Similar Documents at Cook |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
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N.R.C. OPERATING DATA REPORT l DOCKET NO. 50-315 i DATE 5/1/95 i COMPLETED BY CLIMER TELEPHONE 616-465-5901 >
OPERATING STATUS 4 1.. Unit Name D. C. Cook Unit 1 -----------------------
2.. Reporting Period Apr. 85 notes :
- 3. Licensed ThermalePower (MWt) 3250 1
- 0. Name Plate Rating (Gross MWe) 1152 1 i
- 5. Design Electrical Rating (Net MWe) 1030 : : I
- 6. Maximum Dependable Capacity _(GROSS MWe) 1056 I I -
- 7. Maximum Dependable Capacity (Net MWe) 1020 --------- - =~--------
]
O. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since (,
Last Report Give Reasons _______________________________________ _
_ __________________ _==________=- _-__. - _ _ _ _
=_________
__--- -- =__________ - ===__
t
- 9. Power Level To Which Restricted. =If Any (Net MWe) _________________ 6
- 10. Reasons For Restrictions. If Any:____________________ _ _ ___ __
- _ _____________________- __________________- =_______
This Mo. Yr. to Date Cumm.
- 11. Hours in Reporting Period 719.0 2879.0 90551'.D
- 12. No. of Hrs. Reactor Was Critical 122.4 1868.0 67561.8
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 463.0 14.-Hours Generator on Line 122.4 1856.2 66217.7
- 15. Unit Reserve Shutdown Hours 0.0 0.0 321.0
- 16. Gross Therm. Energy Gen. (MWH) 341767 5410521 195200094
- 17. Gross Elect. Energy Gen. (MWH) 112030 1761840 63533730
- 18. Net Elect. Energy Gen. (MWH) 107515 1694853 61125948
- 19. Unit Service Factor 17.0 64.5 74.9
- 20. Unit Availability-Factor 17.0 64.5 74.9
- 21. Unit Capacity Factor (MDC Net) 14.7 57.7 67.8
- 22. Unit Capacity Factor (DER Net) 14.5 57.2 65.2
- 23. Unit Forced Outage Rate 0.0 0.0 7.2
- 24. Shutdowns Scheduled over Next Six Months (Type,Date,and Duration):
~ - ~~ ~ ~ ~~~ ~
- 25. ii Shut Down 3EIEn5~~oI~ rep ~ ort PbEi~od~~EStI~m$ted ~ ~D3te oI~5tArtu E912 slid 9_29tas9_9 s tima.t99_ s tart-ue_b?3?st_Lk.198 s_.____ ___ ____pI~ ___
- 26. Units in Test Status (Prior to Commercial Operation):
Forcast Achieved IN[ITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL CPERATION 8505240405 B50430 PDR ADOCK 05000315 R PDR 1M VI
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AVERAGE DAILY POWER LEVEL (MWe-Net) f DOCKET NO. 50-315
. UNIT ONE DATE 5/1/85 ..
~
COMPLETED BY CLIMER j t TELEPHONE -616-465-5901 ;-
b MONTH. Apr. 85 $
AVERAGE DAILY' AVERAGE DAILY 4 DAY- POWER LEVEL DAY POWER LEVEL !'
i 1 929 17 O t'
2 924 18 J-O g 3 -930 19 0 ,
4 826' O' 20 5 - 839 21 Oi
~6 32 22 O?' ,
7 0 23- O , . . ,.
-B O 24' O q, f/ y ,g; 9 O 25 _O J r?v
- 10. O 26 0; {g . -
11- 0 27 0- in 12 0 28 0
.13 O. 29 0
.14 0 30 0 15~ O 31 0-
.16 0 4
0 h
t 4
t DOCKET NO.
