ML20127E124

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Insp Rept 50-320/85-10 on 850411-0517.Violation Noted: Failure to Comply W/Procedures Re Security Practices. Portions Deleted (Ref 10CFR73.21)
ML20127E124
Person / Time
Site: Crane Constellation icon.png
Issue date: 06/12/1985
From: Barr K, Bell J, Dan Collins, Cook R, Cowgill C, Moslak T
Office of Nuclear Reactor Regulation
To:
Shared Package
ML20127E075 List:
References
50-320-85-10, NUDOCS 8506240442
Download: ML20127E124 (13)


See also: IR 05000320/1985010

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U. S. NUCLEAR REGULATORY COMMISSION

DCS No.

50320-850327

Report No.

50-320/85-10

Docket No. 50-320

License No. DPR-73

Priority

Category

C

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Licensee:

GPU Nuclear Corporation

P.O. Box 480

Middletown, Pennsylvania 17057

Facility Name:

Three Mile Island Nuclear Station, Unit 2

Inspection At: Middletown, Pennsylvania

Inspe.: tion Conducted: April 11 - May 17, 1985

Inspector -

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ident Inspector (TMI-2)

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T. Moslak', Residtht Inspector (TMI-2)

date figned

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L D11, Senior Radiation Specialist

c ate ligned

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c //</C

. Barr, Raciation Specialist

date signed

10. PAN

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D. Collins, Radiation Specialist

date signed

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Approved By:

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C.'fowgill, Chigf, TMI-2 Project Section

cite signed

Inspection Sumary:

Areas Inspected:

Routine safety inspection by site inspectors of plant

operations (long term shutdown) including licensee action on previous

inspection findings' quality assurance annual assessment; witnessing of fire

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brigade drill; operator training; review of licensee event reports;

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preparations associated with plenum assembly removal including modified fuel

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transfer system turnover, flooding of the deep end of the fuel transfer canal,

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polar crane inspection, installation of fuel transfer canal dam, inspection of

the fuel transfer canal prior to flooding, refurbishment and testing of the

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polar crane auxiliary hoist; removal of the plenum assembly; reactor building

entry by NRC to examine "A" D-ring; routine health physics ano environmental

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reviews and security. The inspection involved 417 inspector-hours.

Results:

Failure to comply with procedures regarding security practices.

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DETAILS

1.0 Ongoing Recovery Operations

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a.

Routine Plant Operations

Inspections of the facility were conducted to assess compliance with

the requirements of the Proposed Technical Specifications and

Recovery Operations Plan in the following areas:

licensee review of

selected plant parameters for abnormal trends; plant status from a

maintenance / modification viewpoint, including plant cleanliness,

control of switching and tagging, and fire protection; licensee

control of routine and special evolutions, including control room

personnel awareness of these evolutions; control of documents,

including log keeping practices; radiological controls; and security

plan implementation.

Random inspections of the control room during regular and back shift

hours were routinely conducted. The Shift Foreman's Log and

selected portions of the Control Room Operator's Log were reviewed

for the period April 11 - May 17,1985. Other logs reviewed during

the inspection period included the Submerged Demineralizer System

(SDS) Operations Log, Radiological Controls Foreman's Log, and

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Auxiliary Operator's Daily Log Sheets.

Operability of components in systems required to be available for

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response to emergencies was reviewed to verify that they could

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perfom their intended functions. The inspectors attended selected

licensee planning meetings. Shift staffing for licensed operators,

non-licensed personnel, and fire brigade members was observed.

During plant walk arounds, the inspector noted improvements need to

be made in overall plant housekeeping.

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No violations were identified.

2.0 Licensee Action on Previous Inspection Findings

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(Closed)InspectorFollowItem(320/84-24-01): Adequacy of Radiological

Review for SDS standpipe pump disassembly and cutting in preparation for

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disposal.

