate primary containment postmaintenance testing

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requirements. This appeared incomplete, since the work control staff had prepared

a maintenance work package which would not have adequately accomplished

primary containment testing and had provided this package to the control room as

ready for work.

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Af ter discussion with the inspector, the licensee initiated a second problem

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identification report to determine how the design requirements of primary

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containment boundary work should be verified after maintenance activities.

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Conclusions

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Initial corrective actions for this occurrence were weak in that they did not address

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primary containment postmaintenance testing requirements by maintenance

planners.

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E2

Engineering Support of Facilities and Equipment

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E2.1

Unaualified Relav and Housina

a.

inspection Scope (37828)

The inspector assessed the technical support for the replacement of an

undervoltage relay.

b.

Observations and Findinas

Sections 04.1 and M1.2 of this report discuss the evaluation of the installation of

an unqualified replacement relay and housing and the lack of an evaluation of the

affect of jumpers on operability. The evaluation performed for electrical jumpers

was incomplete in that only the need for jumpers was considered. The evaluation

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did not address the affect of the jumpers on undervoltage circuitry operability.

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Similarly, the evaluation of the problem identification report for relay qualification

was incomplete in that it addressed only the circuit which the relay monitored. The

review did not address the effect of the unqualified relay housing on the de power

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circuitry. Subsequently, the unqualified relay was evaluated to be acceptable. The

jumpers were only installed for approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

c.

Conclusion

Technical support for the relay replacement was weak in that incomplete

evaluations were performed. These incomplete evaluations resulted in the impact of

maintenance activities on operability not being fully understood.

E2.2 Temporary Modifications Installed by Procedures

a.

Inspection Scope (37828)

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The inspector reviewed the design controls for jumpers and temporary modifications

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which were installed by procedures.

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b.

Observations and Findinas

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The inspector found that design changes may affect jumpers and plant temporary

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modifications which were installed by operations procedures. A portion of

operations review of design modifications involves determining if plant jumpers

invoked during emergency operating procedures may be affected. The inspector

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noted that jumpers installed by procedures which were not emergency procedures

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could also be affected. The only barrier in place to prevent circuit alterations which

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could affect these jumpers was the review by operations for emergency operating

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procedures. The inspector also questioned the fact that few jumpers had been

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tested, and past modifications may have affected these jumpers. The inspector

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noted that this question was raised during the recent engineering self-assessment,

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but was not addressed as a concern.

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The licensee stated that the potential that past modifications may have altered

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circuits used by jumpers, the lack of inclusion of the concern in the engineering self-

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assessment, and the lack of testing when opportunities were available were

concerns which would be evaluated to determine their safety consequences. A

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problem identification report was initiated to address these issues. The licensee

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planned to address the full scope of these concerns and determine if past

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modifications have affected jumpers, in.the first quarter of 1997. The NRC plans to

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review the results of the licensee's determination. This is an inspection followup

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item (298/96019-03).

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E2.3 Enaineerina Identification of issues

a.

Insoection Scope (37751)

The inspector reviewed activities by engineering to identify and evaluate issues.

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b.

Observations and Findinas

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The licensee identified that the scram discharge isolation drain valves contained only

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one automatic isolation valve per scram discharge volume. The other drain isolation

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valve was a manual valve. This is not typical of scram discharge valve installations,

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however, the licensee determined that the configuration had been approved by a

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license amendment. The associated operability evaluation addressed the

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consequences of a failure of the automatic drain valve and pointed out that the

consequences were bounded by existing analyses. The inspector noted that

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operations crews routinely train with this scenario and have various options to

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respond to the condition. The operability evaluation did not document the expected

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operations response and engineers were unaware that operations responded to this

event in training on a routine basis. The licensee has initiated plans to correct the

condition with a plant modification.

