ML20098C167

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Monthly Operating Rept for Aug 1984
ML20098C167
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 08/31/1984
From: Brons J, Kelly L
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
IP-LK-3390, NUDOCS 8409260450
Download: ML20098C167 (7)


Text

.

G OPERATING DATA REPORT DOCKET NO.

50-286 DATE sept. 3, 1984 COMPLETED BY L Kallv TELEPHONE (914) 739-8200 OPERATING STATUS

1. Unic Name: Indian Point No. 3 Nuclear Power Plant Jotes
2. Reporting Period:

Auqust 1984

3. Licensed Thermal Power (MWt):

3025

4. Nameplate Rating (Gross MWe):

1013 965

5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):

1000 965

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratingi(Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted,II Any (Net MWe):
10. Reasons For Restrictions. If Any:

Tnis Month Yr..to.Date Cumulative 744 5855.0 70,176.0

11. Hours in Reporting Period 40.

5101.58 39,526.08

12. Number Of I'ours Reactor Was Critical
13. Reactor Reserve Shutdown Hours 0

0 0

14. Hours Generator On.Line 653.17 4875.62 38,017.62
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1.RR6.630.33 13.936.564.24 100.362.209.24
17. Gross Electrical Energy Generated (MWH) 598,390 4.540.915 30.907.525
18. Net Electrical Energy Generated (MWH1 575,245 4.370.133 29.614.311
19. Unit Service Factor 87.8 83.3 54.2
20. Unit Availability Factor 87.8 83.3 54.2
21. Unit Capacity Factor (Using MDC Net) 80.1 77.3 a3.7 80.1 77.3 43.7
22. Unit Capacity Factor (Using DER Net)
23. Unit Forced Outage Ra'e 3.3 15.1 22.6 l
24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Eacht:

l

'Mid Cycle Steam Generator innnectinn n*,nn for four wookn enrH nn - October 13, 1984 l

25 If Shur Down At End Of Report Period, Estimated Date of Startup:

26 Units in Test Status a Prior to Commercial Operations:

Forecast Achieved INITIAL CRITICALITY I

INITIA L ELECTRICITY g

l COMMERCI AL OPERATION d

8409260450 840831 l

PDR ADOCK 05000286

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r AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-286 Indian Point UNIT No. 3 DATE sent.

3.

1984 COMPLETED BY L-Kellv TELEPHONE (914) 739-8200 MONTH' August-1984 DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)

(Mwe. Net)

I 928 17 927 2

921 18 928 3

939 gg 915 937 904 4

20 i

5 936 925 2g 823 6

7 931 23 17 8

930 24 653 9

931 23 920 931 892 10 26 t

932 iI 27 757 12 9M 28 n

13 930 29 0

14 929 30 n

927 15 31 416 927 l

l 1

INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the reportina month. Compute to the nearest whole megawatt.

(9/77)

's DOCKET 'lO.'

50-286 UNIT SiluTDOWNS /.ND POWER CEl>UCTIONS

~ UNIT NAME Tnai m hi e m, 3 DATE sept-1.

1994 COMPLETEI) BY T._

retiv REl' ORT MON 111 lELEPHONE' 914-739-8200 e.

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g Licensee E.

$4 Cause & Corsective j

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O Psevent Recurrence 5

10 840882 F

22.25 A

3 84-013-00 CH PUMPXX MBFP Control Oil System caused feed flow perturbations which ultimately led to.a hi-hi level steam generator unit trip.

11 840828 s

68.58 A

1 N/A HF IITEXCII Repair of condenser circulating water D

condenser seams and electrical generater hydrogen coolers.

I 2

3 4

F: Foiced Reason:

Meshod:

Exhibit F-Insisuctiims S: Scheduleil A-Etiuipment Failure (Explain) 1 Manual los Picparation of Data It-Maintenance oi Test 2-Manual Sesam.

linisy Sheets foi 1.icensee C-Refueling 3 Automatic Scram.

livent RepinI (l.l:R)17ile (NURl:G-D Regulatory Restsiction 4-Other I Explain t 0161)

I!-Opesatos Tsaining & license Examinaliini I -Adnunig rative 5

G Opciational Es tor (E xplain) lishibit11 Same Sonice l'7/77) 11 Other (lixplain)