Radiological Awareness Report (RAR)85-005, was initiated by the licensee

following the initial attempt to prepare and package one of two SDS pumps

for disposal. Radiological conditions developed during the work that

resulted in personnel and area (compactor room) contamination and the

establishing of the compactor room as a locked high radiation area. The

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jobwasstoppedandtheRadiationWorkPermit(RWP) terminated. A

critique was conducted by the licensee, a second radiological review and

RWP were completed, and the preparation and packaging of both pumps was

completed without further incident. The inspector attended the critique,

reviewed the processing of the RAR, including closeout action taken by

Radiological Engineering, Radiological Field Operations, and Radiological

Training, and determined that appropriate actions were taken by the

licensee. Consequently, this item is closed.

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(Closed)UnresolvedItem(320/84-09-03):

Sump Sanpling/ Transfer

Requirements.

In order to improve the representativeness of sump samples and refine the

accounting of radioactive releases, the licensee has been developing and

implementing improved sump sampling and sample analysis methods.

Toward

this end, the licensee has rewritten its sump pumping and sampling

procedure to better control liquid transfers and improve the

representativeness of samples.

The revised procedure requires

recirculation of controlled sumps prior to sampling and the sending of

samples offsite for enhanced sensitivity analysis. Sump recirculation is

accomplished through the use of temporary systems, but hard piping is now

being installed under an Engineering Change Authorization.

In

consideration of these actions, this item is closed.

3.0 Quality Assurance Annual Assessment of 1984

On April 25,1985, in accordance with Quality Assurance (QA) Plan

requirements, the licensee's QA department presented its yearly

assessment of the effectiveness of the QA program to senior management.

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The inspector attended this presentation. Managers of sections within

the QA department, including QA Engineering, Site Welding, Quality

Control, Operations QA, Site Audits and QA System Engineering, identified

their respective program's strengths and weaknesses, then made

recommendations for improving performance. A total of 21 recommendations

were made. Examples of the recommended actions included:

Improve controls for modification tie-in to existing systems by

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revising procedures to more clearly define responsibility for

control of tie-ins and turnover

Reduce the inconsistency in supplying welding requirements in Unit

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Work Instructions (UWI) by providing more training to responsible

personnel and closer interfacing between Recovery Operations and the

Maintenance Departments

Improve procedural compliance in properly completing the lifted lead

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electrical jumper and temporary mechanical modification log by

providing renewed emphasis in plant operations training

Reduce the redundancy and duplication of procedures by more

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critically reviewing procedures during the biennial review.

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The inspector determined that presentations were candid and that the

assessment was accurate and consistent with findings identified in NRC

inspections.

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4.0 Witnessing of Fire Brigade Drill

On April 15, 1985, the Resident Inspector observed an unannounced Fire

Brigade drill. The drill simulated extinguishing an electrical fire in

the Cable Room on the 305' elevation of the Control Building.

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The inspector considered the drill to be satisfactory in terms of the

quickness of.the brigade response and actions taken at the scene to

extinguish the simulated fire.

The Brigade Leader took charge

imediately and initiated actions that were considered appropriate and

effective.

Brigade members reported promptly to the scene with their

assigned equipment.

Personnel suited up in turn out gear including,

Self-Contained Breathing apparatus. Two additional shift personnel were

at the scene assisting the Brigade Leader. The drill was monitored by

three members of the Fire Protection Department and two members of the

Training Department. Subsequent to securing the drill, a critique was

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conducted at the scene by the monitoring team. The inspector determined

that the critique was thorough.

The inspector identified no major deficiencies in the conduct of the

drill.

5.0 Operator Training

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On April 24, 27, and May 17, 1985, the inspector evaluated Senior Reactor

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Operator (SR0) and Fuel Handling Limited Senior Reactor Operator (FHSR0)

training pertaining to systems to be used in defueling operations. On

the respective dates, the inspector attended presentations on the Vacuum

Defueling System, Canister Positioning / Storage Systems, and In-Vessel

Lighting System / Core Boring System.

The inspector detemined that these

presentations met Training department objectives by introducing the

students to the equipment that would be used for defueling.

