ML20097A235

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Rev to Unit Shutdown & Power Reductions & Narrative Summary of Operating Experience from Monthly Operating Rept for June 1984
ML20097A235
Person / Time
Site: Ginna Constellation icon.png
Issue date: 06/30/1984
From: Mcnamara A
ROCHESTER GAS & ELECTRIC CORP.
To:
Shared Package
ML20097A196 List:
References
NUDOCS 8409130214
Download: ML20097A235 (2)


Text

_

Revised..Augunt 3, 1984 1,

DOCKET NO.

50-244 UNIT NAME si,Ginas Station -

I,', '

UNIT SHUTDOWN AND POWER REDUCTIONS DATE Aucust 3_

1984 COMPLETED HY EA M.h-Andrew E.

McNamara REPORT MONTH Jim n. 1984 TELEPilONE 1(315)'524-4446 Ext. 301 m

N C

C Cause & Corrective Licensee s,

v oO c

]..c{j No.

Date

{

jj 2

Event

{g Act;on to s-d5 g

li Ji e Report 8

  1. d

!u Prevent Recurrence 2

g u

O 84-4 Began on F

31.75*

A 3**

N/A HA Exciter Air Cooler gasket, poor 5-30-84 Failure compression.

Shimmed air Ended on cooler to provide proper 6-02-84 alignment; sealant on both sides of gasket.

i

  • Hours in June only.
    • Corrects typographical error in previous report.

F: Forced Reason:

Method:

Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C-Refueling

~

4-Other (Explain) 0161) 3-Automatic Scram.

Event Report (LER) File (NUREG-D-Regulatory Restriction E-Operator Trair:ing & License Examination F-Administrative 5

G-Operational Error (Explain) w

..... in e v. in n H-Other (Explain)

Exhibit 1 - Same Source 8409130214 840003 PDR ADOCK 05000244 R

PDR

f.

47Y '

Revised August 3, 1984 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.

50-244 UNIT,Ginna Station, Unit #1 DATE Auguat 3, 1984-COMPLETED BY M h M M ^--

Andrew E.

McNbmara TELEPHONE 1 (315) 524-4446 EXT. 301 at Ginna MONTH June 1984 The. unit.was returned to service on June 2,

1984 after repairs-were effected on the turbine generator exciter cooler.

Repairs are detailed on Page 3 of the previously transmitted report.

The reactor power level was escalated to ~ 87% on June 3; on that date a power _ reduction was initiated to ~ 50% power for inspectionHof the "B"

Condenser for suspected tube plugging problems.

The power level was gradually increased on 6/5 to ~ 90% and full 100% power level was-not reached until 6/8 due to heater drain tank problems.

The reactor power level remained at 100% until 6/15 when it was reduced to ~ 98% to perform periodic tests on the Auxiliary Feedwater System.

On_6/27 the reactor power level was reduced to ~ 90% power level'due to a turbine runback initiated by-a dropped rod signal, caused by an I/C technician pulling control power fuses instead of the instrument. power fuses required by his_ procedure.

Immediate reinstatement of the fuses stopped the rod drop signal before total runback was achieved.

.