ML20097A235
| ML20097A235 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 06/30/1984 |
| From: | Mcnamara A ROCHESTER GAS & ELECTRIC CORP. |
| To: | |
| Shared Package | |
| ML20097A196 | List: |
| References | |
| NUDOCS 8409130214 | |
| Download: ML20097A235 (2) | |
Text
_
Revised..Augunt 3, 1984 1,
DOCKET NO.
50-244 UNIT NAME si,Ginas Station -
I,', '
UNIT SHUTDOWN AND POWER REDUCTIONS DATE Aucust 3_
1984 COMPLETED HY EA M.h-Andrew E.
McNamara REPORT MONTH Jim n. 1984 TELEPilONE 1(315)'524-4446 Ext. 301 m
N C
C Cause & Corrective Licensee s,
v oO c
]..c{j No.
Date
{
jj 2
Event
{g Act;on to s-d5 g
li Ji e Report 8
- d
!u Prevent Recurrence 2
g u
O 84-4 Began on F
31.75*
A 3**
N/A HA Exciter Air Cooler gasket, poor 5-30-84 Failure compression.
Shimmed air Ended on cooler to provide proper 6-02-84 alignment; sealant on both sides of gasket.
i
- Hours in June only.
- Corrects typographical error in previous report.
F: Forced Reason:
Method:
Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling
~
4-Other (Explain) 0161) 3-Automatic Scram.
Event Report (LER) File (NUREG-D-Regulatory Restriction E-Operator Trair:ing & License Examination F-Administrative 5
G-Operational Error (Explain) w
..... in e v. in n H-Other (Explain)
Exhibit 1 - Same Source 8409130214 840003 PDR ADOCK 05000244 R
- f.
47Y '
Revised August 3, 1984 NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50-244 UNIT,Ginna Station, Unit #1 DATE Auguat 3, 1984-COMPLETED BY M h M M ^--
Andrew E.
McNbmara TELEPHONE 1 (315) 524-4446 EXT. 301 at Ginna MONTH June 1984 The. unit.was returned to service on June 2,
1984 after repairs-were effected on the turbine generator exciter cooler.
Repairs are detailed on Page 3 of the previously transmitted report.
The reactor power level was escalated to ~ 87% on June 3; on that date a power _ reduction was initiated to ~ 50% power for inspectionHof the "B"
Condenser for suspected tube plugging problems.
The power level was gradually increased on 6/5 to ~ 90% and full 100% power level was-not reached until 6/8 due to heater drain tank problems.
The reactor power level remained at 100% until 6/15 when it was reduced to ~ 98% to perform periodic tests on the Auxiliary Feedwater System.
On_6/27 the reactor power level was reduced to ~ 90% power level'due to a turbine runback initiated by-a dropped rod signal, caused by an I/C technician pulling control power fuses instead of the instrument. power fuses required by his_ procedure.
Immediate reinstatement of the fuses stopped the rod drop signal before total runback was achieved.
.