ML20127K894
| ML20127K894 | |
| Person / Time | |
|---|---|
| Site: | Big Rock Point File:Consumers Energy icon.png |
| Issue date: | 12/31/1992 |
| From: | Jeanne Johnston CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML20127K890 | List: |
| References | |
| NUDOCS 9301260262 | |
| Download: ML20127K894 (2) | |
Text
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Consumers NUCLEAR OPERATIONS DEPARTMENT Company Unit Shutdowns and Power Reductions Report Month Docket Number Unit Date Completed by Telephone December 1992
$5-150 Dig Rock Etnint Plant January 4, 1993 JE JottNSToM g616) 521-8223 i
Method of l
Shutting Duration Down IJcensee Event System Componpt 3
2 3
Code Cause and Corrective Action To Prevent Recu vence Number Date Type (Hours)
Reason Reactor Report Numtwr Code 92-22 12/06/92 S
90.0 A
2
- The amit was removed free service due to steam leaks thru Brs rm the Reactor Depressurizing System (RDS). The RDS 12/10/92 "A" train had a pinhole leak in a socket weld, and the EDS "B" trnin had a valve flange leak. The nasit fs retu.-ned to service after the completing the rep.,rs.
s
).
1 4
I 2
3 4
F = Forced Reason:
Method:
Exhibit G = Instructions for S = Scheduled A = Equipment Failure (Explain) 1 = Manual Preparation of Data Entry Sheets 4
B = Maintenance of Test 2 = Manual Scram for Licensee Event Report (LER) i C = Refueling 3 = Automatic Scram File (NUREG-0161)
D = Regulatory Restriction 4 = Other (Explain)
E = Operator Training and License Examination 5Exhibit i = Same Source F = Administrative G = Operational Error (Explain)
H = Other (Explsin) 9301260262 930115 Form 3156 1-82 PDR ADOCK 05000155 R
a M
GREYBOOK OPERATING DATA REPORT 6
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DOCKET 'NO; 50-1's5 ' -~ DATE:
i / iS / 93 ~
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BY: JR JOH'45 TON OPERATING STATUS FHOt4E :
616-547-6537sEXT 223 a
- 1. UNIT NAME: BIG ROCK POINT NUCLEAR PLnNT NOTES:
().
- 2. REFORTING PERIOO:
12 / 92
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- 3. LICENSED THERMAL POWER (MWT): '
240
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f 47 NAMEPLATE RATING ~(GROS 5 MWE):
75
- Q sj L DESIGN ELECTRICAL RATING (NET NWE):
72
- L 6_. NAXIMUM,DE'ENDABLE CAPACITY _(Gross MWE)2 71.0
- 7. MAXIMUM CEPENC%BLE Ci4PACITY (NET MWE)r 67.0
' O 8.
IF CHANGES OCCUR IN CAPACITY RATING 5(ITEM 5 3 TH't.U 7) SINCE LAST REPORT, GIVE REA50tJ5:
c, "9.' POWER LEVE*. TO WHICH RESTRICTED,IF ANY (NCT ' t1WC l :
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.O;lo.REA50t45FORRESTRICTIOt45, IF ANY:
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THI5 MONTH YEAR-TO-DuTE cut 4ULaT IVE on
= 11. HOURS IN REPORTING PERIOO 744.0 8734.0 260999.0 d12.' NUMBER OF HOURS REACTOR Wa5' CRITICAL'
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' 6 5 3.7' ^ ~ ~ ~ ~
~4790.5~
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'188159.4,
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C (d 13. REACTOR RE5ERVE SHUTDOWN HOURS 0.0 0.0 0.0 m
s 15. UNIT RESERVE SH8JTDOWN HOURS 0.0 4700.6_
_ 185145.7 14._ HOUR 5 GENERATOR ON-LINE 654.1 0.0 0.0 C* 16. GROSS THERMAL ENERGY GENERATED (MWH) 198262.0 896669.0 35494707.0 e
= 17. GROSS ELECTRICnL ENERGY GEi4ERATED (MWH) 46716.0 287419.0
[167f4ET ELECTRICAL ENERGY GENERATED (MWH)~
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54341.7~~
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'271422.O'
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11272005.0 10663180.4'
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- 19. UNIT SERVICE F ACTOR 87.9%
53.5%
71.0%
e C(d20. UNIT AVAILABILITY FACTOR
~
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' 07.9%
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53.5%
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'60.7%
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71.0%
215~ UNIT'APACITY FACTOR (U5ING MDC NET) 09.0%
46.1%
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08 22. UNIT CAPACITY FACTOR (USING DER NCT) 62.8%
42.9%
56.8%
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- 23. _ UNIT FORCED OUTAGE RATE 0.0%, _ _
11.2%.
12.9%
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- 24. 5HUTDOWN5. 5CHEDULED OVER NEXT 6 mot 4TH5(TYPE,4eTE, & DURATIOtt OF E"ACHl
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- 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DHTE OF STARTUP:
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