The

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handouts, audio visual aids, and lesson plans had sufficient detail to

provide a general overview of how components of the defueling systems

would be arranged and there basic principles of operations.

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The inspector detemined that the references used for development of this

training have been restricted to final design reports, design drawings

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and testing documents. Accordingly, the inclusion of several key areas

in systems training has been incomplete. These key areas are operating

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procedures, administrative procedures, technical specifications, and

limits and precautions.

These aspects of the systems training are to be

incorporated as the respective documents are drafted and finalized.

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Through discussions with the licensee's Operating Training Manager, the

inspector detemined that more detailed presentations, addressing the key

areas, are scheduled to be made by Design Engineers from the Bechtel

organization in mid-June.

Subsequent to completing this classroom

training, SR0's and FHSR0's will attend Penn State University (PSU) for

reactor training. This training using the PSU Braezale Reactor is to

accomplish four objectives:

Simulate the collapse of fuel to provide the operator with a first

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hand observation of neutron population change and criticality safety

margin reduction

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Remove fuel from various regions of the core to simulate a defueling

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operation

Simulate a deboration until criticality is reached to emphasize the

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criticality safety at high boron concentrations

Load fuel rods into a specific area of the core to simulate loading

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fuel fragments into a canister submerged under water.

Following the PSU reactor training, three additional phases will be

conducted to complete the system's training.

These phases are mockup

training using defueling equipment on the Defueling Test Assembly located

in the Turbine Building, hands-on training using the Fuel Canister

Handling Bridge in the Reactor Building, and Integrated

Systems / Procedures Classroom.

The NRC will continue to monitor the licensee's training program for

qualifying SR0's and FHSR0's to perform core alterations.

6.0 Licensee Event Report (LER) Review

The inspector reviewed the LER listed below which was submitted to the

NRC TMI Program Office to verify that the details of the event were

clearly reported, including the accuracy of the description of the cause

and the adequacy of corrective action.

The inspector determined whether

further infonnation was required from the licensee, whether the event

should be classified as an Abnonnal Occurrence, whether generic

implications were indicated, and whether the event warranted onsite

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followup.

LER 85-06 dated April 25, 1985, addressed a licensee identified

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condition in which a containment isolation valve is maintained in

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the open position without an NRC approved procedure so authorizing

this position. The root cause of this administrative discrepancy

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was an apparent typographical error which resulted in the position

of the valve, RR-V-20E (an instrument isolation valve located on the

inboard side of penetration R-588 for the Reactor Building (RB)

cooling coils), being listed as " closed" vice "open" in Revision 1

of 2104-5.1.

The inspector determined that this event resulted from an

administrative error and did not involve an actual mispositioning of

the valve. Accordingly, the inspector concluded that the LER was

submitted to meet the administrative reporting requirements of

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10 CFR 650.73 and had no effect on system operation nor the health

and safety of plant personnel and the public.

7.0 Plenum Assembly Removal

On May 15, 1985, the plenum assembly was removed from the reactor vessel

and placed in storage, under water, in the deep end of the refueling

transfer canal (RTC). Prior to completing this evolution the licensee

had to complete the following pre-requisites:

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Startup testing on the modified Fuel Transfer System

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Installation and testing of the dam that would separate the shallow

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end of the RTC from the deep end

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Annual preventative maintenance on the RB polar crane

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Refurbishment and testing of the auxiliary hoist of the polar crane

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Flooding of the deep end of the RTC.

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Site NRC inspectors performed the following as a verification that the

prerequisites had been properly completed.

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Modified Fuel Transfer System (FTS) Turnover: At various times

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during the three week testing phase, the inspector discussed test

progress with the lead Startup and Test Engineer.

The inspector

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determined that some of the remedial actions that were taken during

the testing prior to completing a Return-To-Service (RTS) to plant

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operations included changeout of a winch assembly due to excessive

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vibration and noise, repositioning of a lifting eye on the canister

basket due to a mechanical interference, and various mechanical

alignments to provide smoother operation.

