ML20093K283
| ML20093K283 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 09/30/1984 |
| From: | Maxwell D, Scott D COMMONWEALTH EDISON CO. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| 84-1110, NUDOCS 8410170260 | |
| Download: ML20093K283 (14) | |
Text
.
OPERATING DATA REPORT DOCKET NO. 050-237 DATE Oct. 4.
1984 COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 OPERATING STATUS NOTES 1.
Unit Name:
Dresden II 2.
Reporting Period:
gone,mhor. 19a4 3
Licensed Thermal Power (MWt):
2,527-4.
Nameplate Rating (Gross MWe):
828-5 Design Electrical Rating (Net NWe): 794 6.
Maximum Dependable Capacity (Gross NWe):
812 7.
Maximum Dependable Capacity (Net MWe):
772 8.
If Changes Cccur in Capacity Ratings (items 3 Throi.gh 7) Since Last Report, Give Reasons:
i I
9 Power Level to Which Restricted, if Any (Net MWe):
10.
Reasons For Restrictions, if Any:
j This Month Yr-to-Date Cumul.at ive.
11.
Hours in Reporting Period
-720 6.57s 126.095 12.
Number of Hours Reactor Was Critical 720.0 6.387.3 98.611.8 13.
Reactor Reserve Shutdown Hours n
n 0
14.
Hours Generator On-Line 72n.0 A. ?ns a 97.191.3 15.
Unit Reserve Shutdown Hours 0
o 0
16.
Gross Thermal Energy Generated (MWH).
-1.414.370 14.408.906 191,103,542 17 Gross Electrical Energy Generated (MWH) 650.725 4.627.281 61.129.480 18.
Het Electrical Energy Generated. (MWH) 426.112 4.404.398 57.812.662 19 Unit Service Factor 100.0 95.6 77.1 20.
Unit Availability Factor 100.0 95.6 77.1 21.
Unit Capacity Factor (Using MDC Net) 76.7 86.8 59.4 i
22.
Unit Capacity Factor (Using DER Net) 74.5 84.4 57.7 l
23.
Unit Forced Outage Rate 0
4.4 II.2 24.
Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
i Refueling outage scheduled to begin 10-05-84 for approximately 12 weeks.
25 If Shut Down At End Of Report Period, Estimated Date of Startup:
8410170260 840930
{DRADOCK 05000237 h
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OPERATING DATA REPORT DOCKET NO.
050-249 DATE Oct. 4.
1984 COMPLETED BY D. C. Maxwell i
TELEPHONE g,q gq7_797n OPERATING STATUS NOTES
- 1. -Unit Name:
Dresden III 2.
Reporting Period: September, 1984 3
Licensed Thermal Power (MWt):
2,527 4.
Nameplate Rating (Gross MWe):
828 5.
Design Electrical Rating (Net MWe): 794 6.
Maximum Dependable Capacity (Gross MWe): 812 7.
Maximum Dependable Capacity (Net MWe):
773 8.
If Changes Occur in Capacity Ratings (items 3 Through 7) Since Last Report, Give Reasons:
.t 9
Power Level to Which Restricted, if Any (Net MWe):
10.
Reasons For Restrictions, if Any:
a This Month Yr-to-Date Cumulativo.
t 11.
Hours in Reporting Period 720 6.575 115.680-12.
Number of Hours Reactor Was Critical 6 14.9 1.908.1 84.753.1 13 Reactor Reserve Shutdown Hours 0
0 0
14.
Hours Generator On-Line 567.5 1.441.3 81.302.4 i
15 Unit Reserve Shutdown Hours 0
0 0
)
16.
Gross Thermal Energy Generated (MWH) 1.120,500 2,838,834 162,799,932 17 Gross Electrical Energy Generated (MWH) 1A6_s22 865,575 52.818.494 18.
Net Electrical Energy Generated.(MWH) 12s_20s 797,501 51.028.085 19 Unit Service Factor 78.8 21.9 70.3 20.
Unit Availability Factor 78.8 21.9 70.3 21.
Unit Capacity Factor (Using MDC Net) 58.4 15.7 57.1 l
22.
