ML20099E907
| ML20099E907 | |
| Person / Time | |
|---|---|
| Site: | McGuire, Mcguire |
| Issue date: | 10/31/1984 |
| From: | Reavis J, Tucker H DUKE POWER CO. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| NUDOCS 8411260134 | |
| Download: ML20099E907 (12) | |
Text
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a OPERATLNG DATA REPORT DOCKET NO. 50-369 DATE 11-15-84_
COMPLETED BY
.T A nnavis TELEPHONE 7na-373 7567 OPERATING STATUS
- 1. Unit Name:
McGuire 1 Notes
- Nameplate Rating
' 2. Reporting Period: October 1.1984-October 31. 1984 (Gross MWe) calculated as
- 3. Licensed Thermal Power ISIW ):
3411 1450.000 MVA x.90 power
- 4. Nameplate Rating (Gross alWe):
1305*
factor per Page 111, NUREG-0020.
1180
- 5. Design Electrical Rating (Net MWe):
- 6. Masimum Dependable Capacity (Gross MWe):
- 7. Masimum Dependable Capacity (Net SIWE):
0
- 8. If Changes Occur in Capacity Ra:Ings (Items Number 3 Through 7) Since Last Report.Give Reasons:
None
- 9. Power Letel To hhich Restricted. lf Any (Net MWe):
N "*
- 10. Reasons For Restrictions.lf Any:
' This Month Yr..to.Date Cumulative
- 11. Ilours in Reporting Period 745 0-7 't?n_n
.?s saa n
- 12. Number Of floun Reactor Was Critical 647.0 5 450.1 17 523.1
- 13. Reactor Resene Shutdown llours
- 14. Ilours Generator On Line 643.2 5 383.0
_17 332.1
- 15. Urdt Resene Shutdown flours
- 16. Cross Thermal Energy Generated (MWil) 2 042 345
,,H_3]7 508 45 024 577
.17. Gross Electrical Energy Generated (MWH) 700 923 6 192 462 15 619 627
- 18. Net Electrical Energy Generated (MWil) 670 003 5 f47 016 14 803 271
- 19. Unit Senice Factor 86 3 73.5 67.8
- 20. Unit Avadability Factor 86.3 73,5 67.8
- 21. Unit Capacity Factor IUsing MDC Net!
76.2.
67.7 49.0
- 22. Unit Capacity Factor (Using DER Net) 76.2 67.7 49.0
- 23. Unit Forced Outage Rate 13.7 5.6 16.4
- 24. Shutdowns Seheduled Oser Nest 6 Months IType.Date..and Duration of Eacht:
Maintennnce Outnge - November 24. 1984 - 4 Wooks Refueling Outage - March 9, 1985 - 7 Weeks
- 25. If Shut Down At End of Report Period. Estimated Date of Startup:
- 26. Units in Test Status t Prior to Commerci.il Operation):
Forecast Achleted INiil \\ L CRITICA LliY INITl \\ L ELECTRICITY C0\\lMERCl \\L OPER ATION l
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AVERAGE DAILY UNIT-POWER LEVEL
-dOCKETNO.
50-N9 UNIT Menuire 1
>DATE 11/is/a4 COMPLETED BY.
J.A. Reavis
- TELEPHONE '.
704 373-7567 9
i MONTH
' October, 1984 l'
DAY' AVERAGE' DAILY POWER LEVEL' DAY.
AVERAGE DAILY POWER LEVEL li l
(MWe-Net)-
(NWe-Ne t)
):;
i.' ~
1 1 137
-17 1'137 s
2 1 138 18 1 136 3
1 140 19 1 139 4
1 139 20 1 141 5
1 138 21 1 142 l
6 1 138 22 1 095 7
1 137 23 576 l
8 1 139 24 667 9
1 139 25 551-10 t ino 26 202 l
11 1 136 27 l
12 1 133 28 13 1 137 29 337 14 1 140 30 695 t
l 15 1 119 31 16 1 139 l
INSTRUCTIONS l
On this format, list the averago dally unit power level in NWe-Net for each day l-In the reporting month. Compute to the nearest whole megawatt.
