ML20116G961
| ML20116G961 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 10/31/1992 |
| From: | David Jones, Sieber J DUQUESNE LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9211120203 | |
| Download: ML20116G961 (9) | |
Text
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Telephone (412) 393-6000 Nuclear Group P O Box 4 Shepptrigport. PA 1%)77 00LM Noverter 9,1992 Beaver Valley Pctser Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operatinct Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555 Gentlemen:
In accordance with Appendix A,
Technical Specifications, the Monthly Operating Report is subnitted for Unit 1 and Unit 2 for the month of October, 1992.
Very truly yours, r,
W
. D. Sieber Vice President Nuclear Group DTJ/rmg Enclosures cc: NRC Regional Office King of Prussia, PA i
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_g ADOCK 05000334
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NARPATIVE
SUMMARY
OF MONIELY OPERATING EXPERID1CE UNIT 1 OCIOBER 1992 October 1 The Unit operated at approximately 90% output in accordance through with the planned fuel cyc'le length extension.
Octotnr 8 October 9 At 1652 hours0.0191 days <br />0.459 hours <br />0.00273 weeks <br />6.28586e-4 months <br /> the Unit experienced a reactor trip due to trip of the "A" Reactor Coolant Punp caused by an electrical ground internal to the motor.
October 10 The Unit entered Mode 4 at 1510 hours0.0175 days <br />0.419 hours <br />0.0025 weeks <br />5.74555e-4 months <br /> while cooling down to permit repairs to the "A" Reactor Coolant Pump motor.
October 11 At 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> the Unit entered Mode 5 in preparation for repairs to the "A" Reactor Coolant Pump motor.
October 12 The Unit remained in Mode 5 as repairs to the "A" Reactor through coolant Pump continued.
October 29 October 30 Following conpletion of repairs to the "A" Reactor Coolant
- Pump, the Unit began to heatup ard entered Mode 4 at 2040 hours0.0236 days <br />0.567 hours <br />0.00337 weeks <br />7.7622e-4 months <br />.
October 31 The Unit entered..ade 3 at 0705 hours0.00816 days <br />0.196 hours <br />0.00117 weeks <br />2.682525e-4 months <br /> as startup continued, and remained in this mode for the remainder of the report period.
r
AVEPM E DAILY UNIT FGiER IE/EL DOOTT NO.
50-334 UNIT-BVPS Unit 1 DATE Nov. 2. 1992 COMPLEIID BY Deid T. Jones TELElHONE (412) 393-7612 M0! TIE Octooer 199R__
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POhTR LEVEL (MWe-Net)
(Mie-Net) 1 738 17 0
2 733 18 0
3 717 19 0
4 729 20 0
5 733 21 0
6 729 22 0
7 733 23 0
8 725 24 0
9 503 25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 0
1 14 0
30 0-15 0
31 0
j 16 0
!l' INSEUCTIONS On this forraat, list the average daily unit power level MWe-Net for each da/ in the reporting renth. Coqmte to the nearest whole megawatt.
OPERATING DATA REPORT.
DOCKET NO.:
50 334 REPORT DATE:
11/04/92 COMPLETED BY:. DAVID T. JONES TELEPHONE:
l(412)-393 7612 OPERATING STATUS
- 1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 1 Notes
- 2. REPORTING PERIOD:.0CTOBER 1992
- 3. LICENSED THERMAL POWER (MWe):
2652
- 4. NAMEPLATE RATING (Gross MWe):
923
- 5. DESIGN ELECTRICAL RATING (Net MWe):
835
- 6. MAX. DEPENDABLE CAPACITY (Gross MWe):
860
- 7. MAX. DEPENDABLE CAPACITY (Net MWe):
810
- 8. IF CHANGES OCCUR IN CAPACITI RATINGS SINCE LAST REPORT, GIVE REASONS:
- 9. POWER LEVEL TO VHICH RESTRICTED, IF ANY (Net MWe):
None 10, REASONS FOR RESTRICTIONS,-IF ANY:
N/A THIS MONTH YEAR TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD:
745.0 7320.0 144672,0
- 12. NO. OF HRS. REACTOR WAS CRITICAL:
208.9 6783.9 92107.5
- 13. REACTOR RESERVE SHUTDOWN HOURS:
0,0 0.0 4482.8 14'. HOURS GENERATOR WAS ON LINE:
208.9 6783.9 90215.1
- 15. UNIT RESERVE SHUTDOWN HOURS:
0.0 0.~ 0 0.0-
- 16. CROSS THERMAL ENERGY GEN. (MWH):
494631.0 17073611.0-215585787i5-
- 17. CROSS ELECT. ENERGY GEN. (MWH):
162340.0 5583100.0 69381503.0
- 18. NET ELECTRICAL ENERGY GEN. (MWH):
143230.0.
