ML20101S908

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Informs That Work Has Been Completed Re Enhancement of Electrical Components Which Support Feed & Bleed Cooling Capability Functions Following Seismic Event
ML20101S908
Person / Time
Site: Davis Besse 
Issue date: 07/13/1992
From: Shelton D
CENTERIOR ENERGY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
2058, NUDOCS 9207200139
Download: ML20101S908 (2)


Text

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h"" Inky Donald C. Shelton 300 W A m mpg,w Toledo, OH 436520)01 gg (419)249 2300 Docket Number 50-346 License Number NPF-3 Serial Number 2058 July 13,'1992 United States Nuclear Regulatory Commission Document Control Desk Vashington, D. C.

20555 Subj ec t :

Status of Commitments for the Feed and Bleed Modification Gentlemen:

As recently discussed with Mr. Jon B. Hopkins (NRC Senior Project Manager), Toledo Edison submitted a letter (Serial Number 1836) dated September 18, 1990 which summarized the numerous modifications made for enhancing the feed and bleed cooling capability for the primary syatem of the Davis-Besse Nuclear Power Station (DBNPS).

Although feed and bleed cooling would only be required in a be ond-design basis. event, Toledo Edison committed to enhance the electrical components which support the feed and bleed cooling capability, to be functional following a seismic event.

In this letter, Tcledo Edison stated that the work had been completed to enhance the necessary electrical components for a seismic event.

During the modification closeout process by Toledo Edison, two relay 9

cabinets were identified as missing seismic supports and fou. conduits needed rework and tightening to meet Seismic Qualification Utility Group (SOUG) or seismic class I criteria.

Vork had also not been completed to de-terminate and spare a cable's ground shield.

A nonconformance report was written to initiate corrective action to 3

correct these discrepant items' capability for feed and bleed. As part of the corrective actions for the nonconformance report, a reviev was performed to identify if additional work vas still outstanding and required completion.

Based upon this review, no further outstanding work was found to need completion.

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Commensurate with outage scheduling and parts availability, this remaining vork is planned to be completed by the end of the eighth refueling outage (RRF0) scheduled for Spring, 1993.

As previously

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stated in Toledo Edison's letter (Serial Number 1938) dated May 17, 1991, environmentally qualified AC povered bearing lube oil pump motors vill also be installed during the 8RFO. Vith the exception of the items' described above for completion by the end of 8RF0, Toledo Edison considers that the modifications made during the fifth and sixth refueling outages satisfy the previous commitments with respect to enhancing the feed and bleed capability at the DBNPS.

If you have any questions regarding this matter, please contact Mr. R. V. Schrauder Manager - Nuclear Licensing, at (419) 249-2366.

Very tru

yours, W

RAS /dle d.B Davis, Regional Administrator, NRC Region III

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cc:

b. Hopkins, NRC/NRR DB-1 Senior Project Manager V. Levis, NRC Region III, DB-1 Senior Resident Inspector Utility Radiological Safety Board

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