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UNIT SHUTDOW'4S AND POWER REDUCTIONS DOCKET NO. so-3sg UNIT NAME Mecuire i DATE 11/1s/84 REPORT MONTH october 1984 COMPLETED BY J.
- a. neavis TELEPHONE 704-373-7567 "s_o
'g j License y
Cause & Corrective e32 a5E
~
c No.
Date gh g
jgc Event
,5e, h
Action to
~.5 YE E
%E$
RE 8E F
o~
a:
- c m o Report #
mv vu Prevent Recurrence 36-P 84-10-21 S
B IB INSTRU Preparing for Incore/Excore Calibrations 37-P 84-10-22 F
A CH PLHPXX Dirty Feedwater Pump Control Oil Filter 38-P 84-10-22 F
A AA HTEXCH High Lower Containment Temperatures 39-P 84-10-23 F
A l
CH PUMPXX Feedwater Pump Control Oil Problem 40-P 84-10-24 F
A AA HTEXCH High Lower Containment Temperatures 9
84-10-26 F
71.78 A
1 AA HTEXCH Rod-out Ventilation Units 10 84-10-30 F
30.03 A
1 SG upper Head Injection Chemistry Problems l
l l
1 2
3 4
Reason:
l rc Met 1xxl:
Exhibit G - Instructions 3
g A-Equipment Failure (Explain) 1-Manual for Preparation of Data l
B-lhintenance or Test 2-Manual Scram Entry Sheets for Licensee i
C-Refueling 3-Automatic Scram Event Report (LER) l D-Regulatory Restriction 4-Other (Explain)
File (NIREG-0161)
E-Operator Training 4 License Examination F-Adainistrative 5
G-Operational Error (Explain)
Exhibit I - Same Source H-Other (Explain) l(9m)
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' 'j-i DOCKET NO:
50-369 UNIT: McGuire-1 DATE:
11/15/84 NARRATIVE
SUMMARY
. Month:
October 1984 Unit was at 974 power for incore/excore instrumentation calibration when Lower containment temperature forced unit to plan a shutdown to clean the coolers.
The unit was at 50% when Unit 2 tripped, forcing Unit 1 to remain on-line..
The unit's "A" feedpump developed problems with the control oil system and prevented the unit from escalating power. Lower Containment temperatures--
remained high and when unit 2 returned to service, unit 1 shutdown to clean-its containment coolers. After the unit returned to service, excessive Nitorgen was discovered in the Upper IIcad Injection Water accumulator. The' unit shutdown to drain and refill the accumulator.
s MONTHLY REFUELING INFORMATIF. REQUEST 1.
Facility name:
McGuire Unit 1 2.
Scheduled next refueling shutdown:
March 1985 3.
Scheduled restart following refueling:
May 1985 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Yes If yes, what will these be?
Technical Specification Revision If no, has reload design and core configuration been reviewed by Safety Review Committee regarding unreviewed safety questions?
N/A 5.
Scheduled date(s) for submitting proposed licensing action and supporting information:
N/A 6.
Important licensing considerations (new or different design or supplier, unreviewed design or performance analysis methods, significant changes in design or new operating procedures).
N/A 7.
Number of fuel assemblies (a) in the core:
193 (b) in the spent fuel pool:
91 8.
Present licensed fuel pool capacity:
1463 Size of requested or planned increase:
9.
Projected date of last refueling which can be accommodated by present licensed capacity:
DUKE POWER COMPANY Date:
November 15, 1984 Name of
Contact:
J. A. Reavis Phones 704-373-7567 1
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OPERATING DATA REPORT DOCKET NO.
50-370 DATE 11-15-84 COhlPLETED BY J.A. Reavis TELEPHONE 7na-173-7567
.b OPERATING STATUS
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Notes
- Nameplate Rating
- 1. Unit Name:
Mecuire 2 (Gross MWe) calculated as 2.- Reporting Period: October 1. 1984-October 31. 1984 1450.000 MVA x.90 power
- 3. Licensed Thermal Power (31Wt):
3411 "98 130S*
- 4. Nameplate Rating (Gross SIWE):
1180-
' 5. Design Electrical Rating (Net alWe):
- 6. Staximum Dependable Capacity (Gross alWe):
1180
- 7. blatimum Dependable Capacity (Nat SlWe):
8.- If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Give Reasons:.