Prior to completing the

RTS, plant operators were trained on the operation of the FTS and

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had cycled the West FTS approximately 40 times without any

operational difficulties. The inspector observed the West FTS being

operated three times and noted that the winch drives, horizontal

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transfer mechanism and hydraulic upenders worked satisfactorily.

Subsequent to the testing, the inspector observed blind flanges

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being installed on the transfer tubes in the "A" spent fuel pool and

leak tested to verify that unacceptable leakage would not occur from

the deep end of the RTC (when flooded) to the "A" spent fuel pool.

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The inspector discussed with the Site Operations Director, the

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statusoftheitemsontheIncompleteWorkList(IWL),priorto

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system turnover. Through this discussion, the inspector determined

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that none of the items on the IWL would preclude the FTS from

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perfoming its intended function nor would they be detrimental to

safe operation. The FTS was turned over to the Plant Operations

department on May 14, 1985.

No violations were identified.

Flooding of the Deep End of the RTC: On May 14, 1985, following

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turnover of the FT5 and dam to the Plant Operations department, the

licensee commenced transferring approximately 64,500 gallons of

borated water from the Borated Water Storage Tank (BWST) to the deep

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end of the RTC.

Prior to beginning this evolution, the inspector

discussed valve line-ups with licensed operators, reviewed the

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applicable opereting procedure 4210-0PS-3254.01 (Operation of Canal

Fill and Tool Flushing System), and examined system drawings to

verify flow path. The inspector determined that the controlled

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procedure had been reviewed and approved by the NRC per the

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requirements of TS 6.8.2, that the BWST volume and chemistry

parameters were as required by the TS and that the RTC level

indication met the procedural requirements of 4210-0PS-3254.01.

No violations were identified.

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Polar Crane Inspection:

During the reporting period, the resident

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inspector reviewed the polar crane annual preventative maintenance

procedure 4220-PMG-3882.01, " Periodic Inspection of Polar Crane,"

and the completed data sheets for performing these annual

inspections of the polar crane. As a result of these inspections,

contacts in the main hoist high speed main contactors on the bridge

were replaced because they were found in a degraded state.

The slow

speed main hoist contactor had cracks in the insulating plastic

housing for the auxiliary contacts. The auxiliary contact assembly

was replaced.

The slow speed motor clutch for No. 4 bridge drive

had cracks in the commutator brush holders. The brush holders and

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brushes were replaced. A portion of the bridge rails located at

position No. 12, which is located near the parked position,

exhibited signs of flaking and/or motion.

The gap at this location

was measured at 11/16 inch with a 5/8 inch offset.

Since the crane

is controlled using a pendent switch, the licensee is making a

concerted effort to avoid leaving the crane in the parked oosition,

thus minimizing wheel engagement of the flaking rail.

As a prerequisite to plenum lifting, the resident inspector made an

inspection of the physical condition of the polar crane on May 10,

1985.

It was noted that the plastic tie wrap used to ensure that

the brake shoes of the bridge hydraulic brake do not contact the

drum was broken on the brake at the end opposite from the cab. This

broken tie wrap was replaced prior to the inspector leaving the

polar crane.

It was also noted that there was more trash on the

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crane than anticipated. The trash was picked up and brought from

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the polar crane by the licensee at the time the inspector left the

The licensee has generated internal memoranda to bring staff

crane.

awareness to the need for good housekeeping practices. While on the

crane, the inspector did note that the original bumpers and some

electrical testing equipment which had been previously stored on the

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polar crane had been removed.

Fuel Transfer Canal Dam: Prior to lifting the plenum from the

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reactor vessel, the licensee installed a metal dam across the deep

end of the fuel pool. This dam, which is nominally 5 feet high, is

sealed'by two adjacent inflatable rubber seals located around the

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peripheral sealing surface.

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The resident inspector made an RB entry on April 30, 1985, to

witness inflating of the seals and the hydrostatic test accomplished

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by putting borated water in the annulus area between the seals.