The licensee identified that the reactor water cleanup system high energy line break

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assumed a 4 inch line break. However, a 6-inch line is in place downstream of the

outboard isolation valves and upstream of the 4-inch line. The licensee evaluated

that, for each case, they are bounded within equipment qualification assumptions of

analyzed accidents. However, the 6-inch line break scenario may result in

exceeding the design pressure of a block wall designed as an equipment access

,

port, currently stacked with concrete block and encased in corrugated steel.

The licensee concluded that the failure of the access port wall would not be

significant, since the area and equipment outside the port is nonessential, or located

,

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several feet away, and pressure would drop significantly during incremental f ailure

of the wall. Further detailed evaluation indicated that the outer metal panel may

exceed yield stress and separate at the lower edge. The inner panel and blocks

would not be expected to deform or translate significantly. The licensee issued an

industry notification concerning this vulnerability. The licensee operability

evaluation determined that the high energy line break environmental effects were

bounded and plans to analyze this further and implement permanent corrective

action as required,

c.

Conclusion

The licensee was proactive in identifying engineering and configuration issues, and

was effectively addressing them from a safety perspective. Only minor weaknesses

were noted.

E2.4 Identification of USAR Discrenancies

a.

Scone (37751)

The inspector reviewed the status and issues associated with the licensee initiative

to identify and resolve USAR discrepancies (Inspection Followup Item 298/96007-

06, open).

b.

Observations and Findinas

The licensee has continued to identify cases where the plant practices and

configurations differ from that described in the USAR. Most are of minor safety

significance, and all have been or are being evaluated. Changes to the USAR have

I

been initiated. About 25 items are in the process of evaluation.

One issue involved the procedure for transferring water from the torus to the

condensate system during shutdown conditions. This procedure was approved

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several years ago and has been used; however, the capability to perform this

'

transfer is not described in the USAR. At the end of the inspection period, the

licensee was evaluating the acceptability of this flow path.

Also, for several event scenarios discussed in USAR and design basis documents

and tables, the licensee determined that the pump flows and system configurations

,

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listed for specific scenarios do not clearly indicate context and do not cover

common scenarios making understanding difficult. The licensee initiated a problem

identification report and was taking actions to review equipment performance

2

requirements with respect to the information in the USAR.

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Other findings involved ambiguity of descriptions, drawings and tables which are

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not current, lack of license amendment references, such as station blackout and

1

anticipated transient without scram requirements, and typographical errors.

l

a

f

inspectors performed a routine review of the USAR description of the reactor

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coolant system. The USAR stated that the control rod withdraw piping and Scram

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discharge volume piping were not part of the reactor coolant system boundary.

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Inspectors noted that the ASME Class I reactor coolant boundary as described in

plant drawings and procedures included the Scram Discharge Voiume and portions

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of the control rod withdraw piping. The licensee responded by changing the piping

and volume to ASME Class 11, consistent with the USAR and standard industry

4

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practice. The licensee stated that the inspection requirements would not be

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changed as a result of the lower classification,

c.

Conclusions

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The licensee continued to identify and properly address discrepancies between

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USAR descriptions and plant practices and equipment.

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IV. Plant Support

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R1

Radiological Protection and Chemistry Controls

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R 1.1 Radiation Protection Response to a Reactor Water Cleanuo Pumo Trio and Leaks

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a.

Inspection Scope (71750)

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On August 22,1996, the inspectors reviewed surveys and questioned the radiation

protection technicians concerning the radiation protection response to a reactor

.

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water cleanup pump trip.

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b.

Observations and Findinos

inspectors found that the radiation protection technicians had updated the surveys

to include the steam and water leaks, taken air samples, and contained and directed

the leaks to the drains to prevent further contamination.

c.

Conclusions

The inspectors determined that radiation protection technicians appeared to have

taken appropriate actions in response to a reactor water cleanup pump trip.

