ML20101D051
| ML20101D051 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 01/31/1996 |
| From: | Reible B TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| To: | |
| Shared Package | |
| ML20101D045 | List: |
| References | |
| NUDOCS 9603190353 | |
| Download: ML20101D051 (2) | |
Text
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Attachment to TXX 96073 P'a9e 9 of 11 COMA (CHE PEAK STEAM ELECTRIC STATION. UNIT 1 i
NRC MONTHLY OPERATING REPORT l
REV. 1 DOCKET NO.:
50 445 l
UNIT:
CPSES 1 DATE:
3/11/96 COMPLETED BY:
Bob Reible TELEPHONE:
817 897 0449 OPERATING STATUS 1.
REPORTING PERIOD:
JANUARY 19%
GROSS HOURS IN REPORTING PERIOD:
744 2.
CURRENTLY AUTHORIZED POWER LEVEL (MWt):
3411 MAX. DEPEND. CAPACITY (MWe Net):
1150 DESIGN ELECTRICAL RATING (MWe Net):
1150 3.
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (HWe Net):
NONE l
4.
REASON FOR RESTRICTION (IF ANY):
l THIS MONTH YR TO DATE CUMULATIVE
)
5.
NUMBER OF HOURS REACTOR WAS CRITICAL 443 443 39.195 i
6.
REACTOR RESERVE SHUTDOWN HOURS 0
0 2.604 l
7.
HOURS GENERATOR ON LINE 438 438 38.627 8.
UNIT RESERVE SHUTDOWN HOURS 0
0 0
9.
GROSS THERMAL ENERGY GENERATED (MWH) 1.426.730 1.426.730 124.851.983
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWH) 481.186 481.186 41.547.389
- 11. NET ELECTRICAL ENERGY GENERATED (HWH) 450.558 450.558 39.617.751 1
- 12. REACTOR SERVICE FACTOR 59.6 59.6 81.7
- 13. REACTOR AVAILABILITY FACTOR 59.6 59.6 87.2
- 14. UNIT SERVICE FACTOR 58.9 58.9 80.6
- 15. UNIT AVAILABILITY FACTOR 58.9 58.9 80.6
- 16. UNIT CAPACITY FACTOR (USING MDC) 52.7 52.7 71.9 l
- 17. UNIT CAPACITY FACTOR (USING DESIGN MWe) 52.7 52.7 71.9 l
- 18. UNIT FORCED OUT.'GE RATE 41.1 41.1 5.1 f
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):
i
]
20.
IF SHUTDOWN AT END OF REPORTING PERIOD. ESTIMATED DATE OF STARTUP:
2/ 4/96 l
- 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
ACHIEVED i*
COMMERCIAL OPERATION 900813 9603140353 960315 1-ESTIMATED PDR ADOCK 050004AS R
Attachment to TXX-75073 Page 10 of 11 UNIT SHUTDOWNS AND POWER REDUCTIONS REV. 1 DOCKET NO.:
50-445 UNIT:
CPSES 1
DATE:
2/ 9/96 COMPLETED BY:
Bob Reible TELEPHONE:
817-897-0449 REPORT MONTH:
JANUARY 1996 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO DATE 5: SCHEDULED (HOURS)
REASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS 1
960117 F
73.9 A
3 Rx trip and SI actuation due to instrument spike while re-energizing failed inverter IV1PC2. See previous page. LER 445/96-091-00 2
960122 F
231.9 A
2 Manual RX trip after loss of power to bus 1EC1 due to IV1EC1 Inverter failure. See previous page. LER 445/96-002-00.
1)
REASON 2)
METHOD A:
EQUIPMENT FAILURE (EXPLAIN)
E:
OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B:
MAINT OR TEST F:
ADMINISTRATIVE 2: MANUAL SCRAM C:
REFUELING G:
OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D:
REGULATORY RESTRICTION H:
OTHER (EXPLAIN) 4: OTHER (EXPLAIN)
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