When the bottled nitrogen was energized to the seals, several leaks

were detected using a soap solution. These leaking joints were

remade and/or tightened to effect zero detectable leakage. However,

when the nitrogen gas was energized to the seals, the seals did not

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inflate. The seals could not inflate because inline check valves

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located at the dam seals were installed in a reverse flow direction

which preclude nitrogen gas from entering the seals. The resident

inspector witnessed the inline check valves being reoriented and the

subsequent satisfactory leak test of the affected joints using a

soap solution. When the annulus area between the seals was filled

with borated water, water inadvertently overflowed into a trough

located on the outside of each seal. Therefore, the zero leakage

requirement of the seals could not be determined.

During a subsequent RB entry on May 10, 1985, the resident inspector

was able to observe dry conditions in the trough area while a water

level was maintained in the annulus area between the seals.

Thus, a

zero leakage condition was observed prior to flooding of the deep

end of the fuel transfer canal.

Fuel Transfer Canal Inspection: On May 14, 1985, the resident

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inspector made an RB entry to examine the material condition of the

fuel transfer canal.

The deep end had some minor pieces of debris

which were removed at the time of the inspection. The shallow end

had substantial amounts of debris and other material which could

interfere with pumping and purification systems in the event that

the shallow eno of the pool required flooding.

Prior to flooding

the deep end of the pool to a level of engaging the dam, the

licensee removed materials that could encrouch on safe flooding and

subsequent cleanup of the shallow portion of the fuel transfer

canal.

Polar Crane Auxiliary Hoist: During the inspection of the polar

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crane, the resident inspector examined portions of the polar crane

auxiliary hoist which had been recently refurbished and load tested.

It appeared that the auxiliary hoist had been refurbished as

described by the licensee in their memorandum, Sumary of the Polar

Crane Auxiliary Hoist Mechanical Component Refurbishment, dated

April 17, 1985. The resident inspector inquired whether the clips

which attach the wire rope to the drum are covered in any of the

preventative maintenance examinations as the auxiliary hoist has the

capability of running out most of the wire rope within some portions

of the lifting envelope. The licensee stated they were in the

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process of incorporating surveillance checks on these clips in their

annual preventative maintenance inspection program.

Subsequent to

examining the auxiliary hoist, the resident inspector examined

accessory replacement parts for Amerigear flexible couplings. The

locking nuts used on the couplings were a crimped styled nut. The

locking feature appears quite satisfactory.

During the load testing of the auxiliary hoist, it appeared that the

Dillon Load Cell used was out of calibration as the actual load

indication was above the anticipated test load. Whiting

Corporation, the crane supplier, had authorized testing of the

auxiliary hoist to 65,000 pounds. However, after the questionable

indication on the load cell, another load cell was used. The second

load cell had claimed accuracy of 1%. Considering the load cell

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accuracy and the questions associated with the actual load which may

have been placed on the crane during the attempted first test, there

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was some concern expressed as to whether the 65,000 pounds load

limit imposed by the Whiting Corporation had been (or could be)

exceeded. The Whiting Corporation gave verbal authorization,

followed by a written authorization to exceed the original load test

of 65,000 pounds to 67,500 pounds or 135% over the 50,000 pounds

rated capacity.

After the load test, the licensee sent both Dillon Load Cells to

Morehouse Instrument Company for calibration. The load cell used

for the test (accuracy of 1%), was within the allowable accuracy

limits. The load cell which had indicated higher than anticipated

loads was found out of calibration with readings nominally 3.5% high

at the load test weight. The acclaimed accuracy for this load cell

was 10.5%.

A review of the documentation associated with the auxiliary hoist

load test reveals that no load greater than 66,000 pounds could have

been lifted and the 67,500 pounds one time load limit was not

exceeded. The NRC authorized use of the reactor building polar

crane's auxiliary hoist to loads no greater than 25 tons by letter

dated, April 22, 1985.