Unit Capacity Factor (Using DER Net) 56.9 15.3 55.6 j
23 Unit Forced Outage Rate 21.2 12.7 12.7
)
24.
Shutdowns -Scheduled Over Next 6 Months (Type Date, and Duration of Each):
25.
If Shut Down At End Of Report Period, Estimated Date of Startup:
10-14-84 i
i ly l
~_ -,,
DOCKET NO. 050-237 UNIT NAME Dresden II UNIT SHUTDOWNS AND POWER REDUCTIONS.
DATE October 4, 1984-COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 REPORT MONTH 9entember. 1984 METHOD OF LICENSEE CAUSE & CORRECTIVE 2
i NO.
DATE' TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COMPONENT ACTION TO j
(HOURS)
DOWN' REACTOR 3 REPORT F CODE 4 CODES PREVENT RECURRENCE t
l None i
4 L
4 b
l
)
i 1
2 3
4 F
Forced Reason:
Method:
Exhibit G-Instructions for S: Scheduled A-Equipment Failure (Explain) 1-Manual
' Preparation of Data j
B-Maintenance on Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (
) File l
D-Regulatory Restriction 4-Other (Explain)'
(NUREG-0161) j E-Operator Training & License Examination.
F-Administrative 3
G-Operational Error 3
H-Other (Explain) a
DOCKET NO. 050-249 UNIT NAME Dresden~III-UNIT SHUTDOWNS AND POWER REDUCTIONS DATE October 4.
1984-COMPLETED BY D. C. Maxwell.
TELEPHONE (815) 942-2920 REPORT MONTH Seotember. 1984 METHOD OF LICENSEE CAUSE & CORRECTIVE NO.
DATE' TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COMPONENT ACTION TO l
(HOURS)
DOWN REACTOR 3 REPORT F CODE 4 CODES PREVENT RECURRENCE i
3 84-9-11 11:47 A
Rx Remained EHC oil leak.
Critical 4
84-9-25 140:46 A
Manual at 4
Cohdenser tube leak.
l 0452 of 9-25-84. Rx Scram at 0530 of 9-25-84.
l t
1 1
i
}
4 f
i i
1 2
3 F
Forced Reason:
4 Method:
Exhibit G-Instructions for i
S: Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (
j D-Regulatory Restriction 4-Other (Explain)
(NUREG-0161).
) File 1
E-Operator Training & License Examination.
F-Administrative i
i G-Operational Error i
l H-Other (Explain) i
AVERAGE DAILY UNIT POWER LEVEL f~,
DOCKET NO. 050-237-UNIT II-t DATE - Oct. 4, 1984 COMPLETED BY D. C. Maxwell' TELEPHONE-815/942-2920 MON 1H September, 1984 DAY AVERAGE' DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (HWe-Net)
(MWe-Net) 1 644 17 6a ?
j.
2 698
- 18 ag6 1
3 669 19 361
)
l 4
620 20 389 1
Q 5
716 21 445
[
6-561 22 639 7
672 23 630 1
i 8
664 24 642 9
668 25 624 10 583 26 611 11 667 27 634 12 657 28 489 13 654 29 463 I4 647 30.
513
.s l
15 649 31 16 584
- O i
._,....,,..e
,,,v-~
-.,<~,--ve~-rvr-~-~~-~'r~-
i
~
AVERAGE DAILY UNIT POWER LEVEL
.f3 DOCKET NO. 0s0-249 UNIT III DATE Oct. 4, 1985 COMPLETED BY
-D. C. Maxwell TELEPHONE 815/942-2920 MONTH sentember. 1984 DAY.
AVERAGE DAILY POWER LEVEL DAY AVERAGE-DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 722 17 742 2
746-18 522 3
543 19 390 4
668 20 443 Q
5 701 21 406 6
769 22 415 7
683' 23 4 16 8
737 24 228 9
453 25 6
10 616 26 0
11 116 27 0
12 473 28 0
13 672 29 0
14 730 30 0
15 725 31 16 685 O
m
DRESDEN UNIT 2 SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE dESULT CORRECTIVE ACTION f
Open Ind, on Corrective W.R. #32059 N/A N/A Re-wired connection to the 2-2499-3B 2499-4 B and 4B valves per electrical prints.