None-
.Nono
- 9. Power Level To Which Restricted,if Any (N-t alWe):
- 10. Reasons For Restrictions,if Any:
J This >tonth Yr..to-Date Cumulative 745.0 5 880.0
-5 880.0 I1. Hours In Reporting Period 687.8 4 838.0 4 R1R.n
- 12. Number Of Hours Reactor Was Critical
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator On-Line 684.4 4 805.6 4 805.6
- 15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (alWH) 2 260 438 15 828 348 15 828 348
.17. Gioss Electrical Energy Generated (alWH) 792 780 5 603 564 5 603 564
- 18. Net Electrical Energy Generated (alWH) 761 721 5 381 573 5 381 573
- 19. Unit Service Factor 91.9 81.7 81.7 91.9 81.7 81.~ 7
- 20. Unit Availability Factor
- 21. Unit Capacity Factor (Using SIDC Net) 86.7 77.6-77.6
- 22. Unit Capacity Factor (Using DER Net) 86.7 77.6 77.6 1
- 23. Unit Forced Outage Rate 8.1 17.1 17.1
- 24. Shutdowns Scheduled Over Next 6 Stonths (Type. Date.and Duration of Eacht:
' Maintenance Outage - November 15, 1984 - 4 Days Refueling Outage - January 1,1985 - 8 Weeks
- 25. If Shut Down At End Of Report Perind. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Coms.ercial Operation):
Forecast Achieved INITIAL CRITICA LITY INITIAL ELECTRICITY CO\\lMERCIAL OPERATION (0/77) m
/
AVERAGE DAILY UNIT POWER LEVEL l
DOCKET NO.
50-370 UNIT McGuire 2 DATE 11/1s/g4 COMPLETED BY J.A. Reavis TELEPHONE 704-373-7567 MONTH October, 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Ne t)
I 1 156 17 1 155 2
1 156 18 1 156 3
1 156 19 1 105 0
1 155 20 1 156 I 1s6 21 1 158 6
1 1s6 22 1 156 7
1 15s 23 201 0
1 155 24 9
1 154 25 39 10 1 154 26 1 074 11 1 128 27 1 154 12 1 156 28 1 200 13 679 29 1 149 10 975 30 1 147 15 1 155 31 1 127 16 1 155 INSTRUCTIONS On thi s format, list the average daily unit power level in MWe-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
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UNIT SHUTDOWNS AND POWER REDUCTIONS
. DOCKET NO. sn_ivn
- ^
UNIT NAME wenn<r.
2-DATE-11fis/s4 REPORT MONTH october 1984 COMPLETED BY a_ x n.,nri.
TELEPHONE vo4-272_ m,-
"s_3 o o, g License y
Cause'& Corrective:
e3?
"a v"E e
Ns.
Date
%y ygc Event Be En
~ Action to o
a s-o
.o os2
%.8 a.g N 55 E
$ dis Report #
&S
$8 Prevent Recurrence 54-P 84-10-11 S
B CC VALVEX Turbine Valve Movement Test 55-P 84-10-13 F
A CH VALVEX Repair Packing on Feedwater Regulating Valve.
.56-P 84-10-19 F
A SF INSTRU Repair a Safety Injection Valve j
57-P 84-10-19 F
A CH XXXXXX Feedwater Pump Control Oil Problems 14 84-10-23 F
56.22 A
3 CA INSTRU Abraided Cable to Shutdown Bank Controls 15 84-10-25 F
4.40 A
3 CH PUMPXX-High Discharge Pressure on Feedwater Pump 58-P 84-10-26 F
B IB INSTRU._
Nuclear Instrumentation Recalibration 59-P 84-10-31 F
A SF XXXXXX Upper Head Injection Chemistry Problems b
1 1
2 3
4.,
Reason:
Method:
Exhibit G - Instructions S
led A-Equipment Failure (Explain)_
1-Manual.