P2

Status of Emergency Preparedness Facilities, Equipment, and Resources

P2.1

Insoection of Emeraency Operations Facility and Technical Support Center

Ventilation and Electrical Power Systems

a.

inspection Scope (71750)

The inspectors walked down the Emergency Operation Facility (EOF) and Technical

Support Center (TSC). Both f acilities were undergoing major modifications. The

inspectors physically inspected all of the penetrations leading into each of the

facilities and questioned licensee personnel on the ventilation systems and power

sources for each f acility (emergency and nonemergency power), in addition, the

,

inspectors reviewed Surveillance Procedures 15.HV.101," EOF Emergency Fan

Charcoal and HEPA Filter Leak Test, Fan Capacity Test, and Charcoal Sampling,"

Revision 0, and 15.HV.102, "TSC Emergency Fan Charcoal and HEPA Filter Leak

,

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Test, Fan Capacity Test, and Charcoal Sampling."

b.

Observations and Findinas

The inspectors found that the penetrations were appropriately sealed to support

habitability within each f acility following a design basis accident. Availability of

emergency power to the appropriate equipment necessary to support the f acility,

during a loss of normal power, was noted. The surveillance procedures were

appropriate for monitoring the operability of the emergency fan charcoal and high

efficiency particulate air filter in each facility,

c.

Conclusion

The facility penetrations in both the EOF and TSC appeared satisfactory to support

habitability.

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S1

Conduct of Security and Safeguards Activities

S 1.1

Lack of Guidance to Inform Security of Events

!

a.

Insoection Scope (71750)

Inspectors evaluated whether a switch found in an incorrect position was reported

to security.

b.

Observations and Findinas

An operator found an emergency diesel generator fuel oil pump switch in an

incorrect position. As a result of the incorrect switch position, the diesel was

operable since the pump would have started automatically on it's diesel fuel tank

low level. It would not have started automatically on a low level on the other

diesel's fuel tank.

The inspector observed that security had not been informed of the mispositioning of

the switch and, consequently, had not determined if the event was reportable under

10 CFR Part 73 requirements and had not reviewed the event for misconduct. The

licensee had not determined a definite root cause of the mispositioned switch.

The event was subsequently determined not to be reportable and no potential for

misconduct was found. The inspector questioned whether security should routinely

be informed of occurrences such as this. The licensee responded by conducting

briefings of supervisors to ensure that these types of events were reported to

security. The licensee planned to trend these types of events and develop

procedural guidance to inform security of events such as these.

c.

Conclusion

Initial review of this occurrence by the licensee was incomplete in that security

I

reporting and investigation were not considered until questioned by the inspector.

Security and corrective action group response was strong in that briefings were

performed promptly to ensure that these types of occurrences be reported to

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security. Procedure revisions to include this guidance were initiated promptly.

VI. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

exit meeting on September 10,1996. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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SUPPLEMENTAL INFORM ATION

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PARTIAL LIST OF PERSONS CONTACTED

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Licensee

Mike Boyce, Engineering Manager

Dan Buman, Design Engineering Manager

)

Jack Dillich, Maintenance Manager

)

Rick Gardner, Operations Manager

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Jim Gausman, Plant Engineering Manager

Robert Godley, Nuclear Licensing and Safety Manager

Philip Graham, Site Manager

Mike Pec' ham, Plant Manager

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 37828: Installation and Testing of Modifications

IP 61726: Surveillance Observation

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IP 62707: Maintenance Observation

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IP 71707: Plant Operations

IP 71750: Plant Support Activities

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ITEMS OPENED AND UPDATED

Opened

298/96019-01

VIO

failure to properly assess operability of unqualified relay

installed in 4160v circuit (Section 04.1) and failure to properly

evaluate jumpers installed in 4160v undervoltage circuitry

(Section M1.2)

298/96019-02

VIO

inappropriate installation of test equipment on safety-related

equipment (Sections M1.3 and M1.4)

298/96019-03

IFl

potentiallack of design controls and testing of jumpers in

operating, annunciator responses, and abnormal procedures

(Section E2.2)

Updated

298/96007-06

IFl

licensee initiative to address Final Safety Analysis Report

discrepancies (Section E2.4)