Re-adjusted limits.
2-2499-3A Corrective W.R. #32061 N/A N.A Re-connected wire to 2-2499-3A valve.
V lv:2
.~ - -
m, 3
n
, 3, DRESDEN UNIT 3 SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984:
4 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION i
q B Recirc.' Loop Preventive W.R. #34183 N/A N/A Installed new heaters and cleared
) Equalizer By-jumper log.
paso Valve 3-202-9B Refuel Grapple Preventive W.R. #36234 N/A N/A.
Set upper limit as-instructed.
MOV 2301-3 Preventive W.R. #36268
.N/A N/A Replaced light' bulb.
j Ccntrol Sta.
I U3 HPCI Preventive W.R. #24006 N/A N/A Replaced solenoid..
lMO 1301-1 Preventive W.R. #27424 N/A N/A Replaced motor.
lMO3-202-5A Preventive W.R. #31011 N/A N/A Removed and replaced damaged seal tite.
!CCSW Vault Preventive W.R. #30982
.N/A-N/A Sealed; penetration.with silicon RTV.
iPenttrctions LPCI H2at Ex-Preventive W.R. #27140 N/A N/A Increased torque setting.
chenger Dis-charge Valves,
!EPN #3-1501-3A l
l MO.1402-25A Preventive W.R. #28504 N/A.
N/A Completed data sheet to verify the'as-
[
found setting.or catalogue number on MO 1402-25A.
l
'N20B Jat Pump' Preventive W.R. #26670 N/A N/A Removed-indication found during PT-Instrument inspection.
Reacter Prot.
Preventive W.R.'#33594' N/A N/A Removed and installed jumpers.'
Syctem U3.Rx Scrams
...a..
DRESDEN UNIT 3 SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANQE NUMBER CAUSE RESULT CORRECTIVE ACTION SBLC Preventive W.R. J33102 N/A N/A Set thermostat to 90. Operating ok.
Cora Spray Preventive W.R. #33723 N/A N/A Removed, cleaned and installed jumper.
Valva 3-1402-24A CRD P-4 Preventive W.R. #33908 N/A N/A Replaced solenoid.
P-12 Preventive W.R. #33907 N/A N/A Replaced solenoid.
MSIV Pilot Preventive W.R. s34036 N/A N/A Tested all relays.
Ralryz, EPN
- 2031(2) (A,B, C,D) R1 (2)
MOV 3-1501-20A Preventive W.R. #3}) N/A N/A Removed an,d reinstalled motor operator for 1501-20A valve after drying it out. MO 1402-25B Preventive W.R. #28503 N/A N/A Adjusted limits and setting on MOV (25C) 1402-25B. IRM #18 Corrective W.R. #30623 N/A N/A Replaced selector switch on IRM #18. Refual Grapple Preventive W.R. #31919 N/A N/A Removed and installed temporary jumpers. AO'c 220-44, Preventive W.R. #21158 N/A N/A Lubricated ASCO solenoid valves 220-46 and A0-3-220-44, -46, and -47. 220-47 LPRM 16-25A Preventive W.R. #34395 N/A N/A Replaced transistor and integrated. U3 24/48 Preventive W.R. #36594 N/A N/A Adjusted voltages. Bottom B Chcrg rs
F l DRESDEN UNIT 3 9 SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984-- 4 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT . CORRECTIVE ACTION s\\ 3D CCSW PP Preventive W.R. #32506 N/A N/A-Remounted-spring.and adjusted. linkage.. Brocker U3 HPCI Room Preventive W.R. #34243 N/A N/A-Replaced and cleaned contactor. x Cooler 5 . D3 HPCI Room Preventive W.R. #32855 N/A N/A Replaced both bel'ts. Cooler . U3 HPCI Room Preventive W.R. #33858 N/A N/A Replaced both bearin'gs. Cooler , #3 Dingel Preventive W.R. #33859 N/A N/A Performed quarterly inspection. ~ l Genarctor ^ MSIV, EPN Preventive W.R. #29613 N/A N/A Replaced terminal blocks.on all MSIV's. " #AO-3-203 l t Supply Air Preventive W.R. #35996 N/A N/A' Replaced solenoid. , SDisnaid to , AO 3-2301-31 i-f'AcndBLPCI Preventive W.R. #35620 N/A N/A-Cleaned,and painted A and B' mot'rs. o
- . Pump MI; tors, s
i EPN.#3A & 3B 1502
- i. Main Steam Line Preventive W.R. #36063 N/A N/A Replaced bad' fitting on PSW 261-213.