5252000.0-64819550.0
- 19. UNIT SERVICE FACTOR: (PERCENT)
- 28.0 92.7 64.4-
- 20. UNIT AVAILABILITY FACTOR:(PERCENT) 28.0 92.7 64.4i
- 22. UNIT CAPACITY FACTOR (DER): PCT 23;0-85.9 56.3
- 23. UNIT FORCED.0UTAGE RATE: (PERCENT).
72.0 7.3 16.1
- 24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE,DATE,AND DURATION:0F EACH):
THE UNIT IS SCHEDULED TO SHUTDOWN FOR ITS NINTH REFUELIt4u GUTAGE ON APRIL 2. 1993.
THE REFUELING OUTAGE IS SCHEDULED TO LAST FOR 70 DAYS.
- 25. IF SMUT DOWN AT END OF REPORT ~ PERIOD, ESTIMATED.DATE OF STARTUP:
-26. UNITS IN' TEST STATUS (PRIOR TO COMMERCIAL.0PERATION):
FORECAST ~
ACHIEVED INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A
UNIT SHUTDOWNS AND POWER REDUCTIO 45 (220%)
Doc ke t No.
50-334 Unit Name BVPS Unit #1 Date November 4 1992 Completed By David T.
Jones REPORT MONTH OCTOBER 1992 Telephone (412) 393-7612 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action to No.
Date Type 1 (Hours)
Reason 2 Down Reactor 3 Report #-
Code 4 Code 5 Prevent Recurrence -
15-921001 S
0 N
4 N/A ZZ ZZZZ2Z unit continued to operate at a reduced output of approximately 90%
in accordance with the planned fuel cycle tength extension.
16 921009 F
536.1
, A 3
92-009-00 C8 MOTORX Unit experienced a reactor trip due to a trip of the "A" Reactor Coolant Pump caused by an electrical ground internat to the motor.
1 2
3 4
F-Forced Reason:
Method:
Exhibit F-Instructions for S-Schedoted A-Equipment Faiture (Explain) 1-Manual Preparation of Data Entry Sheets 8-Maintenance or Test 2-Manual Scram for Licensee Event Report (LER) File C-Refueling 3-Automatic Scram (NUREG0161).
-D-Regulatory Restriction 4-Cont'd. from Previous Month E-Operator Training & License Exam 5 Reduction 5
F - Admini st rat ive 9-Other Exhibit H-Same Source.
G-Operational Error (Explain)
H-Other (Explain) a v
-w'
+
' NARRATIVE
SUMMARY
OF
^
M0 tin {LY OPERATING D(PERID1CE
?>
UNIT 2-OCTOBER 1992 October 1-
'Ihe Unit operated at a nominal value of 100% output during through the entire-report period.
October 31 t
I
p 4
AVERAGE DAILY UNIT Poh'ER LWEL DOCKET No.
