ML20108B052
| ML20108B052 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 09/30/1984 |
| From: | Carey J, Holtz J DUQUESNE LIGHT CO. |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| NUDOCS 8411150289 | |
| Download: ML20108B052 (5) | |
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NARRATIVE ShMMARY OF MONTHLY OPERATING EXPERIENCE - SEPTEMBER, 1984 1
S;ptember 1-J
.The station was in operational mode.1 with reactor power a through nominal 100%. The reactor coolant system was at normal S:ptember 6
. operating ~ temperature and pressure.
'Saptember 7-
.The 1A heater drain pump was started at 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br /> following
-repacking. The pump tripped at 1429 hours0.0165 days <br />0.397 hours <br />0.00236 weeks <br />5.437345e-4 months <br /> on low heater drain tank level due to tank low level control valve, LCV-SD-106B, failing open.
-A ruptured diaphragm was the cause.
The loss
' of the heater drain. pump caused the IB main feedwater pump to begin vibrating. Tho'feedwater pump was shutdown at 1450 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.51725e-4 months <br /> and reactor power was stabilized at 58%. 'The pump was restarted at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> and reactor. power was increased to 100%.
. September 8 Permission was received at 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br /> from the DLCo. system operator to' reduce station load to 60% in order to remove the
'lB main.feedwater pump from service.
'A seal water line to the L
-pump was leaking. Repairs were made and the pump was restarted at 1010 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.84305e-4 months <br />. Station load was.being increased when the seal water line to the 1B main feedwater pump again began leaking.
Station load was reduced to 60% reactor power.
FW-P-1B was shutdown for repairs due to continued high vibration.
September 9 Repairs were being made to FW-P-18.
The pump was started and I
through shutdown.soveral times during the troubleshooting.
The repairs l
September 16 were completed at approximately 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on the 16th and the pump was started at 1206 hours0.014 days <br />0.335 hours <br />0.00199 weeks <br />4.58883e-4 months <br />. Reactor power ascension began at 1252 with holds at 5% increments for vibration readings on l
the IB main feedwater pump. Reactor power reached 100% at approximately 1830 hours0.0212 days <br />0.508 hours <br />0.00303 weeks <br />6.96315e-4 months <br />.
l September 17 The station was in operational mode 1 with reactor power a through nominal 100%.
September 28 September 29 The station experienced a 50 MWo load rejection at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> when rehoater steam supply valves FCV-MS-100A and C tripped shut. The valves were opened at 0938 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.56909e-4 months <br /> using the local nanual override. Reactor power was increased to 100%.
September 30 The station was in operational modo 1 with reactor power a nominal'100%.
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MAJOR MAINTENANCE - SEPTEMBER, 1984
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Replaced entire rotating assembly'in FW-P-1B.
2.
Repaired SD-P-1A.
3.
Repaired SD-P-1B.
4.
Repaired ruptured diaphragm on LCV-SD-106B.
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OPERATISG DATA REPORT DOCKET NO. 150-334 DATE _10-11-84 COMPLETED BY
_J.
L.
troltz TELEPHONE. 41?-443-_1369 OPERATING STATUS
- l. Unit Name: Beaver Valley Power Station. Unit #1 Notes
- 2. Reporting Period:
Senternbe r, 1984
- 3. Licensed Thermal Power (MWt):
74A0
- 4. Nameplate Rating (Gross MWe):
923 835
- 5. Design Electrical Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe):
860
- 7. Maximum Dependable Capacity (Net MWe):
810
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Give Reasons:
- 9. Power Level To Which Restricted.lf Any (Net MWe):
None
- 10. Reasons For Restrictions.lf Any:
N/A This Month Yr..to.Da t e
" Cumulative
- 11. Hours in Reporting Period 720 6,575 73,799
- 12. Number Of Hours Reactor Was Critical 720 6,221.3 37,100.7
- 13. Reactor Reserve Shutdown Hours 0
0 4,482.8
- 14. Hours Generator On Line 720 6,049.1 35,827.9
- 15. Unit Resene Shutdown Hours 1,674,388 15,150,170 82,739,709 0
0 0
- 16. Cross Thermal Energy Generated (MWH)
- 17. Cross Electrical Energy Generated (MWH) 526,000 4,855,500 26,284,400 IS. Net E!cetrical Energy Generated (MWH) 491,190 4,553,825 24,442,713
- 19. Unit Senice Factor 100.0 92.0 51.0
- 20. Unit Asailability Factor 100.0 92.0 51.0
- 21. Unit Capacity Factor (Using MDC Net) 84.2 85.5 44.6
- 22. Unit Capacity Factor (hing DER Net) 81.7 82.9 43.2
- 23. Unit Forced Outage Ra 0
3.1 27.2
' 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.snd Duration of Each t:
Scheduled shutdown:
October 13 for 4th refuelin<7 Scheduled duration:
66 days 25 If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test StatusIPrior to Commercial Operationi:
Forecast Achieved INITIA L CRITICA LITY V/A N/A INITIA L ELECTRICITY N/A N/A COM%IEP.CI A L OPERATION N/A N/A (9/77)
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- o AVERACE D AILi UNIT POWER LEVEL.
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DOCKET NO' 50-334~
. UNI'T EV?S Uni 41'--
-DATE Oct. 11, 1994 i
.. Holtz
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COMPLETED BY _
J.
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TELEPHONE (412) 643-138 l-L 5
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MONTH sentomber
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DAY AVERAGE DAILY POWER LEVEL DAY
- AVERAGE DAILY POWER LEVEL.
l lMWe-Net)
(MWe-Net p.
l i
[
g 784 g7 783 2
784 gg 784 l-3 743 39 783
[
(
4 783 20 741 5
784 2}
784 6
794 n.
742 7
701 23 783 j
.8 620 34 783 9
413 23 742 i
10 414 26 783 lj 455 27 784 12 414 23 R74 13 414 29 794 14 456 30 794
- 15 415 33 16 620 l
INSTRL'CTIONS On this format, hs the average d: iv unit po ser !cw! in MWe. Net let each day an the reputting montn. 0nnt:ute f u the ne:re:t wnule mepwart.
($1/77 )
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Telephone (412) 393-6000 Nuclear Division P.O. Box 4 Shippingport, PA 15077-0004 October 11, 1984 Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 Monthly Operating Report United States Nuclear Regulatory Commission Director, Office of Management Information & Program Control Washington, D. C.
20555 Gentlemen:
In accordance with Appendix A, Technical Specifications, the Monthly Operating Report is submitted for the month of September, 1984.
Very truly yours, n
h Carey Vic President Nuclear Group Enclosures cc NRC Regional Office, King of Prussia, PA h
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