i I High Flow Switch l 4 !,LPRM48-4IB Preventive W.R. #34392 N/A .N/A Replaced LPRM card.- 1 4 I . J
-m f DRESDEN UNIT 3 ~ SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION j \\ LPRM 48-33 D Preventive W.R. #34394 N/A N/A Repaired wire connection on socket in full core display 903-5. IRh Ch. 12 Preventive W.R. #34573 N/A N/A Adjusted gain on IRM pre-amp. 3-1501-13A Preventive W.R. #34996 N/A N/A Relamped/ cycled valve several times. Indication ok. Pr;s;ure Sup-Preventive W.R. #35076 N/A N/A Replaced solenoid with new S.R. solenoid. prrc0icn Nitro-g2n M'keup to TcruJ ASCO Valv3 A0 3-1601-59 3A-1402 Core Preventive W.R. #35617 N/A N/A Cleaned and painted motor. Spray Motor CCSW Pump Preventive W.R. #35618 N/A N/A Cleaned and painted all motors. Mottra 1501-44A,B,C,D 3-1501-21B Preventive W.R. #35036 N/A N/A Adjusted packing. Refuel Grapple Preventive W.R. #36177 N/A N/A Adjusted frame hoist upper limit to accomodate unloading of D1 fuel from TN-9. LPRM 08-25A Corrective W.R. #34393 N/A N/A Replaced LPRM 8-25A transistor #08. HPCI T3 stable Corrective W.R. #34246 N/A N/A Adjusted HPCI testable check' valve Chnck Valve A0 3-2301 - 7 limits. A0 3-2301-7
l DRESDEN UNIT 3 SAFETY RELATED MAINTENANCE - SEPTEMBER, 1984 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION 1 CRD ASCO Relays Corrective W.R. #35343 N/A N/A Tightened fittings on CRD ASCO valves. Cnd Air Lines APRM'#4 Re-Corrective W.R. #34080 N/A N/A Replaced amplifier board on'APRM #4-ctrdsr, EPN recorder. -#RR3-750-10B LPRM's Preventive W.R. #29697 N/A N/A Removed and re-installed LPRM cables for normal maintenance during refuel' outage. LPRM 48-33A Corrective W.R. #34389 N/A N/A Replaced Q8 transistor on LPRM 48-33A card. T 1 l
m ~
SUMMARY
-0F OPERATING EXPERIENCE UNIT ONE SEPTEMBER, 1984 The status of Unit I remains shutdown with all fuel removed. The environ-ment and equipment continues to be maintained as needed. On August 31, 1984, an announcement was made by CECO. Corporate Offices that as of this date Unit I has been officially retired. Chemical cleaning activities are continuing. During the period September 13 through September 17, 1984, the "hundred hour" run of chemical cleaning solu-tion through the piping was accomplished. Since then, there has been three (3) . flush and drain operations to remove any residual chemicals and contamination. The solution injected has been very effective in drastically lowering dose rates.
.+.
