ML20101D051

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Revised Monthly Operating Rept for Jan 1996 for Comanche Peak Steam Electric Station Unit 1
ML20101D051
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 01/31/1996
From: Reible B
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To:
Shared Package
ML20101D045 List:
References
NUDOCS 9603190353
Download: ML20101D051 (2)


Text

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Attachment to TXX 96073 P'a9e 9 of 11 COMA (CHE PEAK STEAM ELECTRIC STATION. UNIT 1 i

NRC MONTHLY OPERATING REPORT l

REV. 1 DOCKET NO.:

50 445 l

UNIT:

CPSES 1 DATE:

3/11/96 COMPLETED BY:

Bob Reible TELEPHONE:

817 897 0449 OPERATING STATUS 1.

REPORTING PERIOD:

JANUARY 19%

GROSS HOURS IN REPORTING PERIOD:

744 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWt):

3411 MAX. DEPEND. CAPACITY (MWe Net):

1150 DESIGN ELECTRICAL RATING (MWe Net):

1150 3.

POWER LEVEL TO WHICH RESTRICTED (IF ANY) (HWe Net):

NONE l

4.

REASON FOR RESTRICTION (IF ANY):

l THIS MONTH YR TO DATE CUMULATIVE

)

5.

NUMBER OF HOURS REACTOR WAS CRITICAL 443 443 39.195 i

6.

REACTOR RESERVE SHUTDOWN HOURS 0

0 2.604 l

7.

HOURS GENERATOR ON LINE 438 438 38.627 8.

UNIT RESERVE SHUTDOWN HOURS 0

0 0

9.

GROSS THERMAL ENERGY GENERATED (MWH) 1.426.730 1.426.730 124.851.983

10. GROSS ELECTRICAL ENERGY GENERATED (MWH) 481.186 481.186 41.547.389
11. NET ELECTRICAL ENERGY GENERATED (HWH) 450.558 450.558 39.617.751 1
12. REACTOR SERVICE FACTOR 59.6 59.6 81.7
13. REACTOR AVAILABILITY FACTOR 59.6 59.6 87.2
14. UNIT SERVICE FACTOR 58.9 58.9 80.6
15. UNIT AVAILABILITY FACTOR 58.9 58.9 80.6
16. UNIT CAPACITY FACTOR (USING MDC) 52.7 52.7 71.9 l
17. UNIT CAPACITY FACTOR (USING DESIGN MWe) 52.7 52.7 71.9 l
18. UNIT FORCED OUT.'GE RATE 41.1 41.1 5.1 f
19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):

i

]

20.

IF SHUTDOWN AT END OF REPORTING PERIOD. ESTIMATED DATE OF STARTUP:

2/ 4/96 l

21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

ACHIEVED i*

COMMERCIAL OPERATION 900813 9603140353 960315 1-ESTIMATED PDR ADOCK 050004AS R

PDR

Attachment to TXX-75073 Page 10 of 11 UNIT SHUTDOWNS AND POWER REDUCTIONS REV. 1 DOCKET NO.:

50-445 UNIT:

CPSES 1

DATE:

2/ 9/96 COMPLETED BY:

Bob Reible TELEPHONE:

817-897-0449 REPORT MONTH:

JANUARY 1996 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO DATE 5: SCHEDULED (HOURS)

REASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS 1

960117 F

73.9 A

3 Rx trip and SI actuation due to instrument spike while re-energizing failed inverter IV1PC2. See previous page. LER 445/96-091-00 2

960122 F

231.9 A

2 Manual RX trip after loss of power to bus 1EC1 due to IV1EC1 Inverter failure. See previous page. LER 445/96-002-00.

1)

REASON 2)

METHOD A:

EQUIPMENT FAILURE (EXPLAIN)

E:

OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B:

MAINT OR TEST F:

ADMINISTRATIVE 2: MANUAL SCRAM C:

REFUELING G:

OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D:

REGULATORY RESTRICTION H:

OTHER (EXPLAIN) 4: OTHER (EXPLAIN)

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