8.0 NRC Reactor Building Entry

On April 19, 1985, an NRC inspector made an RB entry to assess radiation

safety, industrial safety, general housekeeping and work activities in

the "A" D-ring. The inspection included the 349', 330', 323' and 309'

elevations inside the "A" D-ring, as well as several small intermediate

level platforms. A photo survey was made of the 349' and 308' elevations

to record the condition of work areas and equipment staged in surrounding

areas to be used in the characterization of any fuel in pressurizer

relief and safety valves (349' elevation), in the base of the

pressurizer, and in the horizontal runs of the pressurizer surge line

(308' elevation).

In addition, on the 308' elevation, observations were

performed of the planned access routes for equipment drops to

characterize the "J" legs of the steam generator. Verification was

performed of the installed winches on each elevation for personnel

rescue.

The entry was made under Unit Work Instruction (UWI) 4370-305A-85-0072,

ALARA review 51030 and Radiation Work Permit (RWP) 011431.

Supporting

paperwork was reviewed for accuracy and appropriateness of specified

clothing, dosimetry and respiratory protection. All requirements were

found adequate.

The inspector attended the required task supervisor's meeting for job

planning and scheduling on the day prior to the entry and the job

briefing and Red Tag Key (high rad beta) area briefings just prior to the

entry. All briefings were found to be complete, done in appropriate

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detail and accurately reflected conditions encountered.

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The protective clothing, safety equipment, dosimetry and respiratory

protection requirements were found to be conservative. A problem did

arise during the suiting up process related to the acceptability of the

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use of a small size MSA respirator mask with a powered air purifier

respirator (PAPR). A Breezer respirator (same protection factor as PAPR)

was substituted for the PAPR.

Following the entry, it was detennined

that the use of the small size mask with the MSA PAPR is acceptable.

The

confusion was determined to be the result of the technician

misunderstanding the acceptable letter codes for mask use with particular

respirators. NRC will review the technician training program which

addresses the issuance of respiratory protection equipment to verify its

adequacy.

(320/85-10-01)

The inspection of the "A" D-ring resulted in the following observations:

Safety equipment, including lighting, was adequate

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Radiation dose rates were confinned to be as stated on the RWP and

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recent surveys

Wires impeding access on the 340' elevation to the ladder on the

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340' elevation (320/85-10-02)

The step-off pad at the top of the D-ring ladder presents a fall

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risk (320/85-10-03)

There were sheets of mirror insulation on the 349' elevation inside

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the D-ring. The insulation slows work in the area and presents a

potential increased contamination problem. The inspector will

follow licensee progress on removal of the material.

(320/85-10-04)

9.0 Routine Health Physics and Environmental Review

a.

Plant Tours

The NRC site radiation specialists perfonned routine plant

inspection tours. These inspections included all radiological

control points and selected radiologically controlled areas.

Items

inspected included:

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Access control to radiologically controlled areas

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Adherence to RWP requirements

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Proper use of respiratory protection equipment

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Adherence to radiation protection procedures

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Use of survey meters including personnel frisking techniques

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Cleanliness and housekeeping conditions

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Fire protection measures.

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No violations were identified. However, during a routine plant

walk-through inspection, the inspector noted a worker in the

personnel hatch anteroom in a relaxed position (sitting, leaning

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back against the wall, head resting on shoulder, eyes closed).

The

inspector noted a second worker speak to the worker.

The resting

worker seemed to respond appropriately.

The inspector noted that

both workers in the anteroom wore protective clothing and was

infonned by a licensee representative that these workers are

required to be present at the personnel hatch in order to make an

immediate entry in case of an emergency in the reactor building

(Procedure 4000-ADM-3240.01, Revision 1). The GPU Nuclear

Corporation Radiation Protection Plan (1000-PLN-4010.01, Revision 0)

states in Article 2 - Responsibilities of Workers, Item 18, that

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workers are to " Assure a mentally alert and physically sound

condition for performing assigned work." The suitability of

workers' condition for perfonning assigned work will be reviewed

during future inspections.