50-412 UNIT BVPS Unit 2 DATE Nov. 2, 1992 COMPLEIID BY David T. Jones TELEPHONE (412) 393-7612-MONIH October 1992 DAY AVERAGE DAILY PCWER LEVEL DAY AVERAGE DAILY PONER LEVEL (M0e-Net)
(MWe-Net)'
1 836 17 841 2
835 18 841 3
832 19 841 4
837 20
'842 5
841 21 838 6
841 22 841 7
839 23 839 8
836 24 835 9
836 25 839 10 837 26 834 11 838 27 836' 12 838 28 836 13 840 29 835
- 14 836 30 837 15 830 31 836
- 16 834 HISIRJCTIONS On this format, list the average daily unit power level MWe-Net for each day =in the reporting month. Corpute to the nearest whole megawatt.
OPERATING DATA REPORT DOCKET No.:
50 412 REPORT DATE:
11/04/92 COMPLETED BY: DAVID T. JONES TELEPHONE:
(412) 393-7612 OPERATING STATUS
- 1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 2 Notes
- 2. REPORTING PERIOD: OCTOBER 1992
- 3. LICENSED THERMAL POWER (MWt):
2652
- 4. NAMEPLATE RATING (Gross MWe):
923
- 5. DESIGN ELECTRICAL RATING (Net MWe):
836
- 6. MAX. DEPENDABLE CAPACITY (Gross MWe):
870
- 7. MAK. DEPENDABLE CAPACITY (Net MWe):
820 8.
IF CHANGES OCCUR IN CAPACITY RATINGS SINCE LAST REPORT, GIVE REASONS:
9.
POWER LEVEL TO WHICH RESTRICTED. IF ANY (Net MWe):.
None
- 10. REASONS FOR RESTRICTIONS, IF ANY:
N/A THIS MONTH YEAR TO 9 ATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD:
745.0 7320.0 43455.0
- 12. NO. OF HRS REACTOR WAS CRITICAL:
745.0 5957.0 37037.2
- 13. REACTOR RESERVE SHUTD0k. HOURS:
0.0 0.0 0.0
- 14. HOURS GENERATOR WAS ON LINE:
745.0 5879.3 36761.3-
- 15. UNIT RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 16. GROSS THERMAL ENERGY GEN. (MWH):
1960015.0 14723406.0 90083153.4
- 17. CROSS ELECT. ENERGY GEN. (MWH):
656209.0 4817768.0 28992349.0
- 18. NET ELECTRICAL ENERGY GEN. (MWH):
623846.0 4553534.0 27359019.0
- 19. UNIT SERVICE FACTOR: (PERCENT) 100.0 80.3 84,6
- 20. UNIT AVAILABILITY FACTOR:(PERCENT) 100.0 80.3 84.6
- 22. UNIT CAPACITY FACTOR (DER): PCT 100.2 74.4 75.3
- 23. UNIT FORCED OUTAGE RATE: (PERCENT) 0.0 0.2 3.4
- 24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE,DATE,AND DURATION OF EACH):
- 25. IF SHUT'DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
- 26. UNITS IN. TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST-ACh_dVED INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A-COMMERCIAL OPERATION N/A-N/A
+
4 Us31T SNUTDOVNS AWD POWER REDUcitoWS (220%)
Docket No.
50-412 Unit Name BVPS Unit #2 Date. November 2. 1992 Completed 8y David T.
Jones REPORT MONTH OCTOBER 1992 Telephone (412) 393-7612 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action to No.
Date Typel (Nours)
Reason 2 Down Reactor 3 Report &'
Code 4 Code 5 Prevent Recurrence NONE 1
2 3
4 F-Forced Reason:
Method:
Exhibit F-Instructions for S-Scheduled
'A-Equipment 7aiture (Explain).
1-Panual Preparation of Data Entry Sheets B-Maintenance or Test 2-renual Scram for Licensee Event Report.(LER) File C-Refueling
.3-Automatic Scram (kURECD161).
D-ReJu'atory Restriction 4-Cont'd. from Previous Month E-Operstor Training & License Exam 5-Reduction 5
F-Administrative 9-Other Exhibit n-Same Source.
G-Operational Error (Explain}'
H-Other (Explain) m