50-315 . .
ilNITSiltiTIM)WNS AND POWER HEIDUCTIONS D.C. Cook, Unit 1 UNIT NAME DATE 5-8-85 COMPLETEllley B.A. Svensson HEPORT MON ~nt April, 1985 . ~ TELEPHONE 616/465-5901 "t. -
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)sgh* liensee ,iig h. Cause & Causective Actiim no No. Dane g-,
5 livent 3,7 g3 I- yE $ ~ ;y, g Hepius e so O g' Psevens Hecisnence 6
246 850406 S 596.6 B&C 2 N.A. ZZ ZZZZZZ The Unit was removed from service at 0221 hours0.00256 days <br />0.0614 hours <br />3.654101e-4 weeks <br />8.40905e-5 months <br /> on 850406 for the ten-year Inservice Inspection and Cycle IX Re-fueling Outage. In addition to the refueling work, major maintenance work includes steam generator eddy current testing, control rod guide tube replacement, main turbine con-denser retubing, replacement of feed pump turbine condensers and Appendix "R" design changes, u
I 2 3 4
. 12: FinccJ Heason- Meiland: Exlubit G . Insinactinuis S: Stheiluleil A-linguipinent Failme(Explain) 1-Manual for Psepasasiim of Data ll-Maintenance of Test 2 Manual Scsam- lintsy Sheets fus IAcusee C Refueling 3 Automasse Stam. livens Repose (i.l?R)1 ile INilRI:G-
' Il Regulatoiy Restsicliam Othes (lixplain) 01611 1 Opesatos Tsaining& licenw 1:xaminalism 12 Ailministsalive 5 G Ogmaliunal linin Blixplaml Exinbis I- Same Somce 19/D) II Othe (lixplain)
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UNIT SHUTDOWNS AND POWER REDUCTIONS INSTRUCTIONS This report should descnbe all plant shutdowns dunng the in accordance with the taole appearms on the report form, report penod. In adcitron. it should be the tource of explan. If category 4 must be used. supply brief comments.
anon of sigruncant dips m 2verage powerlents. Each signi.
ticant reduction in power lew! (greater than 20", reduction LICENSEE EVENT REPORT :r. Reference the applicable in average daily power !avel for the preceding 24 hnurs) reportsole occurrence pertammg to the outage or power should be noted, even though the unit may not have been reduction. Enter the first four parts (event year. sequennal shut down completelyl . For such reductions in power level. report number, occurrence ecde and report type) of the tive the dursuon should be listed as zero, the method of reduction part designation as descnbed in item I7 of Instrucuons for should be listed as 4 (Other). 2nd the Cause and Correcuw Preparanon of Data Entry Sheets for Licensee Event Report Action to P. event Recurrence column should explain. The (LER) File (NUREG.0161). This information may not be Cause 2nd Correcuve Acuan to Prevent Recurrence column immediately evident for all such shutdowns,of ceurse, since should be used to provide any needed explanation to fully further invesugation may be required to ascertam whether er desenbe the circumstances of the outage or power reduction. not a reportable occurrence was involved.) If the cutage or power reduction will not result in a reportable occurrence.
. NUMBER. This column should indicate the sequential num. the positive indication of th:s !sek of correlation should be ber assigned to each shutdown orsignidesnt reducuanin power noted as not applicable (N/A).
for that calendar year. When a shutdown or signtricant power SYSTEM CODE. The system in whica the outsge or power reduction begins in one report period and ends n another. ggg an entry shot.ld be made for both report periods to be sure
, . g , ,
sit snutdowns or signulcant power reducuons are reported. Exhibit G . Instrucuons for Preparstiert ot Data Entry Sheets Unt:1 a unit has achieved its f!:st power generation, no num. fM bcusu Ennt Repen DER) Ne MREM 16t h ber should be asugned to each entry. Systems that do not tit any existing code should se deugns.
ted XX. The code ZZ should be used for those events where DATE. This column should ind:cste the date of the start a system is not aoplicaole.
of each shutdown or ugniacant power reducuen. Report as year. month, and day. August 14.1977 would be reported COMPONENT CODE. Select the most appropriate .omponent as 770814 When a shutdown or ngrudesnt power reduccon from Exh* t I . Instrucuens for Preparanon of Data Entry begmsin one report pened and ends in 2nother, an entry should Sheets for Licensee Ennt Report (LER) File (NCREG4161).
be made for both report periods to be sure all shutdowns usmg the followmg critiena:
or cgnidcant power reductions are reported.