MONTHLY MAINTENANCE REPORT Auguat 1984~

MONTH 4- )' -

WRf DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION 4952

-8/13/84 31 Steam Generator Failed closed Replaced SOV-1314 Blowndown Valve 1214 Solenoid Valve 1314 r

5027 8/27/84 R11/12 Containment Failed closed Replaced coil in solenoid Isolation Valve Solenoid Valve 1535 5051 8/29/84 R11/12 Containment Failed closed Replaced coil in solenoid Isolation Valve Solenoid Valve 1536 l

l

- 5057 8/30/84 35 Fan Cooler Unit Motor cooler coil leak Replaced motor cooler Motor Cooler 5044 8/31/84 31 Control Will not maintain Repaired leak in sight glass Room Air Conditioner temperature and recharged with refrigerant 5052 8/31/84 32 Steam Generator Diaphragm leaks Replaced valve diaphragm Blowndown Valve 1215 5059 8/31/84 32 Service Water Pump Motor trips on ovrrload Repaired gearbox Zurn Strainer

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4

,;j MONTHLY REPORT MONTHLY I & C CATEGORY I REPORT August 1984 MONTH WRf DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION IC-1-2886 6-19-84 Channel B Steam Flow Indicates low Replaced magnetic' amplifiers Indicator 419B in loop current repeater-IC-1-2883 7-2-84

  1. 32 Steam Generator Low Level Bistable setpoint drifts Replaced bistable Mismatch Bistable LC-427G IC-1-2884 7-2-84
  1. 34 Steam Generator Iow-Low Bistable setpoint drifts Replaced bistable IC-1-2861 7-5-84 Waste Gas Process Radiation Meter reading erretic, Repaired connections on Monitor R20 high alarm up ccnstantly

. drawer connector IC-1-2933 7-17-84 Main Turbine Independent Open relay coil on relay

-Replaced relay coil Electric Overspeed Protection VA3 System IC-1-2966 8-6-84 Overtemperature A T Test Light No response to test Replaced defective test-TC-412AX relay relay IC-1-2967 8-7-84 Reactor Trip Relay RT-6B Relay coil open Replaced relay IC-i-2932 8-10-84 Wide Range Noble Gas Monitor RM23 readout does not Replaced RM23 R-27 respond t.o operator readout module-commands t

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SUMMARY

OF OPERATING EXPERIENCE AUGUST 1984 Indian Point Unit'3 was synchronized to the bus for a total of 653.17

' hours producing a gross generation of 598,390 MWH for this reporting

. period

'As a result of a feedwater transient'a unit trip occurred on August 22 oat 2122 hours0.0246 days <br />0.589 hours <br />0.00351 weeks <br />8.07421e-4 months <br /> due to a hi-hi" steam generator level. The investigation revealed that a leak in a control oil hose caused the perturbation in the

- main boiler. feed pump control oil system. The' unit was returned to service on August 23 at 1937 hours0.0224 days <br />0.538 hours <br />0.0032 weeks <br />7.370285e-4 months <br />. On August 28 at 0133 hours0.00154 days <br />0.0369 hours <br />2.199074e-4 weeks <br />5.06065e-5 months <br /> the unit was removed from service in order to perform repairs on the main condenser

'l circulating water seams, and repair the. main electrical generator coolers.. The unit was returned to service-on August 30 at 2208 hours0.0256 days <br />0.613 hours <br />0.00365 weeks <br />8.40144e-4 months <br />.

' The cumulative capacity factor based on a NDC net weighted average through August 31, 1984 is 46.1%.

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Indian Point 3 Nue, leet Power Plant P.O. Box 215 Buchanan, NewYbrk 10511 914 739.8200

  1. > NewWrkPbwer 4# Authodty September 14, 1984 IP-LK-3390 Docket No. 50-286 License No. DPR-64 Director, Office of Inspection and Enforcement U. S. Nuclear Regulatory Conanisulon Washington, D. C. 20555 Attention: Document Control Desk

Dear Sir:

Enclosed you will find twelva copies of the monthly operating report relating to Indian Point 3 Nuclear Power Plant for the month of August, 1984.

Very truly yours, A

Tohn. Brons Resident Manager LK/bam Enclosures (12 Copies) cc:

Dr. Thomas E. Murley, Regional Administrator Region 1 U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 IP3 Resident Inspectors' Office George Wilverding (SRC), WPO J. P. Bayne, WPO S. V. Fuller, NYO W. R. Yario, NYO INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 9

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