ML20127F591
| ML20127F591 | |
| Person / Time | |
|---|---|
| Site: | Catawba |
| Issue date: | 03/29/1985 |
| From: | Tucker H DUKE POWER CO. |
| To: | Grace J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML20127F586 | List: |
| References | |
| NUDOCS 8505200517 | |
| Download: ML20127F591 (3) | |
Text
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DUKE POWER GOMPANY P.O. HOK G3180 CHARLOTrE, N.C. 28242 HALB. TUCKER Ten.ernow.
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]0 APy 3 p g ~, 4 7 March 29.-1985 Dr. J. Nelson Grace, Regional Administrator U.S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia. 30323 Re: RII:PHS/PKV 50-413/84-106
Dear Dr. Grace:
Please find attached responses to Violation.No. 413/84-106-03 and Violation
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No. 413/84-106-04, as identified in the above referenced' inspection report.
This item was also addressed in Licensee Event Report LER/85-02 and was discussed at the Enforcement Conference held in Atlanta on February 8, 1985.
Duke Power Company does not consider.any information contained in this inspection report to be proprietary.
Very truly yours, Hal B. Tucker LTP:smh Attachment cc: NRC Resident Inspector Catawba Nuclear Station Robert Guild, Esq.
P. O. Box'12097 Charleston, South Carolina 29412 Palmetto Alliance 2135 Devine Street Columbia, South Carolina 29205 Mr. Jesse L. Riley Carolina Environmental Study Group 854 Henley Place Charlotte, North Carolina 28207 8505200517 850409 PDR ADOCK 05000413 0
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Ys ni DUKE POWER COMPANY CATAWBA NUCLEAR STATION JViolations:
~1.
Technical Specification (TS) 3.0.4 prohibits entry into an Operational
- Mode unless the~ condition for the Limiting Conditions-for Operations are met.without reliance on provisions contained in the Action requirements.
TS 3.6.5.3 requires' ice condenser inlet doors.be closed and operable.
Contrary to the.above, fice condenser inlet doors were blocked closed between December:31,,1984 1following Operational Modes were entered:and January 9, 1985 and therefore, Mode 4 on December 31, 1984, Mode
- 3 on January 2,.1985.and Mode 2 on January 7, 1985,
- 2.. TS '6.8.1 requires written procedures be established and implemented for safety-related systems and components. OP/1/A/6100/01, Controlling
-Procedure for Unit Startup, requires verification that the blocks on the
-ice condenser' lower inlet. doors are removed.
Station Directive 4.2.2, Section 3.1.1,. implements NUREG 0737, Item I.C.6 as referenced in'FSAR Table
- 1.9-1, states.that Independent Verification applies to. removal from and return to operability of all systems or components that effect safety-related functions.
Contrary to the above, OP/1A/6100/01
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was erroneously completed and indicated that the ice condenser inlet door blocks had been removed when in fact they
-were still installed until January 9, 1985.
Additionally,- independent iverification was not assured and consequently not performed'for' the removal of the door: blocks.
. Response:.
- 1., Duke Power admits the violations.
2.
MiscommuniEation between personnel. created the impression that the ice condenser door blocks had beenLremoved, when in fact the blocks were
'still'in place. This resulted in the unit changing. modes while the limiting conditions-for' operations for technical specification 3.6.5.3 were not being met.
13.
- The door blocking devices were removed.
All. Unit One door blocking devices have been-painted fluorescent orange and will be sequentially numbered
-(1 through 24).
This is to ensure that the blocking devices will be accountable and highly visible when installed. 'A procedure has been
. developed'and implemented to ensure that all mode related requirements
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- under the. responsibility of the group responsible for unblocking the -
. doors, have been satisfied prior to entering each mode of operation.
Also:a procedure has been implemented specifically for installation and removal of' the door blocking devices. This procedure requires that the installation and removal-be independently verified. Also, all appropriate personnel,as designated by. the Station Manager, have reviewed the methods used to assure completion of required work pertaining to
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OP/1/A/6100/01..
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<; 99 i I ;',,.,',
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.4.'All Unit Two door blocking devices will be painted fluorescent green
.and sequentially numbered. This' action and those actions outlined in (3)'will avoid further violations.
- 5. The actiidns outlined in (3) have been completed. The Unit Two door blocking devices will be painted and numbered by May 1, 1985. Catawba will be in full compliance at this.' time.
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