" " *"** "*" I "'
TYPE. Use "F" or "S" to indicate either " Forced" or " Sche.
duled.*' respectively, for each shutcown or signiacant power B. If not a component failure, us'e the related component:
reducuon. Forced shutdowns incluce those required to be e.g.. wrong valve operated through errett list valve as innisted by no later than the weekend following ciscovery component.
of an off4tormal condition. It is recognized that somejudg.
ment is requsted in categorizmg shutdowns in this way. In C. If a chain of fadures occurs, the tirst component to mai.
generst a forced shutdown is one that would not have been function should be listed. The sequence of events. includ.
completed in the absence of the condition for which corrective ing the other components which fail, saould be desenbed action was taken. under the Cause and Correcuve Acuon to Prevent Recur.
rence column.
DURATION. Self-explanatory. Wher. a shutdown extends Components that do not tit any ex: sung code should be de.
beyond the end or a report penod. count only tne time to the signated XXXXXX. The code 777777 should be used for end of the report penod and pick up the ensumg down ume in the following report cenods. Report duratson of outaps events where a component deugnation is not toplicscle.
ruunced to the nearest tenth of an hour to fac:litate sommation.
The sum of the total outage hours ptus the hours the pners. CAUSE & CORRECTIVE ACTION TO PREVENT RECUR.
RENCE. Use the column in a narrative fash:on to amatify or tot was on line should equal tne gross hours in the reportmg explam the circumstances of the sautdown or power reducuen.
penod.
The column should include the specide cause for each shut.
REASON. Categonze by fetter deugnanon in accordance-
- n M Nm csm pown redwumt and the imnwdiau snd with the taole appearmg on the report form. If category H eentemplated long term correcuve scuan taken. if appropn.
must be used, sacciy bnef comments, ste. T'us r column snould also be used for a descrtation of the maior safety.related corrective mamtenance performed dunna METHOD OF SHUTTING DOWN THE REACTOR OR the outage or power reduction includmg an idenufication ot}
REDUC:NG POWER. Categonze ov numner dengnanon tne enuest path acuwty and a repon at any ange niesse et radioacunty or smgfe tsdistion exoosure spectiesdy asscet.
INote that this dairers : rem the Edium Eleutne Insutute sted with the outage which accounts for more than 10 :ereen t eel) denmuens of " Forced Par'ts! Outate" and "Sene, of the silowsole annual values.
suled Psctra! Outage." For these temu. eel uses 4 hange at For long textual reports eontmue narrative on separate ;' aper 20 MW as the bress pnmt. For larger puwer rencors. 30 MW .nd referense the shutdown or power re:su uun im tma a sm > mall J .hange to wanant espianatwn. narrative.
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. Docket'No.: 50-315 ~
Unit Ntms: D.C. Cook Unit 1 Completed By: A. S. Puplis Telephone: (616) 465-5901 Date: May 10, 1985 Page: 1 of'2 MONTHLY OPERATING ACTIVITIES - APRIL, 1985 HIGHLIGHTS:
The_ reporting period began with the Unit in Mode 1 at 90% power
~
in coast down toward an April 5, 1985 shutdown to begin the Ten
- . Year Inservice Inspection and Cycle 9 Refueling Outage. The' Unit was removed from service at 0221 on April 6. At the end of the reporting period the reactor vessel closure head was removed and the refueling cavity was being filled to the refueling-level.
Gross electrical generation for the reporting period was 112,030 MWH.
Summary:
4-03-85 At 0135, a slow power reduction to 85%-was initiated as part of the coast down. Power reached 85% at 1600.
4-05-85 -At 2055, the Unit shutdown was started.
~4-06-85 At 0221, the Unit was manually tripped from 22%.
At 0640, the 0400 dose; equivalent iodine sample indicated an iodine spike of 4.48 pCi/ml, which is greater than the Technical Specification limit of 1.0 pCi/ml.