SUMMARY
OF OPERATING EXPERIENCE UNIT TWO SFPTEMBER, 1984 2 Unit 2 entered the month' operating at a power level of 725 MWe and operated continuously during the entire month (with normal power reductions-for weekend surveillances) reaching a power level of 747 MWe with a capacity factor of 75.00% and an availability of 100%. 1 r i . =..
y
SUMMARY
OF OPERATING EXPERIENCE UNIT THREE . SEPTEMBER, 1984 09-01 to 09-11 Unit 3 entered the month operating at a power level of 725 MWe and operated until September 11, 1984, when it was taken off-line to repair an EHC oil leak (the Rx remained critical). 09-11 to 09-30 The unit was brought on-line in the afternoon of September 11, 1984 and operated until September 25, 1984 when it was taken off-line.to repair a main condenser leak. After the Rx was subcritical, a scram occurred because of low condenser vacuum. Condenser inspection and repairs continued through the remainder of the month. Capacity factor for the month was 57.80% and availability was 78.81%.
UNIQUE REPORTING REQUIREMENTS' MAIN STEAM RELIEF VALVE OPERATIONS i i Relief valve operations during the reporting period are summarized in the following table. The table includes information as to which relief valve was actuated, how it. was actuated, and the circumstances resulting in its actuation. I l ) Valves Description Unit Date Actuated Actuations Conditions of Events 1 09-01-84 to 09-30-84 None l 2 None 3 None l n,
TO's ' Gen 2ral cc:unting- '307-Ediagn. MONTHLY REPORT OF PRODUCTION FUEL OIL ^ REPORTING AREA Dresden Sta. # 12 DIESEL FUEL OIL IGNITION FUEL OIL "-'" '"' 'u' . KNTH September 19 84 0o^S'u"S'"u" 4 PURCHASL ORDER $NVOICE APPROVAL GALLONS DATE NUMBER NUMBER '9-2A-R4 OO72R6 DR-s 5.500 i i T i A. INVENTORY - BEGINNING OF MONTH 43,955 PLUSl B. TOTAL GALLONS INVOICED 5,500 c. TOTAL GALLcNS wCCcivEo m $NvolCEo 5,500 i MINUSS D. TOTAL GALLONS CONSUMEJ 4,435 i E. TOTAL GALLONS NOT INVOICEO IN PREVIOUS MONTH F. INVENTORY - END OF MONTH l FUNCTION M ER 51106 STATTON cc: D. L. Maxwell SUFERINTENDENT g u s C.E.CO. 36 2036fS) 10 79'
October 4,1984 DJS LTR: 84-1009 TO: Technical Services Tech Center, Maywood
SUBJECT:
Dresden Station Nuclear Fuel Consumption, Fuel Oil Therms and Auxiliary Power for the Month of' September , 1984 Unit 2 Unit 3 Nuclear Therms 48,272,451.03 13,242,667.32 MWT Days 58,932.08 46,687.5 Therms Diesel Oil 3,038 3,038 Gallons Diesel Oil 2,217.5 2,217.5 Auxiliary Power Lift Pump 2,107 1,619-Sprays & Lighting 565 435 Prepared byI b. D. C. Maxwell Technical Staff Approved by l_ D. J. S96tt /f Statio@'up#intendent Dresden Nuclear Power Station DJS:DCM:hjb cc: F. Kurasz T. Lamantia l C. Larson Comptroller's Staff J. Brunner D. Maxwell J. Tiemann File / Numerical
O Commonweaith Edison Dresden Nuclear Power St1 tion R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 October 4,1984 DJS LTR: 84-1110 Director, Office of Inspection and Enforcement United States Nuclear Regulatory Commission Washington, DC 20555 Attention: Document Control Desk
Dear Sir:
Enclosed, please find Dresden Station's operating data for last month. This information is supplied to your office per the instruc-tions set forth in Regulatory Guide 1.16. Sincerely, 0 D. . Scott Station Superintendent Dresden Nuclear Power Station DJS:DCM:hjb Enclosure cc: Region III, Regulatory Operations, U.S. NRC Chief, Division Nuclear Safety, State of IL U.S. NRC, Document Management Branch Nuclear Licensing Administrator Nuc. Sta. Div. Vice Pres. Manager, Tech. Serv. Nuc. Sta. Tech. Staff AE On-Site NRC Inspector Sta. Nuc. Eng. Dept. Comptro11er's Office PIP Coordinator INPO Records Center File /NRC Op. Data File / Numerical h 1, i _}}