ML20125B386

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Ro:On 711120,trip Setting of ECCS Pump Start Permissive Switch Ps 2-3-53A,switch 2,found to Be 438 psig,12 Psi Below Required Trip Setting of 450 Psig.Caused by Large Air Gap. New Switches Designed for 125-volt Dc Use Will Be Purchased
ML20125B386
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 12/20/1971
From: Mayer L
NORTHERN STATES POWER CO.
To: Morris P
US ATOMIC ENERGY COMMISSION (AEC)
References
NUDOCS 9212090339
Download: ML20125B386 (3)


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Dear Dr. Morris:

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gr rgb WNTICELLO f;UCLEAR GENERATING PLANT Docket No. 50263 License No. DPR-22 C#

Failure of ECCS Pump Start Per nissive Switch and Relay A condition has occurred recently at the Monticello Nucitar Generating Plant which we interpret to be reportable in accordance with Section 6.6,0.1 of the Tcchnical Speci ficalions.

The Region iIi Compiiance office has bcon notified of thi s event.

Summar v of Occur r ence On November 20, 1971, whilc performing a regularly scheduled surveillance test, the trip setting of f CCS pump start permissive switch PS 2-3-53A, switch #2 was found to be 433 psig,12 psi belew the required trip cetting of A450 p,sig.

During thir survcillance test it was also discovered that a relay in the ECCS pump start pcrmissive logic failed to energize with the pump start permissive switch PS 2-3-53A, switch #1, closed.

An investigation of this occurrence revealed that the two switches contained in PS 2-3-53A were not designed for the 125V DC application for which they were being used.

This investi ation also revealed that the air cup on the failed C

relay was too large requiring a hi h pull-in voltage to energize the relay.

C New owitches desi ned for 125V DC use will be purchased and installed for all C

instruments of this type.

The pump permissive switches have been calibrated to tr ip at 460 psic, to allow for setpoint drift.

The relay air gap was reduced and the pull-in voltage was adjusted to less than 80fe of rated voltaCe. The relay was tested and found to operate satisfactorily.

Surveillance testing of this instrumcnt will be performed more frequently until the drif t problems have been corrected.

The correct relay pick up voltage setiirg will be vcrificd with the manufacturer and the setiings adjusted as necessary on this and all similar relays.

56/5 5

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2 A Si ni ficant Optrat ing I. vent repoi t has l>een wr itten for this occurrence C

and wil; Le available to the Recion lli Ccepliance inspec t or for review durire hir next visit.

Yours very truly,

[. M L. O. Mayer Director of Nml<:ar Support Serviceo LO'//Gi1J/mm m-u mium i