4-09-85 At 0724, and again at 0736, an ESF actuation occurred which-caused the containment. ventilation system'.to isolate due to an instrument spike on' containment atmosphere radiation monitor ERS 1301.
At 1214, an ESF Actuation occurred due to an instrument spike on containment atmosphere radiation monitor ERS 1401.
4-11-85 At:0110, an ESF Actuation was caused by ERS 1301.
i At 0615, the Turbine Driven Auxiliary Feedwater Pump l was declared inoperable because it could.not develop sufficient discharge pressure. ,
At 2230, an RCS Cooldown to 500*F was initiated.
4-12-85 At'll15, the RCS entered Mode 4, Hot Shutdown.
i
a F 50-315 D ckst No.:
Unit Names D.C. Cook Unit 1 Completed By: A. S. Puplis.
Telephone: (616) 465-5901 Date: May 10, 1985 Page: 2 of 2
, 4-13-85 At 1020, Mode 5 Cold Shutdown'was entered.
~
4-18-85 ~At 0210, draining of the reactor coolant system to half loop was started.
4-19-85 At 0955, the RCS was at. half loop.
4-23-85 At 1827, the RCS entered Mode 6, Refueling.
27-85 .At 1021, an Unusual Event was declared per EPP.010, Toxic Gas Release Guideline. The toxic gas resulted from a hydrazine leak on FFC-241 main feed flow controller. The Unusual Event was terminated at 1118.
4-29-85 At 0611, an'ESF actuation occurred due to a spike _an ESF 1401.
At 1015, an Unusual Event was declared as the result of a serious. personnel injury. The Unusual Event was terminated at 1328.
.The Control Room Cable Vault Halon System remains inoperable as of 1400 on 4-05-83. The backup CO System for the Control Room 2
Cable Vault remains operable.
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J av 1
DOCKET NO. J50 - 315 UNIT NAME' D. C.-Cook - Unit No. 1 DATE 5-8-85 4 COMPLETED BY B. A. Svensson
- MAJOR SAFETY-RELATED MAINTENANCE APRIL', 1985
-M-1 During the performance of hydrostatic testing, a seal plate packing spring on the inboard auxiliary stuffing box of the' North Safety Injection Pump failed, Conversations.with the.
', pump manufacturer revealed that-the spring served as a spacer and lacking a replacement could be replaced with a gasket of
- . . suitable dimension. Along with the spacer gasket, a new
. mechanical seal was installed and operability; testing was performed 1to ensure the effectiveness of the repairs.
C&I-1 'The."W" Motor Driven Auxiliary Feedpump~ tripped following an automatic start. Two of the.three pressure. switches on'the ;
~
pumps' suction were out of calibration,' tripping at_a higher j pressure than normal. They were recalibrated.. The other.
y switch was found : inoperable, because ent insulator strip' in-
, s terfered with the trip mechanism.. The strip was cut off to prevent the interference, and the; pressure switch was recal-' ,
ibrated.-
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fg=::"._ INDIANA & MICMSAN ELECTRIC C_0MPAN1 Gy,a--
Donald C. Cook Nuclear Plant P.O. Box 458, Bridgman, Mchigan 49106 Blf May 8, 1985 Director, Office Of Management Information and Program Control
.U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Gentlemen:
Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 1 Technical Specification 6.9.1.6, the attached Monthly Operating Report for the Month of April, 1985 is submitted.
- Sincerely,
~ (1 y)./ ; y W. G. h, Jr.
Plant Manager WGS:ab Attachments cc: 'J. E. Dolan M. P. Alexich R.-W. Jurgensen NRC Region III B. L. Jorgensen R. O.-Bruggee R. C. Callen S. J. Mierzwa R. F. Kroeger B. H. Bennett
.P. D. Rennix J. H. Hennigan Z. Cordero J. J. Markowsky J. F. Stietzel-PNSRC File' INPO Records Center ANI Nuclear Engineering Department
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