(320/85-10-05)

b.

Measurement Verification

Measurements were independently made by the inspector to verify the

quality of licensee performance in the areas of radioactive material

shipping, radiological control, radiation and contamination surveys,

and onsite environmental air and water sampling analyses. The

inspector reviewed the radiological controls applied within the

plant. Appropriate postings, surveys, and controls were observed

during inspector tours during day-shift and off-shift hours.

No violations were identified.

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c.

Reactor Building Entries

The site staff monitored RB entries conducted during the inspection

period. The inspection activities included review of selected

documents and direct observations of RB entries. The following

items were verified on a sampling basis.

The RB entry was properly planned and coordinated to assure

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that task implementation including adequate As Low As Is

Reasonably Achievable (ALARA) review, personnel training, and

equipment testing.

Radiological precautions were planned and implemented including

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the use of a RWP and specific work instructions.

Entries 583 through 614 were conducted during this inspection

period.

On May 15, 1985, the licensee removed the plenum assembly from the

reactor vessel. The plenum was placed under about 5 feet of

shielding water in the deep end of the fuel transfer canal in the

RB.

Radiological Controls included precautions for personnel access,

fall back provisions and area monitoring during the lift.

The

highest dose rate at the lift station atop the "A" D-ring was

30 mR/hr, double the normal readings.

No personnel were in

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line-of-sight of the plenum at any time that it was out of the

Total man-rem was 3.033; latching, 1.095 man-rem; the lift

water.

and transfer, 0.710 man-rem; and, unlatching,1.228 man-rem.

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highest dose rate recorded was 80 R/hr with the bottom of the plenum

directly above and about 4 feet from the detector.

Reactor Buil

airborne particulate radioactivity concentrations were 1.8 x 10'gng

uCi/cc, within the range noted during routine activities conducted

in the RB. The inspector observed the RB vent monitoring readout in

the Control Room during plenum removal.

Readings were within the

normal range.

No violations were identified,

d.

Radioactive Material Shipments

The NRC site radiation specialists inspected TMI-2 radioactive

material shipments during the inspection period to verify the items

listed below.

The licensee had complied with approved packaging and shipping

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procedures.

The licensee had prepared shipping papers, which certifieu that

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the radioactive materials were properly classified, described,

packaged, and marked for transport.

The licensee had applied warning labels to all packages and had

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placarded vehicles.

The licensee had controlled the radioactive contamination and

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dose rates below the regulatory limits.

Inspector review of this area consisted of (1) examination of

shipping papers, procedures, packages, and vehicles, and (2) performance

of radiation and contamination surveys of the shipments which were

inspected.

No violations were identified

10.0 _ Security

THESE PARAGRAPHS, CONTAINING SAFEGUARDS INFORMATION, NOT FOR PUBLIC

DISCLOSURE, ARE INTENTIONALLY LEFT BLANK.

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11.0 Inspector Follow Items

Inspector follow items are inspector concerns or perceived weaknesses in

the licensee's conduct of operation (hardware or programmatic) that could

lead to violations if left uncorrected.

Inspector follow items are

addressed in paragraphs 2, 9 and 10.

12.0 Unresolved Items

Unresolved items are findings about which more information is needed to

ascertain whether they are violations, deviations, or acceptable.

Unresolved items are addressed in paragraph 2.

13.0 Exit Interview

The inspectors met periodically with licensee representatives to discuss

inspection findings. On May 22, 1985, the inspector summarized the

inspection findings to the following personnel at the exit meeting:

J. Auger, Licensing Engineer

J. Byrne, Manager, Licensing TMI-2

W. Craft, (Acting) Manager, Radiological Field Operation

S. Levin, Site Operations Director

F. Standerfer, Vice President / Director, TMI-2

At no time during the inspection was written material provided to the

licensee by the TMIPO staff except for procedure reviews pursuant to

Technical Specification 6.8.2.

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