for Preparation of Data B-Maintenance or Test-2-Manual Scram Entry Sheets for Licensee-C-Refueling 3-Automatic Scram Event Report (LER)
D-Regulatory Restriction 4-Other (Explain)
File' (MREG-0161)
E-Operator Training 6' License Examination F-Administrative 5
G-Operational Error (Explain)
. Exhibit.I:- Same Source H-Other (Explain)
.'(4/77)
DOCKET NO: 50-370 UNIT: McGuire 2 DATE: 11/15/84 NARRATIVE
SUMMARY
Month:
October 1984 The unit has one turbine valve movement test. A forced reduction occurred when packing on a feedwater reg. valve required repair. Additional problems with a feedpump also kept the unit at reduced load. While performing a control rod movement PT on 10/19, the "B" shutdown bank moved when the "B" Control Bank was selected. Technicians working on the problen pulled a circuit card and the Shutdown Bank dropped causing a trip. An abraided cable was repaired and two circuit cards were replaced. The unit tripped shortly after startup when the feedpump increased discharge pressure due to a faulty signal, causing the pump to trip along with a turbine / Reactor trip. The unit held at 97% for incore/excore calibration but was forced to reduce power to below 46% by Tech Spec because of excessive Nitrogen in the Upper Head Injection system.
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MONTHLY REFUELING'INFORMATION REQUEST 1.
Facility name:
McGuire' Unit'2' 2.
Scheduled next refueling shutdown:
January 1985-s 3.
Scheduled restart following refueling:
March 1985 4.
Will refueling or resumption of operation thereaf ter require.a technical specification change or other license amendment?
Yes If yes, what will these be?
Technical Specification Revision 1
1 If no, has reload design and core configuration been reviewed by Safety Review Connittee regarding unreviewed safety questions?
N/A 5.
Scheduled date(s) for submitting proposed licensing action and supporting information:
N/A 6.
Important licensing considerations (new or different design or supplier, unreviewed design or performance analysis methods, significant changes in design or new operating procedures).
N/A 4
3 7.
Number of fuel assemblies (a) in the core:
193 (b) in the spent fuel pool:
0 8.
Present licensed fuel pool capacity:
1463 Size of requested or planned increase:
9.
Projected date of last refueling which can be accommodated by present licensed capacity:
DUKE POWER COMPANY Date:
November 15, 1984 Name of
Contact:
J. A. Reavis Phone:
704-373-7567 J
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McGUIRE NUCLEAR STATION Monthly Operating Status Report 1.
Personnel Exposure For the month of September, no individuals exceeded'10 percent of their.
allowable annual radiation dose limit.
. 2.
The-total station liquid release for September has been compared with
'the Technical Specifications maximum annual dose commitment and was less than 10 percent of this limit.
The total station gaseous' release for September has been compared with the Technical Specifications maximum annual dose commitment'and was less than 10 percent of this limit.
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9 DuxE POWER GOMPANY P.O. BOX 33180 CHARLOfrTP, N.O. 28242 HALH. TUCKER TER.EPHONE
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November 15, 1984 (ro4) ora-4sa IrtJCLEAR PN'UT3 Ole
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C Director
' Office of' Inspection and Enforcement U. S. Nuclear Regulatory Commission-Washington, D. C.
20555 Attention: Document Control Desk Re: McGuire Nuclear Station Docket No. 50-369, -370
Dear Sir:
Please find attached information concerning the performance and operating status of the McGuire Nuclear Station for the month of October 1984.
Very truly yours,-
' /d k-x Hal B. Tucker JAR:scs Attachments cc: Regional Administrator Mr. Ralph Birkel U. S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Region II U. S. Nuclear Regulatory Commission 101 Marietta Street, Suite 2900 Washington, D. C.
20555 Atlanta, Georgia 30323 Mr. Phil Ross American Nuclear Insurers U. S. Nuclear Regulatory Commission c/o Dottie Sherman, ANI Library NNBB-5715 The Exchange, Suite 245 Washington, D. C.
20555 270 Farmington, Avenue Farmington, Connecticut 06032 INP0 Records Center Suite 1500 Ms. Judy Dovers 1100 Circle 75 Parkway Nuclear Assurance Corporation l
Atlanta, Georgia 30339 5720 Peachtree Parkway I
Norcross, Georgia 30092 Senior Resident Inspector McGuire Nuclear Station p
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